• Title/Summary/Keyword: Gear Clearance

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Efficient Numerical Analysis for Shape Design of Turbine Seal (효율적인 수치해석에 의한 터빈 시일의 형상설계)

  • Han, Kyu-Taek
    • Journal of the Korean Society of Manufacturing Process Engineers
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    • v.15 no.4
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    • pp.118-124
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    • 2016
  • In this paper, the model to develop the forming process for turbine seal is suggested. And numerical approach for the shape design of the turbine seal is examined. Because of the thin thickness of the turbine seal, the seal is easily fractured in the manufacturing process. The main factors of the seal manufacturing consist of addendum angle and dedendum angle, fillet on the addendum face, number of the gear teeth, sheet initial location and gear initial location, rake and vertical clearance. The structure and shape of seal are modeled using the commercial 3D mechanical design program, CATIA(V5/R20). Also, rolling process to manufacture the turbine seal is analyzed using DEFORM$^{TM}$-3D(V11), commercial forming analysis software and runs under PC workstation. This study focused on the shape design of turbine seal. Through this research, the main factors to make the turbine seal for airplane turbine engine can be obtained. This study results are reflected to the shape design for turbine seal.

A Study of the Linear Analysis of an Equivalently Reduced System from the Original Torsional System (회전 시스템의 수학적 모델과 간소화된 시스템의 선형 특성 연구)

  • Ahn, Min-Ju;Yoon, Jong-Yun;Qi, Zhang;Ahn, In-Hyo;Lyu, Sung-Ki
    • Journal of the Korean Society of Safety
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    • v.25 no.3
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    • pp.7-14
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    • 2010
  • In order to analyze the vibro-impacts in the torsional system, several clearance types of nonlinearities should be included with the analytical or numerical method. These kinds of nonlinear factors can cause the errors while the system is calculated specifically with the numerical method, also it might take too long to get right answers with the every nonlinearity in the original system. Therefore, there are several methods developed for the sake of overcoming the deficiency of the analysis with the original system and saving the calculating time. The original system can be reduced by keeping the system characteristics such as from 14 to 6 DOF. Especially, since the torque flow in the torsional system is connected with the specific gear ratios, the original system can be transferred into the simpler system corresponding to each gear ratio rather than the original system, which can also show the same system characteristics such as the natural frequencies and the mode shapes. By using the reduced system, the calculating time can be saved and the redundant nonlinear effects for the system analysis can be ignored without any numerical errors.

Design Technique for Durability Improvement of Military Vehicle Clutch System (군용차량 클러치 내구수명 향상에 대한 연구)

  • Shin, Cheol-Ho;Kang, Tae-Woo;Kim, Sung-Gon;Kim, Seon-Jin
    • Journal of the Korea Academia-Industrial cooperation Society
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    • v.20 no.10
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    • pp.117-124
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    • 2019
  • Military Vehicles of the Korean army had been developed before 2004 and used manual transmissions. Manual transmissions contain a clutch system regulating the force from engine to transmission. In this study, a 2.5-ton military vehicle's clutch system was investigated. The existing clutch system had the characteristics that need to adjust the clearance between the clutch cover and release bearing. Improper clearance led to early wear of the clutch disk and failure of the clutch cover. To solve these problems, an improved clutch system was suggested and tested. The improved clutch system contains auto adjustment of the clearance and an enhanced clutch disk. To verify the improved clutch systems, 2 stage tests were conducted: an accelerated life test of the clutch system, and a driving test by trainee of driving more than 3,000km. As a result, the problems caused by the improper clearance adjustment were solved and this design was verified.

A Study on Tootk Design Program Development of Gerotor Pump/Motor (지로터 펌프/모터의 치형설계 프로그램 개발에 관한 연구)

  • 장주섭;이종원;한동철;조명래
    • Proceedings of the Korean Society of Tribologists and Lubrication Engineers Conference
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    • 1996.05a
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    • pp.17-23
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    • 1996
  • Gerotor Pump and Motors are widely used in lubrication and hydraulic actuator systems, These have many advantage compared with internal gear pump and motors, But the gerotor profile have not been sufficiently analyzed theoretically. So it is vary difficult for designer to decide the specifications of the gerotor profile, and it is not yet confirmed to calculating flow rate and minimum distance of clearance in the contact point of inner and outer rotor. In this paper, When we design inner and outer rotor concurently, We have analyzed the gerotor and displayed the calculated results such as flow rate, minumum distance between inner and outer rotor and gerotor profiles

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Performance of Roots-type Vacuum Pump with Cassini Oval Lobe Shape (Cassini 형 루츠 진공 펌프의 성능에 관한 연구)

  • Kim, H.J.;Cho, J.H.;Kim, Youn-J.
    • Proceedings of the KSME Conference
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    • 2000.04b
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    • pp.813-818
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    • 2000
  • The objective of this study is to elucidate the characteristic performance of Roots-type vacuum pump with Cassini oval lobe shape. The modelled lobe shape of Roots-type vacuum pump is two-lobe spur gear. The numerical analyses are performed fer leak flows, using 4th-order Runge-Kutta method and are compared with experimental results. Results show that for the case of involute lobe shape the total amount of the leak flow conductance is greater than that of cycloid and Cassini oval lobe shapes.

