• Title/Summary/Keyword: 회전시험

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Spin Testing for the Endurance Verification of Gas Turbine Blades (고속회전시험기를 활용한 가스터빈 동익의 내구성 시험)

  • Lee, Dooyoung;Kim, Doosoo;Son, Taeha;Goo, Jaeryang
    • KEPCO Journal on Electric Power and Energy
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    • v.4 no.1
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    • pp.19-24
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    • 2018
  • The long-term research and development for the production of domestic blades has been consistently performed. As the direct and indirect results of its nationwide technologies in precision casting have been improved as well as maintenance costs for turbine machinery has been reduced. Whereas, there are still not a few concerns about the reliability of newly manufactured blades in spite of the quality certificate in metallurgical and mechanical properties. A spin tester is a machine that gives centrifugal loading to a rotating part, and its practical application is the overspeed test that is usually used to check the quality of products. A new spin rig has been constructed in KEPCO Research Institute for the purpose of evaluating the reliability of blades. In this paper, the test methodology for low cycle fatigue damage mechanism as well as the overspeed test for newly developed blades is described, and their reliability is evaluated too.

Design of a Torque Application Device in Test Rig for a Wind Turbine Gearbox (풍력발전기용 증속기 시험 장비의 토크 인가 장치 설계)

  • Kim, Jeong-Gil;Park, Young-Jun;Lee, Geun-Ho;Nam, Yong-Yun;Oh, Joo-Young
    • Transactions of the Korean Society of Mechanical Engineers A
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    • v.39 no.5
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    • pp.507-515
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    • 2015
  • This study was conducted to develop and verify a torque application device for use in a mechanical power-circulation test rig for 5.5 MW wind turbine gearboxes. The design and analysis of the torque application device was conducted. In addition, the torsional stiffness of the test rig was calculated using the rotational angle measurements for each of the components. The calculated stiffness of the test rig was $231.13kN{\cdot}m/rad$ for a clockwise torque application. The rated torque can be applied when the stiffness of the gearbox is greater than $1,064,400kN{\cdot}m/rad$ for a clockwise torque application. Because of the limited rotational angle of the test rig, the potential application of the rated torque is determined according to the torsional stiffness of the test gearbox.

Water Tests of Lox Pump for 75-ton Class Liquid Rocket Engine (75톤급 액체로켓엔진용 산화제펌프의 수류시험)

  • Kim, Dae-Jin;Hong, Soon-Sam;Choi, Chang-Ho;Kim, Jin-Han
    • Aerospace Engineering and Technology
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    • v.10 no.1
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    • pp.122-128
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    • 2011
  • A series of water tests of a Lox pump for liquid rocket engines are performed at a room temperature. According to the hydraulic test results, the head coefficient is slightly decreased when the rotational speed of the pump is increased. However the efficiency is high at the high-speed test. Also, according to the cavitation test results, the cavitation performance of the pump is found to be decreased when the flow ratio is less than 92%. Furthermore, the vibration characteristic is analyzed using measured high frequency data.

Cross-rotating Multi-copter (교차회전 멀티콥터)

  • Hwang, SeungJae;Park, YoungMin;Cho, TaeHwan
    • Journal of Aerospace System Engineering
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    • v.13 no.1
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    • pp.47-53
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    • 2019
  • To improve an aerodynamic characteristic of the eVOTL aircraft, Korea Aerospace Research Institute (KARI) performed a validity test of the cross-rotating propeller technology. First, CFD analysis was carried out and an idea of the cross-rotating propeller to imply on a multi-copter confirmed with a commerce pitch control multi-copter that has two different blades, 0.11 and 0.21 m. After verifying the idea, a multi-copter with about 3 kg maximum take-off weight (MTOW) was custom designed to complete a ground test to measure thrust and noise. The test was performed with 15 and 22 in. propellers at the identical tip speed. The test results show that the 22 in. propeller with the cross-rotating technology required about 30 % less power and reduced 3~5 dB aerodynamic noise as compared to 15 in. propeller without cross-rotating.

An Experimental Study of the Gas Turbine Slinger Combustor (가스터빈 슬링거 연소기 실험연구)

  • Choe, Seong-Man;Lee, Gang-Yeop;Lee, Dong-Hun;Park, Jeong-Bae
    • Journal of the Korean Society for Aeronautical & Space Sciences
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    • v.34 no.2
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    • pp.68-74
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    • 2006
  • An experimental study was carried out to investigate the combustion characteristics of the slinger combustor. A combustion test rig was manufactured and installed in KARI combustor test facility. From the ignition test results, we found that there were two major factors influencing the ignition limits; by increasing the rotational speed and the air mass flow rate, a better ignition performance was attained. From the combustion test results, we obtained 99.6% combustion efficiency, 15% pattern factor, and 3% profile factor. The results in this work indicate that the ignition and combustion characteristics of a slinger combustor are markedly different from those of a conventional annular combustor.

