• 제목/요약/키워드: metal working

검색결과 485건 처리시간 0.027초

주기적 생산 스케쥴링 전략의 성능 (Performance of periodic production scheduling policy)

  • 송석천;유준
    • 제어로봇시스템학회:학술대회논문집
    • /
    • 제어로봇시스템학회 1988년도 한국자동제어학술회의논문집(국내학술편); 한국전력공사연수원, 서울; 21-22 Oct. 1988
    • /
    • pp.343-348
    • /
    • 1988
  • This paper describes an application of the periodic scheduling policy to a class of flexible manufacturing systems. A heuristic algorithm is used to determine when each part should be loaded into the system. Simulation results based on a detailed model of metal-working manufacturing facility are presented.

  • PDF

드로비드가 판재성형에 미치는 영향에 관한 실험적 연구 (An Experimental Study on the Effect of the Draw-beads in Sheet Metal Forming)

  • 김진무;유호영;고대림
    • 한국정밀공학회:학술대회논문집
    • /
    • 한국정밀공학회 1994년도 추계학술대회 논문집
    • /
    • pp.240-245
    • /
    • 1994
  • Experiments on the drawability of squared boxes have been performed under various working conditions. In the present work, the pattern of material flow and the local change in the thickness of shell are used as the measures of drawability, and they are measured using the photo-etching technique. The effects of the size of draw bead, the magnitude of blank holding force and the condition of lubrication on the drawability of squared boxes have been analyzed.

  • PDF

직선가이드프레스 구동부의 최적화 (Optimization of the Dirve for Lineaer-Guide Press)

  • 이영섭;황병복
    • 소성∙가공
    • /
    • 제9권2호
    • /
    • pp.171-178
    • /
    • 2000
  • This paper is concerned with the optimization of the drive for linear-guide press which is one of mechanical presses. The design of linear-guide drive for a mechanical press is introduced and the drive for the linear-guide press is optimized for the improvement of load and velocity characteristics. As a result of optimization, the load capacity during stroke increases and the slide velocity decreases in working region, respectively. The new design could be suited to many applications in precision forming such as extrusion and the sheet metal-forming processes.

  • PDF

최적 가공방법의 선택을 위한 모형화 (Modeling the Problem for the Optimal Selection of Process Plans)

  • 기재석;강맹규
    • 산업경영시스템학회지
    • /
    • 제14권24호
    • /
    • pp.193-198
    • /
    • 1991
  • Is this paper the selection of a set of process plans is considered for a flexible manufacturing systems. This problem arises in the metal working industry when numerical controlled(N/C) machines are used to manufacture parts. In this paper a new concept to reduce the size of problem is proposed. A corresponding Integer programming model is formulated. The model formulated is to minimize corresponding manufacturing cost and minimize the number of tools and auxiliary devices such as fixtures, grippers, and feeders.

  • PDF

최적의 프로필렌/프로판 흡착 분리 성능을 가지는 흡착제의 개발 전략들 (Design Strategies for Adsorbents with Optimal Propylene/propane Adsorptive Separation Performances)

  • 김태훈;이승준;김서율;김아름;배윤상
    • Korean Chemical Engineering Research
    • /
    • 제57권4호
    • /
    • pp.484-491
    • /
    • 2019
  • 산업적으로 중요한 가치를 지니는 폴리프로필렌 합성의 원료인 프로필렌을 고순도로 얻기 위해서는 효율적인 프로필렌/프로판 분리 기술이 필요하다. 기존 증류 공정은 프로필렌과 프로판의 유사한 물리화학적 성질로 인해 매우 높은 에너지가 소모되기때문에, 흡착분리 기술이큰관심을받고있다. 본연구에서는 Grand Canonical Monte Carlo (GCMC) 분자 모사를 활용하여 기공의 형태가 다른 두 종류의 유무기복합다공체(Metal-Organic Frameworks)의 빈금속배위자리(open metal sites) 흡착 강도를 임의로 조절하며 프로필렌/프로판 흡착 분리 성능의 변화를 조사하였다. 흡착 분리 성능은 작업 용량, 선택도, Adsorption Figure of Merit (AFM) 등으로 평가하였고, 이를 통해 흡착제가 최적의 프로필렌/프로판 분리 성능을 가지기 위해 필요한 흡착 사이트의 밀도 및 강도 그리고 온도 조건 등을 제시하였다.