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Dimensional Accuracies of Cold-Forged Spur Gears (냉간단조 스퍼어기어의 치수정밀도)

  • 이정환;이영선;박종진
    • Transactions of Materials Processing
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    • v.5 no.2
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    • pp.115-121
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    • 1996
  • Recently it is attempted to manufacture gears by various cold forging methods to meet requirements of mass production and uniform qualities. Compared to machined gears cold forged ears reveal higher tooth strength and better surface roughness but they reveal lower geometrical accuracies. Therefore in the present study a series of experiments are performed to investigate relations between geometrical accuracies of dies and billet and those of the final product. The geometrical accuracies of forged gears are considered through functional gear-element tolerances by measuring pitch error profile error lead error radial error tooth thickness and rolling test. Results of the experiments can be summarized as follows: (1) involute spur gears of KS 5(or AGMA7) accuracies can be made,(2) concentricity of die set should be maintained within 0.01mm (3) clearance between the billet and die set should be less than 0.1mm (4) con-centricity and radial runout should be less than 0.08mm and 0.1mm respectively. However it is thought that FEM analysis of elastic/thermal deformations of dies and the billet is necessary for a better understanding of the findings obtained through the present study.

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Design of Motor-driven Traveling System for High Clearance Working Machinery based on Tractive Performance and Hill Climbing Ability (견인 및 등판 성능을 통한 고소작업기계의 모터 주행장치 설계)

  • Lee, Sangsik;Jang, Seyoon;Kim, Taesoo;Nam, Kyoucheol;Park, Wonyeop
    • The Journal of Korea Institute of Information, Electronics, and Communication Technology
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    • v.9 no.3
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    • pp.257-265
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    • 2016
  • In this study, an optimal design for motor-driven track type traveling system applied into high clearance working machineries in orchard is proposed. Tractive performance and hill climbing ability were predicted and evaluated for the optimal motor traveling system by taking into account of soil characteristics in orchard utilizing the high clearance working machineries. Design criteria for tractive performance were based on the traction force calculated from tractive effort subtracted by motion resistance, while hill climbing ability had its design criteria that fulfill the climbing 20% slope ground at a speed of 3km/h. Based on the evaluation results of traction and climbing ability, two DC48V, 4500rpm, 1.6kW AC motors were independently applied to both left and right side of orbits; each motor is designed to transmit power on driving sprocket of track type traveling system via 50:1 reduction gear ratio. The motor-driven track type traveling system developed in the study found to have 396 kgf of tractive force, which is 12.5% higher than climbing resistance at orchard soil having 20% slope ground (352 kgf), demonstrating sufficient tractive performance and hill climbing ability.

Development of Airframe Structure for Disaster and Public Safety Multicopter UAV (재난치안용 멀티콥터 무인기 기체구조 개발)

  • Shin, Jeong Woo;Lee, Seunggyu;Noh, Jeong Ho
    • Journal of Aerospace System Engineering
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    • v.14 no.3
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    • pp.69-77
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    • 2020
  • Airframe structure development of the 35 kg class 'Disaster and Public Safety Multicopter' UAV is described in this paper. To reduce the airframe weight, T-700 grade CFRP composite material was used, and the fuselage was designed with the semi-monocoque structure and plate installed with the control and communication devices designed in a sandwich structure. The specimen tests for the laminated plate and pipe were conducted to verify the strength and stiffness of the designed parts. The stacking sequence of composite materials was determined by the static strength and vibration analysis, and landing gear strut was designed by the nonlinear analysis with decent speed and ground clearance requirements. The static strength test was performed to evaluate the structural integrity and to verify the landing gear behavior.

A Study on Performance Improvement of Industrial Oil Pump Using Computational Analysis (전산해석을 이용한 산업용 오일펌프 성능개선에 관한 연구)

  • Kim, Jin-Woo;Lee, Hyun-Jun;Kong, Seok-Hwan;Lee, Seong-Won;Chung, Won-Ji
    • Journal of the Korean Society of Industry Convergence
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    • v.25 no.6_2
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    • pp.1111-1117
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    • 2022
  • Recently, interest in the circular economy has emerged in the industry. As a result, interest in Re-manufacturing, which makes old equipment similar to new products, is growing. In the machine tool industry with many aging equipment, the Re-manufacturing industry is essential, and among them, research on the performance improvement of gear type oil pumps was conducted. The purpose was to achieve the target performance of flow rate and volume efficiency by changing the shape of the gear pump housing clearance and inlet/outlet, and Computational Fluid Analysis and Central Composite Design were conducted using ANSYS CFX 2022 R2 and MINITAB®. The level of each determined factor was determined. 20 design points were derived, and the Flow Rate at each design point was calculated, and the Theoretical Flow Rate was calculated to obtain Volumetric Efficiency. The optimal design point was obtained when the Flow Rate was 140 lpm and the Volumetric Efficiency was maximum, the optimal design point was obtained when both were maximum, and the Surface Plot for each factor was obtained to identify the tendency.

Improvement of Flight Safety on Configuration Change of Rotorcraft Wiper Arm (회전익 항공기의 와이퍼 암 형상변경을 통한 비행 안전성 향상)

  • Kim, Dae-Han;Lee, Yoon-Woo;An, Jeong-Min;Park, Jae-Ho
    • Journal of the Korea Academia-Industrial cooperation Society
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    • v.18 no.6
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    • pp.736-741
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    • 2017
  • This paper examines the design for improving the wiper system of rotorcraft. During rotorcraft operation, the wiping performance and excessive clearance can decrease. The wiper system consists of a wiper arm assembly, motor, convertor and flex drive. If there is a problem with the wiper system, the operation ability decreases because the operation is restricted in a rainy environment. There are two main causes of the problem of the wiper system: the lifting forces acting on the wiper arm in aircraft flight and the excessive gap of the components. To remedy these two problems, the wiper arm was improved. The improvements included increased contact pressure on the wiper arm (spring tension), improved gear clearance, and material and shape changes. Durability test, aircraft ground test and flight test were carried out to verify the improved shape, and it was confirmed that the wiping performance and clearance problems were solved. Currently, the rotorcraft is operated without problem by applying the improved shape, and this design improvement process will be a useful reference for future rotorcraft development.