• Title/Summary/Keyword: 구성품성능도

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Influence of Design Parameters on the Behavior of Pyrotechnic Separation Nut (파이로테크닉 분리 너트 거동에 대한 설계 인자의 영향 분석)

  • Woo, Jeongmin;Kim, Jeong Ho;Cho, Jin Yeon;Jang, Seung-Gyo;Lee, Hyo-Nam;Yang, Hee Won
    • Journal of the Korean Society for Aeronautical & Space Sciences
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    • v.47 no.9
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    • pp.617-628
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    • 2019
  • The currently considered pyrotechnic separation nut is separated through the complicated process, because it has many internal moving parts and two variable-volume chambers connected by the vent hole. Therefore, it has many design parameters. Some of these are the contact angles between internal moving parts, the masses of the internal moving parts, the inner diameter of the push rod protrusion, the initial volumes of the chambers, the mass of the explosive charge, and the diameter of the vent hole. To improve the pyrotechnic separation nut, it is necessary to understand how the behavior of the separation nut is changed according to design parameters. In this point of view, parametric studies are carried out using the previously proposed prediction model for pyrotechnic separation nut behaviors. In each case, the parameter of the interest is changed while the others are kept unchanged. From the results, it is investigated how each design parameter influences the separation behavior.

Development of a Portable Vibration Analyzer for Precision Diagnosis of Plant's Rotating Equipment (발전소 회전기기 정밀진단을 위한 휴대용 진동분석기 개발)

  • Noh, Hyungho;Y, Hoseon
    • Plant Journal
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    • v.17 no.4
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    • pp.53-60
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    • 2021
  • The purpose of this study was to develop a portable vibration analyzer that is effective for acquiring and analyzing vibration data of rotating equipment of a power plant and a domestic vibration monitoring system manufacturer Nada Co., Ltd. The hardware of the developed portable vibration analyzer minimizes measurement errors by calibrating the measured values obtained through measurement uncertainty for calibration of the measuring devices in the system, and is composed of a signal processing device with high resolution through high speed data processing. The software structure implements a variety of vibration plots to execute a detailed analysis program, and applies algorithms to measure and remove noise caused by disturbances while operating a rotating machine. The developed product contributed greatly to increase the user's mobility and performance, as well as to reduce the purchase cost due to localization.

A Study on the Design Improvement to prevent the stoppage phenomenon of Launch Support Device for Self-Propelled Artillery (자주포용 발사지지대의 멈춤현상 방지를 위한 설계개선 연구)

  • Kim, Sung Hoon;Park, Young Min;Noh, Sang Wan;Park, Dae Hoon
    • Journal of the Korea Academia-Industrial cooperation Society
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    • v.21 no.5
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    • pp.443-450
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    • 2020
  • This paper reports a design improvement study to solve the stoppage phenomenon caused by the launch-support device applied to K105A1. The K105A1 is a weapon system equipped with an old 105 mm towed howitzer in a wheeled vehicle, which provides superior maneuverability compared to track equipment. The launch support device serves to withstand fire impact and load. In this way, this device is fixed firmly to the ground in preparation for the shooting mission and is responsible for the critical performance, such as fixing the position of the vehicle. On the other hand, during the field test, a temporary stoppage of the launch support occurred, which caused a problem of not being fixed to the ground. To solve this problem, the cause of failure was analyzed by a replay test and parts inspection. In addition, the operating concept, method, and design were analyzed to derive the cause and solve the problem by changing the parts design. Finally, the performance and firing missions were performed normally by applying the changed design to K105A1. The performance stability and reliability of the launch support device were confirmed, which are expected to be of great assistance in the development of military equipment in the future.

Study on the Phase II Qualification Test for Fuel Cell of Rotorcraft (회전익항공기용 연료셀 Phase II 인증시험에 대한 고찰)

  • Kim, Hyun-Gi;Kim, Sung Chan
    • Journal of the Korea Academia-Industrial cooperation Society
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    • v.14 no.3
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    • pp.1054-1060
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    • 2013
  • Fuel tank of a rotorcraft has a great influence on the survivability of crews. For a long time, US army has tried to develop the proper material for fuel cell of a military rotorcraft. As a result, the design specification of fuel cell, MIL-T-27422A, was issued for the first time on 1961. Through a few revisions, it has been developed to ML-DTL-27422D in 2007. It should be assured that fuel cell satisfies the requirement defined in MIL-DTL-27422D. The qualification test of this specification is classified into Phase I test for material and Phase II for fuel cell itself. This paper studies test conditions and procedures of slosh & vibration, gunfire resistance and crash impact test. They are considered as the most important tests which have a high possibility of failure. The rational consideration of this paper can improve the ability for estimating not only the validity of test procedure and test condition but test result. Based on the rational consideration, it is expected that the ability of the systematic development can be improved.

