• 제목/요약/키워드: interval velocity

검색결과 325건 처리시간 0.032초

보행(步行) 이앙기(移秧機)를 위(爲)한 무선자동제어(無線自動制御) 시스템의 개발(開發)(II) -공시기(供試機)의 포장실험(圃場實驗)- (Development of a Wireless Control System for Rice Transplanter of Walking Type(II) -Field Test of the Experimental Machine-)

  • 김창수;최규홍;민영봉;김성태
    • Journal of Biosystems Engineering
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    • 제17권3호
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    • pp.213-222
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    • 1992
  • To develop the wireless remote opreating system of walking rice transplanter, this study was carried out for manufacturing the wireless remote control system acting upon the transplanter. The first report of this study contained about the construction and operating method of a developed remote control system for 2-row walking type transplanter. It is the second report about the field test for an experimental transplanter being attached a wireless control system and for a conventional transplanter. The test was executed to investigate the characteristics of velocity, rectilinearity, turning time, interval of roots and of rows, and field capacity in accordance with various engine speeds for an experimental transplanter. The measurements of this test were compared with those of the conventional transplanter. The obtained results were as follows : 1. The operating velocity of the experimental transplanter was faster than the conventional one when the high speed range of the engine but the variances were very large. 2. The rectilinearity, interval of raws and of roots, and the turning time of the experimental transplanter was inferior to the conventional one at some speed ranges of the engine. 3. Field capacity of the experimental transplanter was superior to the conventional one at high speed of the engine. 4. There were some disadvantages for the experimental transplanter to operate, because it was constructed without any aid devices, such as float and hydraulic system for instance. But if the remote control system of this study equip at the modern walking transplanter, it will be improved and utilized without defects which was revealed from this test.

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주름필터를 적용한 CYBAGFILTER®의 여과성능 특성 (Dust Filtration Characteristics of Pleated Filter Bags Installed in CYBAGFILTER®)

  • 박영옥;노학재;이영우
    • 한국대기환경학회지
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    • 제24권4호
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    • pp.483-491
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    • 2008
  • The filtration characteristics of $CYBAGFILTER^{(R)}$ unit with pleated filter bags were evaluated by comparing the performance of the unit with the lower part of cyclone shape with that of the unit with conventional lower part. Results from the test were also compared with those from the previous research with the $CYBAGFILTER^{(R)}$ in which round filter bags were installed. $CYBAGFILTER^{(R)}$ is the unit which combines the centrifugal separation mechanism and the fabric filtration mechanism in a single unit for efficient removal of particulate matters. The pleated filter bags are made of pleated fabric with an extension of the filtration area about 3 times compared with the conventional round filter bags. The results from the test using pleated filter bags showed an overall collection efficiency of over 99.9% regardless of the shape of lower part installed. When the lower part of cyclone shape was installed, the filter cleaning interval was over 2 times longer compared with that when the conventional lower part was installed. At the same conditions of filtration velocity and filter pressure drop, the $CYBAGFILTER^{(R)}$ with the lower part of cyclone shape, in which the pleated filter bags are installed, can be operated with a flow rate of round 3 times higher than that with conventional round filter bags.

차량의 데이터 처리 오버헤드를 줄이기 위한 이동 속도와 거리 추정 기반의 센싱 데이터 수집 주기 제어 기법 (Velocity and Distance Estimation-based Sensing Data Collection Interval Control Technique for Vehicle Data-Processing Overhead Reduction)

  • 권지수;박대진
    • 한국정보통신학회논문지
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    • 제24권12호
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    • pp.1697-1703
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    • 2020
  • 주변 환경으로부터 직접 데이터를 수집하는 센서 노드는 많은 제약 조건을 가지기 때문에 자원의 효율적인 사용이 필요하다. 본 논문에서는 도로를 주행 중인 차량의 위치 데이터를 수신하는 센서 노드에서, 칼만 필터로 추정한 대상의 속도와 이동 거리 가중치로 데이터 수신 주기를 변경한다. 차량의 속도가 느릴수록 센서 노드의 데이터 수신 주기를 길게 함으로써 전체 네트워크에서 이루어지는 연산 시간을 줄일 수 있다. 제안하는 기법은 MATLAB으로 구현된 교통 시뮬레이터를 통하여 검증하였으며, 기존 방법에 비해 제안하는 기법을 사용하는 센서 네트워크에서 연산에 소요되는 시간이 감소하는 것을 확인하였다.