알루미늄 연속주조 용탕의 탈 가스 일체화 장치 개발 (Development of a monolithic apparatus for degasing aluminum continuous casting molten metal)

  • 이용중;김태원;김기대;류재엽;이형우
    • 한국공작기계학회:학술대회논문집
    • /
    • 한국공작기계학회 2004년도 추계학술대회 논문집
    • /
    • pp.145-149
    • /
    • 2004
  • It is necessary for managing a perfect process for degasing aluminum molten metal according to the increase of a grade of aluminum and its alloy products. There are some methods that have been used to manage a degasing process in recent years, such as an injection method that uses aluminum molten metal powder and chemicals supplier and input method that supplies argon and nitrogen, or chlorine gas by using a gas blow-tube. However, these methods show some problems, and it shows that it is a difficult process to handle. pollution due to the producing a lot of toxic gases like chlorine and fluoride gas. irregular effects, and lowering work efficiency due to the excessive processing time. The problems that are the most fatal are the producing a lot of sludge due to the reaction of aluminum molten metal with chemicals. loss of metals, and decreasing the life of refractory materials. In order to solve these problems. this paper develops a technology that is related to aluminum continuous casting molten metal and monolithic degasing apparatus. A degasing apparatus developed in this study improved the exist ing methods and prevented environmental pollution wi th smokeless. odor less, and harmlessness by using a new method that applies argon and nitrogen gas in which the methods used in the West and Japan are eliminated. The developed method can significantly reduce product faults that are caused by the production of gas and oxidation because it uses a preprocessed molten metal with chemicals. In addition. the amount of the produced sludge can also be reduced by 60-80% maximum compared with the existing methods. Then. it makes it possible to minimize the loss of metals. Moreover. the molten metal processing and settling time is also shortened by comparing it with the existing methods that are applied by using chemicals. In addition, it does much to improve the workers' health, safety and environment because there is no pollution. The improvement of productivity and prevent ion effects of disaster from the results of the development can be summarized as follows. It will contribute to the process rationalization because it does not have any unnecessary processes that the molten metal will be moved to an agitator by using a ladle and returned to process for degasing like the existing process due to the monolithic configuration. There are no floating impurities due to the oxidation caused by the contact with the air as same as the existing process. In addition. it can protect the blending of precipitation impurities. Because it has a monolithic configuration. it can avoid the use of additional energy to compensate the temperature decreasing about 60t that is caused by the moving of molten metal. It is not necessary to invest an extra facilities in order to discharge the gas generated from a degasing process by using an agitator. The working environment can be improved by the hospitable air in the factory because the molten metal is almost not exposed in the interior of the area.

  • PDF

폐타이어 열분해에 의한 카본블랙을 이용한 황화수소와 암모니아 제거를 위한 흡착제 개발 (Development of Adsorbents for Removal of Hydrogen Sulfide and Ammonia Using Carbon Black from Pyrolysis of Waste Tires)

  • 서양곤;김창준;김대혁
    • 청정기술
    • /
    • 제21권2호
    • /
    • pp.108-116
    • /
    • 2015
  • 황화수소와 암모니아는 많은 하수처리장과 산업 플랜트로부터의 배출가스에서 발견되어질 수 있는 가장 흔한 악취성분이다. 이들 유해물질들은 인간에게 건강 문제를 일으키고 촉매에 악영향을 미치기 때문에 생활환경과 산업 현장에서의 제거는 매우 중요하다. 본 연구에서는 황화수소와 암모니아에 대한 우수한 흡착능력을 가지는 흡착제를 개발하기 위하여 폐타이어의 열분해 생성물인 카본블랙을 이용하였다. 카본블랙, 금속산화물과 산 또는 염기를 혼합하여 펠렛형 흡착제를 제조하였고, 상온상압에서 고정층 흡착탑의 파과곡선을 이용하여 황화수소와 암모니아에 대한 흡착성능을 평가하였다. 카본블랙, 산화철(III)과 수산화나트륨 혼합물로 제조된 흡착제가 황화수소에 대한 가장 우수한 작업능력을 나타내었다. 암모니아에 대해서는 카본블랙, 산화구리(II), 염산의 혼합물로 제조된 흡착제가 우수한 작업능력을 보였다.

고온 유리 성형 공정을 위한 직육면체형 Sodium 히트파이프의 실험 연구 (An Experimental Study on a Rectangular Parallelepiped Sodium Heat Pipe for High Temperature Class Forming)

  • 박수용;부준홍;김준범
    • 대한기계학회논문집B
    • /
    • 제26권11호
    • /
    • pp.1622-1629
    • /
    • 2002
  • To enhance isothermal characteristics of glass-farming surface, a rectangular parallelepiped heat pipes was fabricated, tested, and analyzed. The working fluid was sodium and the wall material was stainless steel 304. The dimension of the heat pipe was 210 (L) $\times$ 140(W) $\times$ 92(H)mm. A lattice structure covered with screen mesh was inserted to promote return of working fluid. The bottom side of heat pipe was heated electrically and the top side was cooled by liquid circulation. The temperature distribution at the bottom surface was of major concern and was monitored to determine isothermal characteristics. A frozen start-up of rectangular parallelepiped liquid metal heat pipe was tested. The operating mode of the sodium heat pipe was affected by the temperature of cooling zone, input heat flux, and the operating temperature of heat pipe. The heat pipe operated in a normal fashion as long as the heat flux was over 5.78W/cm$^2$, and the inside wall temperature of condenser part was above 95$^{\circ}C$ The maximum temperature difference at the bottom surface was observed to be 32$^{\circ}C$ when the operating temperature of the heat pipe was operating normally around 50$0^{\circ}C$. The result showed that a sodium heat pipe was very effective in reducing significantly the temperature difference in the glass-forming surface.