Experimental Study on Applying a Transition Track System to Improve Track Serviceability in Railway Bridge Deck Ends (철도교량 단부 궤도의 사용성 향상을 위한 횡단궤도시스템 적용에 관한 실험적 연구)

  • Lim, Jongil;Song, Sunok;Choi, Jungyoul;Park, Yonggul
    • Journal of the Korean Society for Railway
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    • v.16 no.3
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    • pp.207-216
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    • 2013
  • The components of concrete track (rail and rail fastening system) in railway bridge deck ends are damaged and deteriorated by track-bridge interaction forces such as uplift forces and compression forces owing to their structural flexural characteristics (bridge end rotation). This had led to demand for alternatives to improve structural safety and serviceability. In this study, the authors aim to develop a transition track to enhance the long term workability and durability of concrete track components in railway bridge deck ends and thereby improve the performance of concrete track. A time-history analysis and a three-dimensional finite element method analysis were performed to consider the train speed and the effect of multiple train loads and the results were compared with the performance requirements and German standard for transition track. Furthermore, two specimens, a normal concrete track and a transition track, were fabricated to evaluate the effects of application of the developed transition track, and static tests were conducted. From the results, the track-bridge interaction force acting on the track components (rail displacement, rail stress, and clip stress) of the railway bridge deck end were significantly reduced with use of the developed transition track compared with the non-transition track specimen.

Performance Test of a 75-tonf Rocket Engine Turbopump (75톤급 액체로켓엔진용 터보펌프 실매질 성능시험)

  • Jeong, Eunhwan;Kwak, Hyun-Duck;Kim, Dae-Jin;Kim, Jin-Sun;Noh, Jun-Gu;Park, Min-Ju;Park, Pyun-Goo;Bae, Jun-Hwan;Shin, Ju-Hyun;Wang, Seong-Won;Yoon, Suck-Hwan;Lee, Hanggi;Jeon, Seong-Min;Choi, Chang-Ho;Hong, Soon-Sam;Kim, Seong-Lyong;Kim, Seung-Han;Woo, Seong-Phil;Han, Yeong-Min;Kim, Jinhan
    • Journal of the Korean Society of Propulsion Engineers
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    • v.20 no.2
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    • pp.86-93
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    • 2016
  • Performance tests of a 75-tonf liquid rocket engine turbopump were conducted. The performance of sub-components - two pumps and a turbine - and their power matching were measured and examined firstly near the design speed under the LN2 and kerosene environment. In the real propellant - LOX and kerosene - environment tests, design and off-design performance of turbopump were fully verified in regime of the rocket engine operation. During the off-design performance tests, turbopump running time was set longer than the engine operating time to verify the pump operability and set the pump inlet pressure close to design NPSHr to investigate pump suction capability in parallel. It has been found that developed-turbopump satisfied all of the engine required performances.

Development of the Accelerated Life Test Method & Life Test Equipment for the Counterweight of the Construction Machinery (건설기계용 카운터웨이트 시험장비 및 가속수명시험법 개발)

  • Lee, Gi-Chun;Lee, Young-Bum;Choi, Byung-Oh;Kang, Bo-Sik;Kim, Do-Sik;Choi, Jong-Sik;Kim, Jae-Hoon
    • Transactions of the Korean Society of Mechanical Engineers A
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    • v.39 no.12
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    • pp.1275-1280
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    • 2015
  • A large-sized exciter that vibrates a two-ton component is required to simulate the field operating conditions of a counterweight of an excavator. However, it is difficult for a small-medium sized company to obtain a large exciter for the life test of a counterweight which is an equivalent counterbalancing weight that balances a load. Therefore, in this study, we developed life test equipment for evaluating the reliability of construction machinery weighing about two tons. It simulates the field operating conditions using rotational vibrators consisting of electric motors. A failure analysis of the counterweight was also performed for the major components. Field data acquired from various sites were applied to the life test design of the counterweight. Finally, a zero-failure qualification test based on the accelerated life test was designed, and there was no failure during the test, which guarantees a life of $B_5$ 10,000 hours.

