• 제목/요약/키워드: Hydraulic Clutch System

검색결과 48건 처리시간 0.023초

자동변속기용 드럼클러치의 유동제어 성형공정 및 실험장치 개발 연구 (A Study on the Flow Control Forming Process and Experiment Device of Drum Clutch for Automatic Transmission)

  • 박종남
    • 한국기계가공학회지
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    • 제12권6호
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    • pp.69-76
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    • 2013
  • This paper presents the development of the FCF method for the manufacturing of final products using numbers related to the minimum amount of work. The utilized product is a drum clutch, which is part of the transmission of an automobile. A double acting press is secured first and a prediction of the forming load on the practical material is made through an experiment with a plasticine model. Also, a finite element simulation using product shape and properties is performed, as well as a press experiment. A double acting press is manufactured that is suitable for a double acting experiment with a conventional hydraulic press(200 tons). A peripheral device for the press is additionally designed for experimental purposes. And, the press has as its essential points the drive speed, stroke control, etc., all of which influence the forming and is modified. Especially, a laser system is used for velocity measurement of two punches. The forming load of a practical material is predicted in order to derive a forming load formula for cold conditions on the basis of approximate similarity theory. Finite element analysis of the relative velocity ratio(RVR), etc., for most suitable flow defect(unfilling, etc.) prevention is achieved as well. The results are verified through a press experiment.

차량용 자동변속기 유압제어계의 개발동향 (Trends in clutch actuating hydraulic control system of automatic transmission for vehicles)

  • 이일영;양경욱;윤소남
    • 오토저널
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    • 제17권5호
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    • pp.28-35
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    • 1995
  • 본 해설에서는 클러치 제어용 유압계 특성에 대하여 간략히 서술하고 각 장치즐의 장단점을 비교 검토함과 동시에, 본 저자들이 개발한 클러치 조작용 유압계에 쓰이는 압력조절장치에 대하여 설명한다. 1. 변속장치내 클러치 조작용 유압계 특성. 1.1 클러치 조작용 유압계 제어의 필요성. 1.2 변속시 충격 토크의 저감법. 1.3 클러치 조작용 유압계의 제어방식.

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트랙터의 기관속도(機關速度) 및 변속비(變速比)의 자동제어(自動制御)에 관(關)한 연구(硏究)(I) -기관속도(機關速度) 및 변속비(變速比) 제어(制御) 시스템- (Automatic Control of Engine Speed and Transmission Ratio for Efficient Tractor Operations(I) -Control Systems for Engine Speed and Transmission Ratio-)

  • 강성봉;류관희;오길근
    • Journal of Biosystems Engineering
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    • 제18권4호
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    • pp.305-316
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    • 1993
  • Fuel efficiency in tractor operations dep6nds on the selection of transmission gears and upon the engine being operated at or near maximum torque much of time. The objective of this study was to develop automatic control systems for tractor transmission ratio and governor setting so that the engine is operated at or near maximum torque as much of time as possible. An indoor test unit, which can be used to simulate tractor operation, was built in order to investigate the system design parameters and test the performance of the control system designed. The test-unit consists of engine, gear-type transmission, dynamometer, and control systems for transmission ratio and engine speed. Governor setting lever was controlled by a step motor, and the clutch and transmission levers were controlled by hydraulic cylinders and solenoid valves. The control systems showed good time responses which are assumed to be suitable for optimal tractor operation. The time required for shifting gears from clutch disengagement to engagement was about 1 second, which is almost the same as that for manual shift. And the settling time for engine speed control system was about 5 to 6 seconds.

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트랙터용 토로이달식 무단변속기 개발(1): 변속기 메커니즘 (Development of Toroidal Type Continuously Variable-Speed Transmission for Agricultural Tractor(1): Transmission Mechanism)

  • 김의한;이재천
    • 한국자동차공학회논문집
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    • 제10권3호
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    • pp.218-226
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    • 2002
  • This study was carried out to develop continuously variable-speed transmission(CVT) fur an agricultural tractor. The full-toroidal variator mechanism with flour discs and six rollers was utilized as a device fur changing speed ratio continuously. In system layout design, the sizes of the roller cylinders and the end-load cylinder, which were critical factors for controlling the variator, were designed. The planetary gear unit and six pairs of the gear assemblies were designed to establish the maximum speed of the vehicle at 30 ㎞/hr. In addition, the hydraulic clutch, the silent chain, the hydraulic manifold and the electronic controller were designed. Based on the design, a prototype CVT was developed and tested. Test results show that the CVT developed in this study could successfully provide variable speed of the tractor.

