• Title/Summary/Keyword: Engine Supply System

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LPLi Engine Performance and Vehicle Exhaust Emission Characteristics (액상 분사 LPG 엔진 성능 및 차량 배기 배출물 특성에 관한 연구)

  • 임종훈;명차리;박심수;양승주
    • Transactions of the Korean Society of Automotive Engineers
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    • v.11 no.4
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    • pp.15-21
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    • 2003
  • LPG is considered as one of the most prominent alternative automotive fuels in worldwide. However, conventional mixer system can not meet the emission regulations as the mileage accumulation increased. Recently, much attention is focused on the development of LPG liquid injection fuel systems to increase the engine performance and reduce the exhaust emissions. This study evaluates the LPLi(Liquid Phase LPG injection) engine performance and exhaust emission characteristics using a 3.0 liter LPG engine. The fuel supply system and engine management system were changed from FBM into LPLi to control the precise mixture ratio and optimized spark advance.

A Comprehensive Study on Fuel Injector Test Bench for Heavy Duty Engine

  • Das, Shubhra Kanti;Thongchai, Sakda;Lim, Ocktaeck
    • Journal of ILASS-Korea
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    • v.20 no.3
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    • pp.195-201
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    • 2015
  • This study discusses a fuel injector test bench containing a mechanical type fuel supply system for heavy duty diesel engine. The main focus of this study was to evaluate the design stability of the test bench, which basically measures the injector durability of a multi-hole heavy duty injector by using pure diesel as a test fuel. In this experiment, diesel spray was controlled by a specially designed control box and all the experiments were carried out to measure e.g. fuel injection pressure and fuel injection quantity to understand the injection status which is interlinked with the stability factor of total test bench design. Also, the durability test was performed to understand the heavy duty operation lastingness of the designed system and the flow rate of the installed distributor pump in the fuel supply system of this studying test bench was compared with LO-1 and LO-2 pump. The results of the above mention tests revealed that the injector test bench design and control system can serve the purpose for heavy duty injector.

The Development of the Ignition Spark Timing Conversion System for LPG/Gasoline Bi-fuel Vehicle (LPG 및 Gasoline 겸용 차량의 엔진 점화시기 변환 제어시스템 개발)

  • 전봉준;양인권;김재국;김성준
    • Journal of Advanced Marine Engineering and Technology
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    • v.27 no.1
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    • pp.117-123
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    • 2003
  • In a bi-fuel engine using gasoline and LPG fuel, with the current ignition timing for gasoline being used, the effective performance could not be taken in LPG fuel supply mode. The ignition timing in LPG fuel mode must be advanced much more than that of gasoline mode for the compensation of its lower flame speed, due to engine torque drop. This study aims to develop the control system for ignition spark timing conversion which is composed of hardwares and control algorithm for gasoline/LPG engine. We propose the control system which can advance the ignition spark timing in LPG fuel mode more than used in gasoline fuel mode. The advance of ignition timing is achieved by change of the ignition dwell time of coil igniter. The engine torque and F/E(Fuel-Economy) in LPG fuel mode are measured to evaluate the difference of engine performance between before and alter changing ignition spark timings. The engine torque and F/E are increased respectively, which proves the developed control system is effective so much for gasoline and LPG bi-fuel engine.

Development of the Scramjet engine Test Facility(SeTF) in Korea Aerospace Research Institute (한국항공우주연구원 스크램제트 엔진 시험설비의 개발)

  • Lee, Yang-Ji;Kang, Sang-Hun;Oh, Joong-Hwan;Yang, Soo-Seok
    • Journal of the Korean Society of Propulsion Engineers
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    • v.14 no.3
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    • pp.69-78
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    • 2010
  • Korea Aerospace Research Institute started on design and development of a hypersonic air-breathing engine test facility from 2000 and completed the test facility installation in July 2009. This facility, designated as Scramjet engine test facility(SeTF), is a blow-down type high enthalpy wind tunnel which has a pressurized air supply system, air heater system, free-jet test chamber, fuel supply system, facility control/measurement system and exhaust system. In this paper, details of the specifications, and configuration of the SeTF are described. For verifying characteristics of the SeTF, wind tunnel tests are now on progress and some of the data are also described.

Performance Improvement of a Small-Sized Two Stroke Engine by Hydrogen Direct Injection (수소 직접 분사를 통한 2행정 소형 엔진의 성능 향상에 관한 연구)

  • CHOI, JISEON;KIM, YONGRAE;KIM, SEONYOEB;PARK, CHEOLWOONG;CHOI, YOUNG
    • Transactions of the Korean hydrogen and new energy society
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    • v.33 no.3
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    • pp.255-260
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    • 2022
  • Hydrogen gas fuel was applied to a small-sized two stroke engine for a mobile power source instead of gasoline fuel. Port fuel supply showed a limitation in terms of power due to the back fire at the engine intake manifold. So in this study, hydrogen direct injection system was applied to overcome this drawback by using a low pressure direct gas injector. The result from this strategy showed that hydrogen direct injection improved fuel efficiency as well as torque and power comparing to the port fuel supply system.

