• Title/Summary/Keyword: fracture failure

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Structural Behavior Evaluation of NRC Beam-Column Connections (NRC 보-기둥 접합부의 구조적 거동 평가)

  • Jeon, Ji-Hwan;Lee, Sang-Yun;Kim, Seung-Hun
    • Journal of the Korea institute for structural maintenance and inspection
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    • v.26 no.1
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    • pp.73-80
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    • 2022
  • In this study, details of NRC beam-column connections were developed in which beam and columns pre-assembled in factories using steel angles were bolted on site. The developed joint details are NRC-J type and NRC-JD type. NRC-J type is a method of tensile joining with TS bolts to the side and lower surfaces of the side plate of the NRC column and the end plate of the NRC beam. NRC-JD type has a rigid joint with high-strength bolts between the NRC beam and the side of the NRC column for shear, and with lap splices of reinforcing bar penetrating the joint and the beam main reinforcement for bending. For the seismic performance evaluation of the joint, three specimens were tested: an NRC-J specimen and NRC-JD specimen with NRC beam-column joint details, and an RC-J specimen with RC beam-column joint detail. As a result of the repeated lateral load test, the final failure mode of all specimens was the bending fracture of the beam at the beam-column interface. Compared to the RC-J specimen, the maximum strength of the specimen by the positive force was 10.1% and 29.6% higher in the NRC-J specimen and the NRC-JD specimen, respectively. Both NRC joint details were evaluated to secure ductility of 0.03 rad or more, the minimum total inter-story displacement angle required for the composite intermediate moment frame according to the KDS standard (KDS 41 31 00). At the slope by relative storey displacemet of 5.7%, the NRC-J specimen and the NRC-JD specimen had about 34.8% and 61.1% greater cumulative energy dissipation capacity than the RC specimen. The experimental strength of the NRC beam-column connection was evaluated to be 30% to 53% greater than the theoretical strength according to the KDS standard formula, and the standard formula evaluated the joint performance as a safety side.

Limb Salvage Using a Combined Distal Femur and Proximal Tibia Replacement in the Sequelae of an Infected Reconstruction on Either Side of the Knee Joint (슬관절 주위 재건물 감염 후유증 시 슬관절 상하부 종양인공관절을 이용한 사지 구제술)

  • Jeon, Dae-Geun;Cho, Wan Hyeong;Park, Hwanseong;Nam, Heeseung
    • Journal of the Korean Orthopaedic Association
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    • v.54 no.1
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    • pp.37-44
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    • 2019
  • Purpose: Tumor infiltration around the knee joint or skip metastasis, repeated infection sequelae after tumor prosthesis implantation, regional recurrence, and mechanical failure of the megaprosthesis might require combined distal femur and proximal tibia replacement (CFTR). Among the aforementioned situations, there are few reports on the indication, complications, and implant survival of CFTR in temporarily arthrodesed patients who had a massive bony defect on either side of the knee joint to control infection. Materials and Methods: Thirty-four CFTR patients were reviewed retrospectively and 13 temporary arthrodesed cases switched to CFTR were extracted. All 13 cases had undergone a massive bony resection on either side of the knee joint and temporary arthrodesis state to control the repeated infection. This paper describes the diagnosis, tumor location, number of operations until CFTR, duration from the index operation to CFTR, survival of CFTR, complications, and Musculoskeletal Tumor Society (MSTS) score. Results: According to Kaplan-Meier plot, the 5- and 10-year survival of CFTR was 69.0%±12.8%, 46.0%±20.7%, respectively. Six (46.2%) of the 13 cases had major complications. Three cases underwent removal of the prosthesis and were converted to arthrodesis due to infection. Two cases underwent partial change of the implant due to loosening and periprosthetic fracture. The remaining case with a deep infection was resolved after extensive debridement. At the final follow-up, the average MSTS score of 10 cases with CFTR was 24.6 (21-27). In contrast, the MSTS score of 3 arthrodesis cases with failed CFTR was 12.3 (12-13). The average range of motion of the 10 CFTR cases was 67° (0°-100°). The mean extension lag of 10 cases was 48° (20°-80°). Conclusion: Although the complication rates is substantial, conversion of an arthrodesed knee to a mobile joint using CFTR in a patient who had a massive bony defect on either side of the knee joint to control infection should be considered. The patient's functional outcome was different from the arthrodesed one. For successful conversion to a mobile joint, thorough the eradication of scar tissue and creating sufficient space for the tumor prosthesis to flex the knee joint up to 60° to 70° without soft tissue tension.