Performance Evaluation of a Driving Power Transmission System for 50 kW Narrow Tractors

  • Hong, Soon-Jung;Ha, Jong-Kyou;Kim, Yong-Joo;Kabir, Md. Shaha Nur;Seo, Young Woo;Chung, Sun-Ok
    • Journal of Biosystems Engineering
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    • 제43권1호
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    • pp.1-13
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    • 2018
  • Purpose: The development of compact tractors that can be used in dry fields, greenhouses, and orchards for pest control, weeding, transportation, and harvesting is necessary. The development and performance evaluation of power transmission units are very important when it comes to tractor development. This study evaluates the performance of a driving power transmission unit of a 50 kW multi-purpose narrow tractor. Methods: The performance of the transmission and forward-reverse clutch, which are the main components of the driving power transmission unit of multi-purpose narrow tractors, was evaluated herein. The transmission performance was evaluated in terms of power transmission efficiency, noise, and axle load, while the forward-reverse clutch performance was evaluated in terms of durability. The transmission's power transmission efficiency accounts for the measurement of transmission losses, which occur in the transmission's gear, bearing, and oil seal. The motor's power was input in the transmission's input shaft. The rotational speed and torque were measured in the final output shaft. The noise was measured at each speed level after installing a microphone on the left, right, and upper sides. The axle load test was performed through a continuous equilibrium load test, in which a constant load was continuously applied. The forward-reverse clutch performance was calculated using the engine torque to axle torque ratio with the assembled engine and transmission. Results: The loss of power in the transmission efficiency test of the driving power unit was 6.0-9.7 kW based on all gear steps. This loss of horsepower was equal to 11-18% of the input power (52 kW). The transmission efficiency of the driving power unit was 81.5-89.0%. The noise of the driving power unit was 50-57 dB at 800 rpm, 70-77 dB at 1600 rpm, and 76-83 dB at 2400 rpm. The axle load test verified that the input torque and axle revolutions were constant. The results of the forward-reverse clutch performance test revealed that hydraulic pressure and torque changes were stably maintained when moving forward or backward, and its operation met the hydraulic design standards. Conclusions: When comprehensively examined, these research results were similar to the main driving power transmission systems from USA and Japan in terms of performance. Based on these results, tractor prototypes are expected to be created and supplied to farmhouses after going through sufficient in-situ adaptability tests.

휠로더 자동변속기용 비례 제어 밸브의 설계 특성 해석 (Design Parameter Analysis of the Proportional Control Valve for Wheel-Loader Automatic Transmission)

  • 박영준;오주영;윤웅권;이근호
    • 한국정밀공학회지
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    • 제27권5호
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    • pp.27-35
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    • 2010
  • A loader used for uploading materials into truck is a kind of construction equipment. Mainly, a wheel loader is applied to construction work. Recently, an automatic transmission for the wheel loader is used to help drivers get the repetitive works done comfortably. It is composed of geartrain, clutch pack, hydraulic control system and TCU. Especially, a high-performance proportional control valve and its control algorithm is demanded to achieve the shift quality during a change of speed. In this paper, the commercial package program was used in order to justify model of the proportional control valve and simulate it. Steady-state and dynamic characteristics of PCV were analyzed to classify attractive forces and hydraulic control characteristics. This model also was verified the validity compared to the experimental result. Using the developed model, performances of PCV were predicted as studying design parameters.