충격기류식 여과집진장치에서 벤츄리가 압력손실에 미치는 영향 (Prediction of Venturi Effect on Pressure Drop in Pulse Air Jet Bag Filter)

  • 정문섭;김정권;정용현;서정민
    • 한국환경과학회지
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    • 제32권9호
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    • pp.659-669
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    • 2023
  • The purpose of this study is to predict the pressure drop due to the installation of venturi under diverse operating conditions such as dust concentration, pulse interval and pressure, and filtration velocity using algebraic-linear regression model and use it as an economic data and efficient operating condition for a pulse air jet bag filter. A pilot scale bag filter with a filter a filter size(Ø140 × 850ℓ, 12) was used, and the filters used in the experiment were the polyester filters most commonly used in real industrial sites. The SAS 9.4 program (SAS Institute, USA) was used to predict and to determine the effects of inlet concentration (Ci), pulse interval (Pi) and pressure (Pp), filtration velocity (Vf), presence or absence of venturi, etc. The results are shown below. The variation in pressure drop with or without venturi installation was 38.8 mmAq when venturi is installed and 47.6 mmAq when venturi is not installed, indicating a difference in pressure drop of 8.8 mmAq depending on venturi installation. It is estimated that the efficiency can be improved by about 18.5% if the venturi is installed.

초동주시 역산을 통한 KCRT-2008 측선 하부의 지진파 속도구조 (Seismic Velocity Structure Along the KCRT-2008 Profile using Traveltime Inversion of First Arrivals)

  • 김기영;이정모;박창업;정희옥;홍명호;김준영
    • 지구물리와물리탐사
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    • 제13권2호
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    • pp.153-158
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    • 2010
  • 한반도 중남부 지각 속도구조를 밝히기 위해서, 주요 지체구조 경계와 거의 직각을 이루는 북서-남동 방향의 299 km 측선(KCRT-2008)을 따라 대규모 인공지진파 실험을 실시하였다. 21~113 km 간격의 깊이 50~100 m인 8개시추공에서 250~1500 kg의 폭약을 발파하였고, 발생된 지진파 신호는 측선을 따라 평균 500 m 간격으로 매설한 4.5Hz 수신기로 수신하였다. 초동주시를 토모그래피 방식으로 역산한 결과, 파선경로는 2~3, 11~13, 20 km 깊이에 지각 내 굴절면이 존재함을 보인다. 굴절파 속도 7.7~8.1 km/s의 모호면은 중앙부에서 최대 34.2 km 깊이에 달하며, 동해와 황해로 접근하면서 얕아진다. 속도 7.6 km/s 등치선의 깊이는 31.3~34.4 km의 범위에서 변한다. 역산된 속도모델은 옥천계와 경기육괴 하부에, 깊이 7.2 km에 중심을 둔 저속도층이 129km까지 수평으로 연장되어 있고, 경상분지에는 속도5.4 km/s 이하의 저속도 암석이 최대 2.6 km 두께로 쌓여 있는 모습을 보여준다.

단위유량도와 비수갑문 단면 및 방조제 축조곡선 결정을 위한 조속계산 (Calculation of Unit Hydrograph from Discharge Curve, Determination of Sluice Dimension and Tidal Computation for Determination of the Closure curve)