The micro-tensile bond strength of two-step self-etch adhesive to ground enamel with and without prior acid-etching (산부식 전처리에 따른 2단계 자가부식 접착제의 연마 법랑질에 대한 미세인장결합강도)

  • Kim, You-Lee;Kim, Jee-Hwan;Shim, June-Sung;Kim, Kwang-Mahn;Lee, Keun-Woo
    • The Journal of Korean Academy of Prosthodontics
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    • v.46 no.2
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    • pp.148-156
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    • 2008
  • Statement of problems: Self-etch adhesives exhibit some clinical benefits such as ease of manipulation and reduced technique-sensitivity. Nevertheless, some concern remains regarding the bonding effectiveness of self-etch adhesives to enamel, in particular when so-called 'mild' self-etch adhesives are employed. This study compared the microtensile bond strengths to ground enamel of the two-step self-etch adhesive Clearfil SE Bond (Kuraray) to the three-step etch-and- rinse adhesive Scotchbond Multi-Purpose (3M ESPE) and the one-step self-etch adhesive iBond (Heraeus Kulzer). Purpose: The purpose of this study was to determine the effect of a preceding phosphoric acid conditioning step on the bonding effectiveness of a two-step self-etch adhesive to ground enamel. Material and methods: The two-step self-etch adhesive Clearfil SE Bond non-etch group, Clearfil SE Bond etch group with prior 35% phosphoric acid etching, and the one-step self-etch adhesive iBond group were used as experimental groups. The three-step etch-and-rinse adhesive Scotchbond Multi-Purpose was used as a control group. The facial surfaces of bovine incisors were divided in four equal parts cruciformly, and randomly distributed into each group. The facial surface of each incisor was ground with 800-grit silicon carbide paper. Each adhesive group was applied according to the manufacturer's instructions to ground enamel, after which the surface was built up using Light-Core (Bisco). After storage in distilled water at $37^{\circ}C$ for 1 week, the restored teeth were sectioned into enamel beams approximately 0.8*0.8mm in cross section using a low speed precision diamond saw (TOPMET Metsaw-LS). After storage in distilled water at $37^{\circ}C$ for 1 month, 3 months, microtensile bond strength evaluations were performed using microspecimens. The microtensile bond strength (MPa) was derived by dividing the imposed force (N) at time of fracture by the bond area ($mm^2$). The mode of failure at the interface was determined with a microscope (Microscope-B nocular, Nikon). The data of microtensile bond strength were statistically analyzed using a one-way ANOVA, followed by Least Significant Difference Post Hoc Test at a significance level of 5%. Results: The mean microtensile bond strength after 1 month of storage showed no statistically significant difference between all adhesive groups (P>0.05). After 3 months of storage, adhesion to ground enamel of iBond was not significantly different from Clearfil SE Bond etch (P>>0.05), while Clearfil SE Bond non-etch and Scotchbond Multi-Purpose demonstrated significantly lower bond strengths (P<0.05), with no significant differences between the two adhesives. Conclusion: In this study the microtensile bond strength to ground enamel of two-step self-etch adhesive Clearfil SE Bond was not significantly different from three-step etch-and-rinse adhesive Scotchbond Multi-Purpose, and prior etching with 35% phosphoric acid significantly increased the bonding effectiveness of Clearfil SE Bond to enamel at 3 months.