4륜 구동 및 4방식 조향장치를 적용한 로더 개발 (Development of Loader with Four Wheel Driving and Four-Type Wheel Steering System)

  • 조현덕
    • 한국기계가공학회지
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    • 제3권3호
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    • pp.71-78
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    • 2004
  • The loader of this study is an agriculture machine for a stock farmer. We has much researched about power train and steering system in order to develop a new stock machine. So, the loader developed in this study has a 4 wheel driving system and a 4-type wheel steering system. Though the technological region is some large and general, these technologies are very important and their technical life may be very long. The power train of the loader is consisted of many units as follows, engine, clutch, transmission, and axles. And, the 4-type wheel steering system is consisted of oil tank, oil pump, steering valve, solenold valve, electronic controller, hydraulic cylinders, and touch sensors. This study shows construction logics of power train and steering system. We could know from many working tests that the developed loader with 4-type steeling system has many advantages when driving in a narrow corral.

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제주 연근해 삼치·방어용 끌낚시의 조업 장비 개발 (A Study on the Improvement of Trolling Equipment for Spanish Mackerel and Yellow Tail in the Coast of Jeju island)

  • 박용석;김병엽;이창헌
    • 수산해양교육연구
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    • 제27권2호
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    • pp.422-429
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    • 2015
  • The purpose of this study is the improvement of the existing trolling hauler, which has only one wheel to wind a main line, for saving man power around the coast of Jeju island. The trolling hauler manufactured for a test performance consisted of the wheel part of a main line and the roller part of a leader line including labor-saving devices comprised of a friction clutch, a fastener and springs. Even though this existing electric hauler system is convenient to control the wheel speed and the winding direction, it is apt to cost high and to corrode quickly at sea. Therefore, to remove these negative elements and to operate rollers for hoisting a leader line of the trolling, hydraulic motors were used separately. As a result, according to using of labor-saving devices, the towing tension occurred in operating in fishing ground could be selected moderately without breaking of lines and the operating efficiency of the trolling hauler was verified.

6속 자동변속기 밸브바디의 윤활오일유량 분배 특성 연구 (A Study on the Lubrication Flow Distribution in a Six-speed Automatic Transmission Valve Body)

  • 김진용;나병철;이계철
    • 한국기계기술학회지
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    • 제13권2호
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    • pp.79-84
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    • 2011
  • In general, a valve body of the automatic transmission(AT) is controlled by the clutch, the brake and lubricating oil flow in a hydraulic system and lubricant flow for each valve can be adjusted independently. To increase the lifetime of AT, the lubrication flow rate in a valve body for a 6 speed AT based parallel hybrid electric vehicle must be provided with proper oil distribution and control. In this study, we carried out several experiments without the inner parts of AT and with a AT assembly. The variation of the flow rate on oil temperature and pressure between an oil supply port and the outlets of the lubrication port was evaluated and analyzed. In the case of AT without the inner parts, it was evident that as the oil required for an operation of the clutch and brake was discharged from the outlet port, the flow rate from each lubrication port is decreased. However, the flow rate of the AT assembly was slightly increased. In addition, the lubrication flow rate was increased with increasing the oil temperature, and also it was reduced with increasing the oil pressure. Details of the resulting data are discussed.

전자식 비례 압력제어밸브 내 오일 오염 입자 제거 제어 알고리즘 검증 (Verification of Control Algorithm for Removing Oil Contaminant Factor from Proportional Pressure Control Valve)

  • 천수환;박진감;장경제;심성보;장민호;이진웅
    • 드라이브 ㆍ 컨트롤
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    • 제18권4호
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    • pp.1-8
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    • 2021
  • An electro proportional pressure control valve is mainly used to control the clutch of an agricultural tractor's automatic transmission. During transmission, the operating, hydraulic oil is mix with many kinds of contaminants. The contaminants can be trapped between the valve body and spool of the proportional pressure control valve leading to abnormal operating conditions and finally critical damage to the transmission hydraulic system. The present study aimed to verify the valve control algorithm as a basic study of developing control logic that removes contaminants between the spool and the body of the proportional pressure control valve. To develop the algorithm, MATLAB/SIMULINK was used. PWM method was used to control the applied solenoid coil current. The effectiveness of the algorithm was verified by comparing the actual pressure of the normal valve with the actual pressure of the abnormal valve. Based on the present study findings, when the algorithm was applied, the response of the valve pressure according to the current became stable and oil contaminated particles were removed. In the future study, the control algorithm will be optimized for the stability of the proportional pressure reducing valve, and it will be verified in consideration with the driving of the clutch.