3-Phase Power Quality Disturbance Generator with Phase Jump Function (위상급변 기능을 갖는 3상 전력품질 외란발생기)

  • Lee, B.C.;Choi, S.H.;Paeng, S.H.;Park, S.D.;Choi, N.S.;Kim, I.D.;Chun, T.W.;Kim, H.G.;Nho, E.C.
    • The Transactions of the Korean Institute of Power Electronics
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    • v.11 no.5
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    • pp.463-470
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    • 2006
  • This paper deals with a new 3-phase power quality disturbance generator. The proposed generator can provide phase jump as well as voltage sag, swell, outage, unbalance, and over and under voltage. The operating principle of the generator is described in each mode of disturbance. The magnitude of the phase jump is analysed and it is found that the magnitude is the function of the turn-ratios of the transformers consisting the generator. The scheme has simple structure compared with the conventional one, and the major components of the proposed scheme are SCR thyristor and transformer, which guarantees high reliability and cost-effective implementation of the generator. Furthermore, high efficiency can be obtained because there is no PWM switching of the semiconductor devices, and it is easy to control the system. Simulations are carried out to confirm the operation in each disturbance mode, and experiments has been done with 5kVA power rating. The usefulness of the proposed scheme is verified through simulation and experimental results. It is expected that the scheme can be applied to the performance test of the custom power devices such as UPS, DVR, DSTATCOM, and SSTS with cost-effective system.

Tubular Type Direct Methanol Fuel Cell for in situ NMR Diagnosis (In Situ NMR 진단용 원통형 직접 메탄올 연료전지)

  • Joh, Han-Ik;Um, Myung-Sup;Han, Kee-Sung;Han, Oc-Hee;Ha, Heung-Yong;Kim, Soo-Kil
    • Journal of the Korean Electrochemical Society
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    • v.12 no.4
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    • pp.329-334
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    • 2009
  • This study is to develop a fuel cell system applicable to an in situ NMR (Nuclear magnetic resonance) diagnosis. The in situ NMR can be used in real time monitoring of various reactions occurring in the fuel cell, such as oxidation of fuel, reduction of oxygen, transport phenomena, and component degradation. The fuel cell for this purpose is, however, to be operated in a specifically designed tubular shape toroid cavity detector (TCD), which constrains the fuel cell to have a tubular shape. This may cause difficulties in effective mass transport of reactants/products and uniform distribution of assembly pressure. Therefore, a new flow field designed in a particular way is necessary to enhance the mass transport in the tubular fuel cell. In this study, a tubular-shaped close-type flow field made of non-magnetic material is developed. With this flow field, oxygen is effectively delivered to the cathode surface and the produced water is readily removed from the membrane-electrode assembly to prevent flooding. The resulting DMFC (direct methanol fuel cell) outperforms the open-type flow field and exhibits $36\;mW/cm^2$ even at room temperature.

Development of Tacho Generator for Application of Anti-aircraft Weapon System (대공무기체계 적용을 위한 타코제너레이터 개발)

  • Byun, Kisik;Park, Jun Young;Cho, Sung-Yong
    • Journal of the Korea Academia-Industrial cooperation Society
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    • v.21 no.10
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    • pp.174-180
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    • 2020
  • This paper presents the development of a tacho generator that is applicable to a DC motor for anti-aircraft weapon systems. In general, devices such as tacho generators and resolvers are used as feedback devices for controlling DC motors. A tacho generator with a wide operating temperature range was developed, which has robust characteristics against shock loads and vibrations according to the operational characteristics of anti-aircraft weapon systems. The target specifications were set based on the requirements of the tacho generator currently in operation. A rotor coupled to the shaft of the motor and a stator coupled to the housing of the motor were then designed and manufactured. The inductance was 31.0 mH, the terminal resistance was 147.7 ohms, and the rotational measurement factor was satisfactory under both normal operation and operating conditions after the maximum speed for the standard of 9.500 ± 0.475 V/krpm. In addition, the environmental suitability of the applied equipment was confirmed through the rate of change in unit temperature, and it was found that the temperature characteristics were all within 0.03 %/℃.