Effect of Tip-Clearance on the Performance of a Supersonic Impulse Turbine (초음속 충동형 터빈의 팁간극에 따른 성능변화 연구)

  • Jeong, Eun-Hwan;Lee, Hang-Gi;Park, Pyun-Goo;Kim, Jin-Han
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2008.11a
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    • pp.117-121
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    • 2008
  • The effect of tip clearance on the performance of a supersonic impulse turbine was investigated experimentally. Test was performed using high pressure air in wide ranges of pressure ratio and rotational speeds. Test revealed that efficiency gradient of the subject turbine at a reference test point was a very low value of 0.05. Turbine efficiency was varied non-linearly with respect to tip clearance. It has been found that efficiency gradient is proportional to the cube of rotational speed at a fixed turbine pressure ratio. It also has been found that efficiency gradient shows its minimum at a reference test pressure ratio irrespective of rotational speeds.

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저속회전베어링의 전동면 이상진단에 관한 연구 -웨이브렛과 패턴인식법의 적용-

  • 김태구
    • Proceedings of the Korean Institute of Industrial Safety Conference
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    • 2002.05a
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    • pp.413-418
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    • 2002
  • 베어링은 산업현장에서 널리 쓰여지는 중요 부품이다. 따라서 이의 결함에 따른 손실을 예방하기 위해서는 이상을 진단하고 검지하는 기법이 요구된다. 따라서 본 연구에서는 저속회전하므로 노이즈가 많이 포함되어 절상상태의 신호검출이 어려운 저속회전베어링의 외륜이상을 웨이브렛의 Denoising 기법을 적용하여 정량적으로 진단하고 패턴인식법 중의 하나인 KDI(Kullback Discrimination Information)를 적용하여 이상상태의 진단/검지능력을 시험해 보았다. 웨이브랫의 Denoising 기법은 노이즈 캔셀링(Noise canceling)이 능력이 뛰어났고, HDI기법은 저속회전베어링의 정상과 이상의 분류에 뛰어난 검지능력이 있음을 알 수 있었다.(중략)

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Influence of the Dental Implant Abutment Screw Coating Materials on Joint Stability (임플란트 지대주나사 코팅이 결합안정성에 미치는 영향)

  • Lim, Hyun-Pil;Park, Young-Sun;Vang, Mong-Sook;Yang, Hong-So;Park, Sang-Won;Yoon, Suk-ja
    • Journal of Dental Rehabilitation and Applied Science
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    • v.25 no.2
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    • pp.157-169
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    • 2009
  • The aim of this study was to evaluate effect of implant abutment screw coating treatment on joint stability, investigating mechanical properties of these. For this study used $ExFeel^{(R)}$ external hexed implant system and $15mm{\times}1mm$ discs. Experimental group was $1{\mu}m$ TiN, TiCN, TiC coated abutment screws and discs. To know mechanical property, i evaluated adhesion strength, surface hardness, using disc, corrosion test using screw. The results were as follows : rotation angle of coated screws increased than that of non-coated screw because of lower friction coefficient, especially TiC coated screw group had the largest value, but removal torque decreased in all coated screws (p<0.05). Torque loss before and after fatigue test was the smallest in TiC-coated screws, and the largest in non-coated screws (p<0.05), and there was no statistically significant difference between dry condition and wet condition of screws because of higher surface hardness and lower friction coefficient. From the above results, TiN, TiCN, TiC coating group had high abrasion resistance, especially TiC coated group which had low torque-consuming, high rotation angle as low friction coefficient will be considered to influence on implant abutment screw joint stability positively.

An Experimental Study on the Spray Characteristics of a Rotating Fuel Nozzle of a Slinger Combustor for Different Flow Rates and Rotating Speeds (슬링거 연소기 회전연료노즐의 유량과 회전수에 따른 분무특성에 대한 실험적 연구)

  • Shim, Hyeon-Seok;Bae, Jonggeun;Kim, Jupyoung;Kim, Shaun;Kim, Donghyun;Ryu, Gyongwon
    • Journal of the Korean Society of Propulsion Engineers
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    • v.25 no.4
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    • pp.59-70
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    • 2021
  • An experimental study was conducted to observe the spray characteristics for different flow rates and rotating speeds of a rotating fuel nozzle of a slinger combustor. The water spray ejected from the nozzle orifice was visualized using a high-speed camera and a light source. It was confirmed that the atomization was improved, as the flow rate decreased and rotating speed increased. The characteristic maps for the spray characteristics and performance parameters showed that the aerodynamic Weber number and the liquid-air momentum flux ratio were associated with the liquid primary breakup, and the liquid-air momentum flux ratio and Rossby number were closely correlated with the liquid ejection mode.