• Title/Summary/Keyword: Breakdown test

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Breakdown Points of Direction Tests

  • Park, Kyung-Mee
    • Journal of the Korean Statistical Society
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    • v.26 no.2
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    • pp.211-222
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    • 1997
  • We briefly review three Raleigh type location tests based on direction vectors, which have been shown to be efficient when the distribution is unknown, skewed, or heavy-tailed. Then we calculate their test breakdown points and discuss the robustness of Randles multivariate sign test for one-sample.

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Correlation between Insulation Diagnostic Test and AC Breakdown Test for 3.3 kV Class Induction Motor

  • Byun, Doo-Gyoon;Hong, Jin-Woong
    • Transactions on Electrical and Electronic Materials
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    • v.7 no.5
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    • pp.262-266
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    • 2006
  • The insulation diagnostic test and the AC breakdown test were performed under off-line using the 3.3 kV class induction motor which have been served for 10 years. These tests were conducted in means of nondestructive and destructive test. In this paper, we compared the correlation between the nondestructive and destructive test. Furthermore we setup an experimental condition with moisture and compared the insulation characteristics between moist and dry sample. From the results of the nondestructive and destructive test, it was found that the second AC current, which is the previous step of insulation breakdown, suddenly increased at a point of around 8.5 kV. The insulation breakdown of moist sample occurred at 12-14 kV, which is 4-5 kV lower than dry sample.

Characteristics of Insulation Diagnosis and Failure in Gas Turbine Generator Stator Windings

  • Kim, Hee-Dong
    • Journal of Electrical Engineering and Technology
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    • v.9 no.1
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    • pp.280-285
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    • 2014
  • In order to evaluate the insulation deterioration in the stator windings of five gas turbine generators(137 MVA, 13.8 kV) which has been operated for more than 13 years, diagnostic test and AC dielectric breakdown test were performed at phases A, B and C. These tests included measurements of AC current, dissipation factor, partial discharge (PD) magnitude and capacitance. ${\Delta}I$ and ${\Delta}tan{\delta}$ in all three phases (A, B and C) of No. 1 generator stator windings showed that they were in good condition but PD magnitude indicated marginally serviceable and bad level to the insulation condition. Overall analysis of the results suggested that the generator stator windings were indicated serious insulation deterioration and patterns of the PD in all three phases were analyzed to be internal, slot and spark discharges. After the diagnostic test, an AC overvoltage test was performed by gradually increasing the voltage applied to the generator stator windings until electrical insulation failure occurred, in order to determine the breakdown voltage. The breakdown voltage at phases A, B and C of No. 1 generator stator windings failed at 28.0 kV, 17.9 kV, and 21.3 kV, respectively. The breakdown voltage was lower than that expected for good-quality windings (28.6 kV) in a 13.8kV class generator. In the AC dielectric breakdown and diagnostic tests, there was a strong correlation between the breakdown voltage and the voltage at which charging current increases abruptly ($P_{i1}$, $P_{i2}$).

Analysis of Insulation Condition in Traction Motor Stator Windings (견인전동기 고정자 권선의 절연상태 분석)

  • Kim, Hee-Dong;Park, Young
    • Journal of the Korean Institute of Electrical and Electronic Material Engineers
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    • v.20 no.7
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    • pp.631-635
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    • 2007
  • Diagnostic, surge and ac breakdown tests are widely used to evaluate the insulation condition of stator winding in traction motor. Diagnostic test included ac current, tan delta and maximum partial discharge. The result of diagnostic test indicates that five kinds of stator windings are good condition. Surge test was peformed to confirm the healthy of turn insulation in stator windings. This test is very easy to detect the turn insulation failure between normal and defect stator windings. After completing the diagnostic test, ac breakdown test has conducted gradually increasing ac voltage, until the stator winding punctured. No. 5 stator windings failed near rated voltage of 18.9 kV The breakdown voltage of No. 1 stator windings was 13.0 kV The ac breakdown voltage of normal winding is about 1.45 times higher than that of defect windings. The failure was located in a line-end coil at the exit from the core slot.

Interfacial Breakdown characteristics in XLPE/EPDM Laminate (XLPE/EPDM laminate의 절연파괴특성)

  • 남진호;서광석
    • Proceedings of the Korean Institute of Electrical and Electronic Material Engineers Conference
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    • 1999.11a
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    • pp.495-497
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    • 1999
  • In order to determine what influences the interfacial breakdown in EPDM/XLPE laminates, We made the breakdown test ceil and this was pressure controllable breakdown test cell. We make the needle electrode (tip radius: about 10 micrometer) using electrochemical method. We studied the interfacial silicone oil was higher than that with silicone grease. As a function of heat treatment time in a vacuum, interfacial breakdown strength increased much in XLPE/EPDM laminates pasted with silicone grease but increased a little in that with silicone oil.

