• 제목/요약/키워드: Gear Clearance

검색결과 41건 처리시간 0.026초

회전 용적형 기어펌프의 캐비테이션 유동 해석 (Numerical Simulations of Cavitation Flow in Volumetric Gear Pump)

  • 이중호;이상욱
    • 한국가시화정보학회지
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    • 제9권4호
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    • pp.28-34
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    • 2011
  • A volumetric gear pump is often used in extensive industrial applications to provide both high pressure and sufficiently high flow rate by physical displacement of finite volume of fluid with each revolution. Template mesh function in commercial CFD software, PumpLinx, by which 3-D meshes in the complex region between rotor and housing can be readily generated was employed for 3-D flow simulations. For cavitation analysis full cavitation model was included in 3-D simulations. The results showed high pulsation in pressure and flowrate which is implicated in pump vibration and noise. A model test for cavitation visualization was conducted and the results showed good qualitative agreement with numerical prediction.

치면 프로파일 모델에 따른 기어 치면 내부의 응력 분포 (Sub­surface Stress Distribution beneath the Contact Surface of the Gear Teeth for Two Profile Models)

  • 구영필;오명석;김형자;김영대
    • Tribology and Lubricants
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    • 제19권6호
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    • pp.357-364
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    • 2003
  • The sub­surface stress field beneath the gear's contact surface caused by the contact pressure in lubricated condition has been calculated. To evaluate the influence of the clearance shape on the stress field, two kinds of tooth profile models were chosen. One is the conventional cylinder contact model and the other is the new numerical model. Love's rectangular patch solution was used to obtain the sub­surface stress field. The analysis results show that the sub­surface stress is quite dependent on both the contact pressure and the profile model. The maximum effective stress of the new model is lower than that of the old model. The depth where the maximum effective stress occurs in the new model is not proportional to the intensity of the external load.

소규모 발전용 스크롤 팽창기 성능시험 (Performance Test of Scroll Expander for Micro-Power Generation)

  • 김현진;박익서;라필찬
    • 설비공학논문집
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    • 제17권4호
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    • pp.325-332
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    • 2005
  • This paper addresses the development of a scroll expander for power generation from relatively low temperature steam source. It has a double-sided orbiting scroll member so that no thrust bearing is needed to support the base plate of the orbiting scroll. Three power transmission shafts are placed at the periphery of the orbiting scroll base plate, and these shafts can also function as anti-rotation devices. Final output is obtained from the main central shaft engaged with the three power transmission shafts through gear assembly. The clearance between the fixed and orbiting scroll elements was estimated by comparing measurement of the mass flow rate with calculation results of a computer simulation. Due to large clearance, the expander total and volumetric efficiencies were measured to be $34\%\;and\;43\%$, respectively. It has been shown through the computer simulation that the total and volumetric efficiencies could be improved to $65\%\;and\;83\%$, respectively, if the current clearance is reduced by half.

지로터 펌프/모터의 치형 설계 프로그램 개발에 관한 연구 (A Study on Tooth Design Program Development of Gerotor Pump/Motor)

  • 장주섭;이종원;한동철;조명래
    • Tribology and Lubricants
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    • 제12권3호
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    • pp.100-106
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    • 1996
  • Gerotor pumps and motors are widely used in lubrication and hydraulic actuator systems. Compared with internal gear pumps and motors, they have many advantages. However, the gerotor profiles have not been suff'lciently analyzed theoretically. Therefore, it is very difficult for designer to decide the specifications of the gemtor profiles, and calculation of flow rate and minimum distance of clearance in the contact point of inner and outer rotor is not yet confirmed. In this paper, when we design inner and outer rotor concurently, we have analyzed the gerotor profiles and displayed the calculated results such as flow rate, minimum distance between inner and outer rotor and gerotor profiles.