영상표시단말장치의 작업공간 배열에 따른 전자파 폭로 정도 (The Level of Exposure to Electromagnetic Fields Strength from VDT According to the Arrangement of Working Space VDT)

  • 한상일;이세훈
    • 한국산업보건학회지
    • /
    • 제8권1호
    • /
    • pp.146-154
    • /
    • 1998
  • This study was designed to investigate the workers' exposure level to electromagnetic field(EMF) in accordance with the VDT arrangement in the work place and distance from VDT. Author compared the exposure strength of EMF in line group(workers exposed to EMF from both front and back side) and in shielding group(workers exposed to EMF exclusively from front side). The levels of EMF at 30cm and 50cm from front side and at 30cm from back side of VDT were also measured. The result were as follows: 1. Mean distance between a monitor and a worker in shielding group ($47.7{\pm}8.7cm$) significantly longer than that in line group($44.3{\pm}7.2cm$). Strength of EMF in shielding group [$1.3{\pm}0.7V/m$ (electric field) and $18.2{\pm}11.5mA/m$ (magnetic field) were lower than in line group [$1.4{\pm}0.6V/m$ and $26.6{\pm}11.6mA/m$, respectively] at the workers' position. 2. The strength of EMF was decreased with the distance from VDT. The strength at 70cm from VDT was nearly the same as the background strength in the ordinary office rooms. 3. Working distance from 9 inch monitor was significantly shorter than that from 14 inch and wider sized monitors. 4. The strength of EMF in extremely low frequency spectrum of color monitors was higher then that of black and white monitor. 5. Metal coated filters significantly decreased the electric field strength of EMF when earth line was connected. Metallic shield was effectively decreased the EMF strength from VDT, but wooden shield was not. From the above results, line type arrangement of VDT in the work place using metallic shield at the back side of VDT, and metal coated filter to monitor with application of earth line were recommended. It is also recommended to maintain workers position to be 60cm or more distance from monitor and 140cm or more between VDTs for minimizing workers' exposure to EMF.

  • PDF

부산지역 일부 제조업 산업장의 기중 5가지 화학물질의 경시적 농도 변화 (Chronological Concentration Change of Five Chemical Substances in Manufacturing Industry of Busan Area)

  • 박준제;선병관;손병철;문덕환
    • 한국산업보건학회지
    • /
    • 제16권1호
    • /
    • pp.68-80
    • /
    • 2006
  • This study aimed to prepare the fundamental data and assess the status and trend of exposure level for 5 chemical substances such as sulfuric acid, hydrogen chloride, ammonia, formaldehyde and phenol in manufacturing industry by type of industry, working process, and size of factory, chronological change. Subjects related to this study consist of 146 factories, 12 industries and 17 working processes located in Busan area from Jan. 1997 to Dec. 2001. 1. All 5 kinds of chemical substances by type of industry, working process were generated in chemical manufacturing industry. There were founded in 8 types of industries and 13 types of working processes for ammonia, which is the highest number of in all 5 chemical substances. 2. In terms of the exposure level for 5 chemical substances by type of industry, working process, geometric mean concentration for sulfuric acid was $0.40mg/m^3$ in manufacture of chemicals and chemical products, $0.30mg/m^3$ in compounding process, for hydrogen chloride was 0.57 ppm in manufacture of basic metal, 0.48 ppm in dyeing process, for ammonia was 1.11 ppm in manufacture of rubber and plastic products, 0.94 ppm in buffing process, for formaldehyde was 0.49 ppm in manufacture of wood and of products of wood and cork, except furniture; manufacture of articles straw and plating materials, 0.53 ppm in mixing process, and for phenol were 0.53 ppm in manufacture of chemical and chemical products, 0.55 ppm in compounding process, respectively. Results for 5 chemical substances by type of industry and working process were significantly higher than those of the others(p<0.05). 3. The exposure level for hydrogen chloride, formaldehyde were significantly increased by size of industry (p<0.01). ammonia was significantly decreased by size of industry (p<0.01). 4. In trend of the concentration difference of five chemical substances by chronology, geometric mean concentration for sulfuric acid was significantly increased (p<0.01), hydrogen chloride and ammonia were significantly decreased by year (p<0.05) and for formaldehyde and phenol were decreased in chronological change. According to the above results 5 chemical substances were founded together in a way mixed in the same places one another and concentrations of chemical substances by industry, working process, size of industry and year appeared markedly. The authors recommend more systemic and effective work environmental management should be conducted in workplaces generating five chemical substances.