An Experimental Study of Smoke Reduction System using Vacuum (부압을 이용한 매연저감장치의 실험적 연구)

  • Ham, Sung-Hoon;Kwon, Young-Woong;Oh, Se-Hoon;Park, Sung-Cheon
    • Journal of the Korean Society for Railway
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    • v.12 no.5
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    • pp.714-718
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    • 2009
  • Over the past years, many research works have been carried out to investigate the factors which govern the performance of diesel engine. The air pollutant emission from the diesel engine is still a significant environmental concern in many countries. In the present study, new system of smoke reduction of diesel engine is proposed. This new system is using vacuum equipment and filter included moisture for capture smoke. To verificate new system experiments were performed at diesel vehicle. As a result it is founded that smoke is decreased.

A Study on the Power and Smoke Characteristics for the Intake System Improvement using Air Conditioning System in a Diesel Vehicle (디젤 자동차의 에어컨 사용시 흡기계통 개선에 따른 출력 및 매연 특성에 관한 연구)

  • Youn, Y.C.;Kwon, K.R.;Pyeon, H.
    • Journal of Power System Engineering
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    • v.15 no.6
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    • pp.11-15
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    • 2011
  • This study investigated the symptoms of the a reduction in output while driving on the road, or increasing of fumer out exhaust gas on inclined road while working air-conditioner in summer. Notice how the experiment in 2010, the Ministry of Environment(Chapter No. 2010-46), and how the vehicle emissions inspection was carried out. 2500cc Diesel cars used in the study were used and compare to output of engine, exhaust gas, inhalation temperature measurement Inhalation of cold air has not been supplied to all agencies when comparing the results when cold air intake temperature of the supply air-conditioning switch range control from 1 to 4, the temperature drops $98^{\circ}C$ to $78^{\circ}C$. At the momentum of switch level 4, output from 63ps to 66ps after the connection has increased 9.6 percent, the highest concentration of exhaust emissions were reduced by 42.8%. This research can contribute in part to the reduction of exhaust directly supply into the cooling air intake line, doing the output of diesel cars in the summer. In addition, construction equipment and machinery that are currently being used excluding the engine's intercooler cooling of the supply line via a separate output in the summer and help reduce exhaust emissions is expected.

A Study on a Conceptual Design Process of Fuel Feeding Systems for High-Speed Vehicles (초고속 비행체 연료공급시스템 개념설계과정 연구)

  • Lee, Hyung Ju;Park, Jeongbae;Kwon, Minchan;Hwang, Ki-Young
    • Journal of Aerospace System Engineering
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    • v.7 no.3
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    • pp.7-14
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    • 2013
  • Hypersonic vehicles over Mach 5 need active cooling or thermal management systems to resolve excessive heating problems on their fuselage and engines. Endothermic fuels are widely used these days not only for the energy source but also for a heat sink. Therefore, fuel supply systems of hypersonic vehicles should be mainly composed of adiabatic fuel storage tank, cooling systems for the airframe and engine/nozzle, and fuel supply/injection systems in high pressure, high temperature, and high fuel flow rate conditions. This paper describes a conceptual design process of a hypersonic fuel supply system in order for designing a layout of the system, and identifying components and their specification requirements.

Comparison of Effectiveness for Performance Tuning of Liquid Rocket Engine

  • Cho, Won Kook;Kim, Chun Il
    • International Journal of Aerospace System Engineering
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    • v.5 no.2
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    • pp.16-22
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    • 2018
  • An analysis has been made on the performance variation due to pressure drop change at propellant supply pipes of liquid rocket engine. The objective is to compare the effectiveness of control variables to tune the liquid rocket engine performance. The mode analysis program has been used to estimate the engine performance for different modes which is realized by controlling the flow rate of propellant. The oxidizer of combustion chamber, the fuel of combustion chamber, the oxidizer of gas generator and the fuel of gas generator are the independent variables to control engine thrust, engine mixture ratio and temperature of gas generator product gas. The analysis program is validated by comparing with the powerpack test results. The error range of compared variables is order of 4%. After comparison of tuning effectiveness it is turned out that the pressure drop at oxidizer pipe of gas generator and pressure drop at combustion chamber fuel pipe and the pressure drop at the fuel pipe of gas generator can effectively tune the thrust of engine, mixture ratio of engine and temperature of product gas from gas generator respectively.

Investigation of Chill Down Characteristics of Liquid Oxygen Feeding System in 75 Tonf-class Liquid Rocket Engine Firing Test (75톤급 액체로켓엔진 연소시험에서의 액체산소 공급부 예냉특성 고찰)

  • Seo, Daeban;Cho, Namkyung;Han, Yeoungmin
    • Journal of the Korean Society of Propulsion Engineers
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    • v.22 no.4
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    • pp.108-116
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    • 2018
  • A firing test of the 75 tonf-class liquid rocket engine to be used as the first and second stage engines of the KSLV-II was carried out at the rocket engine test facility(RETF). Since this engine uses liquid oxygen as the oxidizer, which is a cryogenic fluid, it is essential that the chill down of the supply pipe line and engine proceed for the firing test; thus, the given inlet requirements must be met. Moreover, it is important to understand the chill down characteristics of the facility and the engine and the amount of liquid oxygen consumed in the chill down process for efficient test operation in the future. In this paper, chill down characteristics of the supply pipe and the engine were evaluated through the investigation of the chill down process of the 75 tonf-class liquid rocket engine at each stage before and after run tank pressurization. In addition, the amount of liquid oxygen consumed was also evaluated.