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The Application of Pre-Breakdown Partial Discharge Detection Method for Breakdown of Investigation of Long Distance XLPE Cable (장조장 XLPE 케이블 절연 파괴 원인 규명을 위한 전구차단 장치의 응용)

  • Lee, C.Y.;Kim, D.W.
    • Proceedings of the KIEE Conference
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    • 2002.07c
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    • pp.1827-1829
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    • 2002
  • This paper describes AC test for long delivered drum length of cable using pre-breakdown partial discharge detection(PPD) method, which can be applied to observe the causes of electrical breakdown of EHV XLPE insulation. This method is to de-energize applied voltage to cable rapidly using pre-breakdown partial discharge, and is able to prevent complete breakdown. By this effect, defects such as voids, metal particles and protrusion in cable can be observed clearly. AC resonant test set was used for PPD method. Localization of partial discharge was performed by time difference detection of the traveling wave. Accuracy of localization was 1% to the length of test cable. Through several experiments with XLPE cable, successful results of PPD method were obtained.

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A study on insulation characteristics with AC Breakdown Test for Stator Winding of 3.3kV class Induction Motor (절연파괴시험을 통한 3.3kV 유도전동기의 절연특성 연구)

  • Lee, Dong-Geun;Lee, Kwang-Ho;Choi, Kyo-Nam;Kim, Hyun-Il;Kwak, Hee-Jin;Oh, Bong-Keun
    • Proceedings of the KIEE Conference
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    • 2005.07c
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    • pp.2118-2122
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    • 2005
  • This test was performed to assess the corelation of insulation deterioration condition with breakdown voltage of the stator winding of 3.3kV class induction motors which have been in service for 10 years after being installed in 1993. The insulation diagnostic tests include resistance, polarization index(P.I), dissipation factor$({\Delta}tan{\delta})$, maximum partial discharges (Qmax) and AC breakdown test. we evaluated the corelation of insulation diagnostic test with AC breakdown test for stator wilding of high voltage induction motor.

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Statistical Analysis of Electrical Tree Inception Voltage, Breakdown Voltage and Tree Breakdown Time Data of Unsaturated Polyester Resin

  • Ahmad, Mohd Hafizi;Bashir, Nouruddeen;Ahmad, Hussein;Piah, Mohamed Afendi Mohamed;Abdul-Malek, Zulkurnain;Yusof, Fadhilah
    • Journal of Electrical Engineering and Technology
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    • v.8 no.4
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    • pp.840-849
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    • 2013
  • This paper presents a statistical approach to analyze electrical tree inception voltage, electrical tree breakdown voltage and tree breakdown time of unsaturated polyester resin subjected to AC voltage. The aim of this work was to show that Weibull and lognormal distribution may not be the most suitable distributions for analysis of electrical treeing data. In this paper, an investigation of statistical distributions of electrical tree inception voltage, electrical tree breakdown voltage and breakdown time data was performed on 108 leaf-like specimen samples. Revelations from the test results showed that Johnson SB distribution is the best fit for electrical tree inception voltage and tree breakdown time data while electrical tree breakdown voltage data is best suited with Wakeby distribution. The fitting step was performed by means of Anderson-Darling (AD) Goodness-of-fit test (GOF). Based on the fitting results of tree inception voltage, tree breakdown time and tree breakdown voltage data, Johnson SB and Wakeby exhibit the lowest error value respectively compared to Weibull and lognormal.

A Robust Wald-Ttype Test in Linear Regression

  • Nam, Ho-Soo
    • Journal of the Korean Statistical Society
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    • v.26 no.4
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    • pp.507-520
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    • 1997
  • In this paper we propose a robust Wald-type test which is based on an efficient Mallows-type one-step GM-estimator. The proposed estimator based on the weight function of Song, Park and Nam (1996) has a bounded influence function and a high breakdown point. Under some regularity conditions, we compute the finite-sample breakdown point, and drive asymptotic normality of the proposed estimator. The level and power breakdown points, influence function and asymptotic distribution of the proposed test statistic are main points of this paper. To compare the performance of the proposed test with other tests, we perform some Monte Carlo simulations.

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Breakdown Characteristics of Dry Air under 362 kV GIB (362 kV GIB 내에서 건조공기의 절연파괴 특성)

  • Han, Ki-Son;Ju, Hyung-Jun;Yoon, Jin-Yul;You, Hong-Geun
    • Journal of the Korean Institute of Electrical and Electronic Material Engineers
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    • v.23 no.10
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    • pp.804-808
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    • 2010
  • In this paper, we studied the dielectric breakdown voltage characteristics by the AC withstand voltage test on using green insulation dry air instead of $SF_6$ insulation gas used in the GIB (gas insulated bus) of 362 kV GIS (gas insulated switchgear). The AC withstand voltage test applied to the standard KEPCO's 362 kV GIB with dry air insulation, and the equivalence of dielectric breakdown voltage for dry air and $SF_6$ gas were examined, and the empirical formulas of dielectric breakdown voltage for dry air were calculated, and the criterion of AC withstand voltage test for dry air insulation was derived. Using the criterion, dry air can be used instead of $SF_6$ gas for 362 kV GIB in the factory acceptance test was confirmed.