주익장착방식의 추진기관 장착설계 (Propulsion Installation Design on Wing-Mounted-Nacelle Type)

  • 진광석;최광윤;공창덕
    • 한국추진공학회:학술대회논문집
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    • 한국추진공학회 1998년도 제10회 학술강연회논문집
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    • pp.4-4
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    • 1998
  • 이 연구에서는 100인승 항공기 급의 저익-주익장착나셀(wing mounted nacelle)의 추진기관 장착설계 방법을 제시하였다. 장착설계 방법을 구체적으로 설명하기 위해 세부적인 설계제한조건(design constraint)과 설계요구조건(design requirement and objectives)을 정의하고, 그러나 기준을 근거로 실례의 항공기(K100)를 사용하여 주익장착방식의 장착설계를 수행하였다. 장착설계는 간접항력(interference drag), roll clearance, ground clearance, nose gear collapse margin, rotor burst, 연료탱크용량 등의 설계제한 사항들을 고려하여 엔진성능을 만족시킬 수 있는 최적의 나셀 장착위치(spanwise, FS, WL)와 장착각도(toe-in, incidence, droop angle), wing day의 위치와 크기를 결정하여 향후에 개발될 주익장착방식의 추진기관 장착설계에 활용될 수 있는 설계절차를 구축하였다.

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유압식 추락 방지장치에 관한 연구 (A Study on the Hydraulic Fall Prevention Device)

  • 최정훈;구재민;석창성;허용;장성용
    • 한국정밀공학회지
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    • 제27권11호
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    • pp.78-83
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    • 2010
  • Since a tower crane is too high for a worker to ascend and by the wind in the high altitude, the possibility of a safety accident is very high, a lift assist is used. In this study, the hydraulic fall prevention device using the pressure generation device by Seok, et al. was developed. For this, the effects on the fall prevention performances of factors such as gear clearance, oil viscosity, rotative velocity and so on were evaluated by the analysis of fluid flow using FEM and the prototype was producted and a function test was performed.

설계인자 보정방법에 의한 사출성형기어의 캐비티 설계 (Cavity Design for Injection Molded Gears by the Compensation Method of Design Parameters)

  • 이성철;김충현;권오관;허용정
    • 대한기계학회논문집A
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    • 제20권10호
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    • pp.3142-3151
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    • 1996
  • As plastics shrink when changing from a molten to a solid state, mold cavities must by made larger than the product specification, In making molded gears, the teeth in the cavity must be carefully compensated for shrinkage so that the teeth of gears will have the correct profile. Two compensation methods are widely used in the cavity design. One is the compensation of a module and the other is the modification of a pressure angle and profile shifting coefficient. These methods, however, do not provide a gear cavity with all disign parameters for gears and several parameters are determined by experience. In this paper, the new design technique, namely the compensation method of design parameters, was proposed , which is based on the three kinds of shrinkage rates obtained from the measuring data of the prototype of molded gears. Using the shrinkage rates in the tip circle, tooth heigth and tooth thickness, we calculate the whole design parameters of a gear cavity. Thus, the gear cavity is considered as a complete gear with the compensated module, pressure angle, profile shifting coefficient, clearance coefficient and back lash amount so that the formula of gears can be applied to the cavity design effectively. Experimental results show that more precision molded gears can be made by using the proposed design method.

전륜 8속 자동변속기 소음 개발에 대한 연구 (A Research for the Noise Development of the FF 8th Speed Automatic Transmission)

