DOI QR코드

DOI QR Code

Hot Test of a Turbopump for a Liquid Rocket Engine

액체로켓엔진용 터보펌프의 고온 성능시험

  • Published : 2009.12.01

Abstract

Hot test of a full-scale turbopump for a 30-ton-thrust liquid rocket engine was carried out. The turbopump is composed of an oxidizer pump, a fuel pump, and a turbine on a single shaft. Model fluid was used in the test, that is, hot air for the turbine and water for the pumps. The turbopump was operated stably at full speed for 120 seconds. In terms of performance characteristics of pumps and turbine, the results from the turbopump assembly test are compared with those from the turbopump component tests which were performed at about half of the design rotational speed.

Keywords

References

  1. Kim, J., Hong, S. S., Jeong, E. H., Choi, C. H. and Jeon, S. M., 2005, ' Development Status of a Turbopump for 30-ton Thrust Level of Engine,' Proceedings of Korean Society of Propulsion Engineers Fall Conference, Daejeon, Korea, pp. 375-383
  2. Kim, J., Lee, E. S., Choi, C. H. and Jeon, S. M., 2004, ' Current Status of Turbopump Development in Korea Aerospace Research Institute, ' Proceedings of 55th International Astronautical Congress, IAC-04-S.P.17, Vancouver, Canada
  3. Kim, D. J., Hong, S. S., Choi, C. H. and Kim, J., 2005, ' Performance Tests of a Fuel Pump for a Turbopump Unit,' Proceedings of the Sixth KSME-JSME Thermal and Fluids Engineering Conference, EA05
  4. Hong, S. S., Kim, D. J., Kim, J. S., Choi, C. H. and Kim, J., 2005, ' Effect of Inducer on Hydraulic Performance of a Turbopump,' Proceedings of the 41st AIAA/ASME/SAE/ASEE Joint Propulsion Conference and Exhibit, AIAA 2005-3947
  5. Jeong, E. H. and Kim J., 2005, ' Experiments on Supersonic Impulse Turbine,' Journal of Fluid Machinery, Vol. 8, No. 6, pp. 26-32 https://doi.org/10.5293/KFMA.2005.8.6.026
  6. Jeong, E. H., Kang, S. H., Shin, D. Y., Park, P. and Kim J., 2006, ' Experimental Investigation of Turbopump Turbine : Turbine Performance and Effect of Nozzle-Rotor Clearance,' Journal of Korean Society of Propulsion Engineers, Vol. 12, No. 5, pp. 78-86
  7. Hong, S. S., Kim, D. J., Kim, J. S. and Kim, J., 2008, ' Hydrodynamic Performance Test of a Turbopump Assembly,' Trans. of the KSME(B), Vol. 32, No. 4, pp. 249-254 https://doi.org/10.3795/KSME-B.2008.32.4.249
  8. Takida, J., Yoshikawa, K., Ogawara, A., Atsumi, M., Miyagawa, K., Kobayashi, K. and Miyawaki, T., 2007, ' Development of High Performance Oxidizer Turbo-pump,' Proceedings of the 43rd AIAA/ASME/SAE/ASEE Joint Propulsion Conference & Exhibit, Cincinnati, OH., AIAA 2007-5509
  9. Kinefuchi, K., Uchiumi, M., Inoue, M. and Hirata, K., 2005, ' LE-7A FTP Full Load Cold Run,' Proceedings of Asian Joint Conference on Propulsion and Power, Kitakyushu, Japan, AJCPP2005-22033

Cited by

  1. vol.13, pp.1, 2010, https://doi.org/10.5293/KFMA.2010.13.1.052