  • 최귀열
    • 한국농공학회지
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    • 제7권1호
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    • pp.861-876
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    • 1965
  • During my stay in the Netherlands, I have studied the following, primarily in relation to the Mokpo Yong-san project which had been studied by the NEDECO for a feasibility report. 1. Unit hydrograph at Naju There are many ways to make unit hydrograph, but I want explain here to make unit hydrograph from the- actual run of curve at Naju. A discharge curve made from one rain storm depends on rainfall intensity per houre After finriing hydrograph every two hours, we will get two-hour unit hydrograph to devide each ordinate of the two-hour hydrograph by the rainfall intensity. I have used one storm from June 24 to June 26, 1963, recording a rainfall intensity of average 9. 4 mm per hour for 12 hours. If several rain gage stations had already been established in the catchment area. above Naju prior to this storm, I could have gathered accurate data on rainfall intensity throughout the catchment area. As it was, I used I the automatic rain gage record of the Mokpo I moteorological station to determine the rainfall lntensity. In order. to develop the unit ~Ydrograph at Naju, I subtracted the basic flow from the total runoff flow. I also tried to keed the difference between the calculated discharge amount and the measured discharge less than 1O~ The discharge period. of an unit graph depends on the length of the catchment area. 2. Determination of sluice dimension Acoording to principles of design presently used in our country, a one-day storm with a frequency of 20 years must be discharged in 8 hours. These design criteria are not adequate, and several dams have washed out in the past years. The design of the spillway and sluice dimensions must be based on the maximun peak discharge flowing into the reservoir to avoid crop and structure damages. The total flow into the reservoir is the summation of flow described by the Mokpo hydrograph, the basic flow from all the catchment areas and the rainfall on the reservoir area. To calculate the amount of water discharged through the sluiceCper half hour), the average head during that interval must be known. This can be calculated from the known water level outside the sluiceCdetermined by the tide) and from an estimated water level inside the reservoir at the end of each time interval. The total amount of water discharged through the sluice can be calculated from this average head, the time interval and the cross-sectional area of' the sluice. From the inflow into the .reservoir and the outflow through the sluice gates I calculated the change in the volume of water stored in the reservoir at half-hour intervals. From the stored volume of water and the known storage capacity of the reservoir, I was able to calculate the water level in the reservoir. The Calculated water level in the reservoir must be the same as the estimated water level. Mean stand tide will be adequate to use for determining the sluice dimension because spring tide is worse case and neap tide is best condition for the I result of the calculatio 3. Tidal computation for determination of the closure curve. During the construction of a dam, whether by building up of a succession of horizontael layers or by building in from both sides, the velocity of the water flowinii through the closing gapwill increase, because of the gradual decrease in the cross sectional area of the gap. 1 calculated the . velocities in the closing gap during flood and ebb for the first mentioned method of construction until the cross-sectional area has been reduced to about 25% of the original area, the change in tidal movement within the reservoir being negligible. Up to that point, the increase of the velocity is more or less hyperbolic. During the closing of the last 25 % of the gap, less water can flow out of the reservoir. This causes a rise of the mean water level of the reservoir. The difference in hydraulic head is then no longer negligible and must be taken into account. When, during the course of construction. the submerged weir become a free weir the critical flow occurs. The critical flow is that point, during either ebb or flood, at which the velocity reaches a maximum. When the dam is raised further. the velocity decreases because of the decrease\ulcorner in the height of the water above the weir. The calculation of the currents and velocities for a stage in the closure of the final gap is done in the following manner; Using an average tide with a neglible daily quantity, I estimated the water level on the pustream side of. the dam (inner water level). I determined the current through the gap for each hour by multiplying the storage area by the increment of the rise in water level. The velocity at a given moment can be determined from the calcalated current in m3/sec, and the cross-sectional area at that moment. At the same time from the difference between inner water level and tidal level (outer water level) the velocity can be calculated with the formula $h= \frac{V^2}{2g}$ and must be equal to the velocity detertnined from the current. If there is a difference in velocity, a new estimate of the inner water level must be made and entire procedure should be repeated. When the higher water level is equal to or more than 2/3 times the difference between the lower water level and the crest of the dam, we speak of a "free weir." The flow over the weir is then dependent upon the higher water level and not on the difference between high and low water levels. When the weir is "submerged", that is, the higher water level is less than 2/3 times the difference between the lower water and the crest of the dam, the difference between the high and low levels being decisive. The free weir normally occurs first during ebb, and is due to. the fact that mean level in the estuary is higher than the mean level of . the tide in building dams with barges the maximum velocity in the closing gap may not be more than 3m/sec. As the maximum velocities are higher than this limit we must use other construction methods in closing the gap. This can be done by dump-cars from each side or by using a cable way.e or by using a cable way.

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승촌보에 설치된 어도에서 어류의 이동성 평가 (Fish Passage Evaluations in the Fishway Constructed on Seungchon Weir)

  • 최지웅;박찬서;임병진;박종환;안광국
    • 한국환경과학회지
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    • 제22권2호
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    • pp.215-223
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    • 2013
  • The objective of this study was to evaluate fish passage efficiency, based on fish-trap monitoring methodology, in the fishway of Seungchon Weir, which was constructed on the lower region of Yeongsan River in 2011. Seasonal patterns and diel variations of fish movements, fish fauna, and compositions in the fishway were analyzed in relation to the current velocity and location of the trap-setting in the fishway. For the analysis, we conducted seven times surveys in 2012 on the fishway and also conducted intensive monitoring of the fishway as 3 hrs interval for the diel variations of fish fauna and compositions in the fishway. According to the fish-trap monitoring methodology, the total number of fish species was 13 species, which was a 43.3% of the total. Most dominant fish used the fishway was Squalidus chankaensis tsuchigae and the relative abundance of the species used the fishway was 33.5% of the total. The season and time zone (in diel variation) observed most frequently in the fishway were July and 18:00-21:00 PM, respectively. The fish movements and use-rates of fishway varied depending on the locations of trap-setting; Fish biomass and the number of species were statistically (p < 0.05) greater in the most right or left-sided traps than in the mid-traps. Also, fish movements and use-rates of fishway were influenced by current velocity on the fishway; fish in the fishway preferred the low current velocity (mean 0.71 m/sec) than the high current velocity (mean 1.13 m/sec). Further long-term studies should be monitored for the efficiency evaluations of the fishway.