  • 이현구;홍사만;김무석;허진욱;유동규
    • 한국소음진동공학회논문집
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    • 제26권5호
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    • pp.559-566
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    • 2016
  • This study shows a development procedure and results of noise reduction for a new developed FF 8th speed automatic transmission. Based on planetary gear operating frequency analysis using PTA(planetary transmission analysis) program developed in 2012, It is expected that gear noise of the rear planetary gear set could be recognized easily in the concept design stage. Therefore, pRMC (planetary run many cases) analysis program that is developed in 2012 was applied to minimize the planetary gear noise level and noise distributions versus torque. To minimize noises coming from oil pump and final gears of a new transmission, several changes were applied, such as changing the clearance of double angular ball bearing, the oil pump rotor tooth number from 9 to 11 and the oil pump type from parachoid to megafloid and so on. Besides, stiffness values of the transmission case and the mount bracket were measured and reinforced properly. Finally, The total noise of the new FF 8th speed automatic transmission was developed successfully. Furthermore, E.O.L. testers also have been adapted to control the noise quality of automatic transmission assembly in the manufacturing factory. This paper could provide practical solutions to the automatic transmission NVH problems.

클리어런스가 없는 초고압 회전용적형 헬리컬기어 펌프의 유동해석에 관한 연구 (A Study on Fluid Flow Analysis of High Pressure Positive Displacement Pump without Clearance)

  • 민세홍;김호철
    • 한국화재소방학회논문지
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    • 제29권2호
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    • pp.33-38
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    • 2015
  • 고압과 정량 흡상을 목적으로 클리어런스가 없는 초고압 회전용적형 헬리컬기어 펌프의 개발을 진행하였다. 펌프의 내부 압력과 토출 유속을 검증하기 위해 CFD 해석을 수행하였다. 이에 따라 FVM 기법으로 유동해석을 수행하였는데 클리어런스가 없는 완전히 밀폐된 형태의 FVM 유동해석은 격자가 연속하게 구성되지 않아 유체영역이 분리되어 정상적인 결과를 얻어낼 수 없었다. 이러한 문제로 격자 구성이 필요치 않은 MPS 기법으로 유동해석을 수행하였고, MPS 유동해석을 통해 펌프의 내부 압력과 토출 유속을 확인할 수 있었다. 로터의 회전속도 1,000 rpm에서 펌프 내부의 압력은 최소일 때 19.5 bar, 최대일 때 44.6 bar이고, 평균 압력은 33.9 bar로 확인되었다. 토출 유속은 최소일 때 64.5 m/s, 최대일 때 84.8 m/s이고, 평균 유속은 76.1 m/s로 확인되었다. 본 연구를 통해 클리어런스가 없는 해석 모델의 유동해석은 FVM 기법보다는 MPS 기법이 더 적합하였음을 확인할 수 있었다. 또한 초고압 회전 용적형 헬리컬기어 펌프의 압력의 변화에 따른 유속과의 관계를 본 연구를 통해 규명할 수 있었다.

리클라이너 결합 성능 향상을 위한 섹터투스의 롤오버 저감 방법 (Reduction of the Roll-Over of the Sector Tooth for Achieving Improved Recliner Locking Performance)

  • 이상훈;최홍석;장명진;김동수;배재호;고대철;김병민
    • 대한기계학회논문집A
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    • 제34권11호
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    • pp.1623-1630
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    • 2010
  • 본 연구에서는 자동차용 시트 리클라이너의 주요 부품인 섹터투스 결합부의 롤오버 저감을 위한 효과적인 성형 방법을 제시하였다. 기존의 성형 공정에 의하여 발생한 과도한 롤오버 때문에 섹터투스 내측기어와 결합 부품인 폴투스 외측기어 간의 정확한 결합이 이루어지지 않아 승차감 및 안전성이 저하된다. 따라서 성형 시, 소재를 롤오버 측으로 유동시켜 롤오버량을 최소화 해야 하며, 이를 위하여 국부 돌기형 다이, 코이닝 펀치를 이용한 방법 및 가변 역클리어런스를 통한 롤오버 저감 방법에 대해 유한요소해석으로 비교 평가 하였고, 이를 검증하기 위해 금형 제작 및 실험을 수행하였다. 실험 결과, 가변 역클리어런스를 이용한 방법이 롤오버 저감 및 금형 강도 측면에서 우수한 특성을 가지는 것을 확인할 수 있었다.