난류하에서의 TMD에 의한 현수교 주탑의 진동제어 (Vibration Control for Tower of Suspension Bridge under Turbulence using TMD)

  • 김기두;황윤국;변윤주;장동일
    • 한국강구조학회 논문집
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    • 제9권2호통권31호
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    • pp.181-191
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    • 1997
  • 케이블이 가설되기 전까지 외팔보 형태로 지지되는 현수교의 주탑에 불규칙적인 변동 공기력이 작용할 때 발생하는 버페팅은 구조물의 기본 고유진동수와 일치하는 풍속이 존재하고 이에 따른 주탑의 공진에 의해 큰 응답을 유발할 수 있다. 버페팅 하중에 의한 동적 응답을 감소시키기 위해서 제진장치의 일종인 TMD(Tuned Mass Damper)를 부착한 주탑의 거동특성에 관한 연구를 유한요소법에 의하여 시간영역에서 수행하였다. 버페팅 하중을 구하기 위하여 주파수 영역의 속도스펙트럼을 시간영역의 무작위변량으로 변환시켰으며, peak factor를 이용하여 일정기간동안 일어날 수 있는 구조물의 최대 변위의 기대치를 구하였다. 최적의 TMD 부착위치와 제원을 변수별 수치해석을 통하여 결정하였으며, 최적의 제원을 갖는 TMD에 의한 풍속별 진동제어 효과를 검토하였다.

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램 가속기 성능 향상을 위한 예 혼합기 조성비 최적화에 관한 연구 (Premixture Composition Optimization for the Ram Accelerator Performance Enhancement)

  • 전용희;이재우;변영환
    • 한국추진공학회지
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    • 제4권2호
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    • pp.21-30
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    • 2000
  • 본 연구에서는 램 가속기의 성능 향상을 위한 수치최적화를 수행하였다. 일정한 형상과 질량을 가진 탄체를 최초의 속도 $V_o$로부터 목표 속도 $V_e$로 가속시킬 때까지의 최소의 램 가속관 길이를 탐색하는 것을 목표로 하였고 $H_2$, $O_2$, $N_2$로 구성된 예 혼합기의 각 화학종의 몰수를 설계변수로서 채택하였다. 목적함수와 구속조건은 설계 과정에서 선형화 하여 구배법과 SLP기법을 적용하였다. 내부유동은 이차원 비점성 유동을 가정하고 화학반응의 해석은 8단계 7화학종 모델을 적용하였다. 가속관 길이의 결정을 위하여 램 가속관 내부의 유동은 준 정상상태로 가정하고 몇 개의 동일 구간으로 분할하여 각 속도에서의 추력 계수와 가속도를 동시에 구하여 전 속도 영역에 대하여 수치 적분하였다. 본 연구를 통하여 7회의 설계 반복으로 가속관의 길이를 19% 감소시켰다. 본 연구의 결과로부터 다단계, 다 화학종의 램 가속기의 설계최적화 문제에 직접적으로 적용할 수 있음을 확인하였다.

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상시미동 측정을 통한 천부 횡파속도 연구 (Shallow Shear-wave Velocities Using the Microtremor Survey Method)

  • 황윤구;김기영
    • 지질공학
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    • 제16권4호
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    • pp.381-392
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    • 2006
  • 상시미동을 이용하는 수동적 표면파 탐사를 결정질암 기반암 지역에서 실시하여, 내진설계 지반분류 기준인 30 m 깊이까지의 평균 횡파속도(Vs30)를 구하고자 연구를 수행하였다. 시험자료는 조사지 A와 B에서 삼각형 배열과 'L' 자형 직각 배열로 2 ms 간격으로 4초 동안 기록하였다. 조사지 A에서 기록한 자료를 공간 자기상관 방법으로 분석하여 위상속도 스펙트럼을 작성하고, 수신기 배열의 길이 및 형태, 기록 횟수, 수신기 수 등의 주요인자들의 영향을 고찰하였다. 조사지 B에서 상시미동 기록자료의 역산을 통해서 구한 횡파속도와 근처 시추공에서 수직탄성파 방법으로 구한 결과가 대체로 일치함을 보여 상시미동을 이용한 표면파 탐사법이 Vs30을 구하는데 효율적인 방법으로 판단된다.