• Title/Summary/Keyword: dryer

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Development of a Rice Circulating Concurrent-flow Dryer (I) - Performance Test of Pilot Scale Dryer - (순환식 병류형 곡물건조기 개발 (I) -시작기의 성능시험 -)

  • Han J.W.;Keum D.H.;Han J.G.;Kim H.;Hong S.J.
    • Journal of Biosystems Engineering
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    • v.31 no.4 s.117
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    • pp.349-354
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    • 2006
  • This study was performed to evaluate the performances for a concurrent flow rice dryer of pilot scale with devices for circulating rice. The pilot scale dryer with the capacity of 700 kg was developed to obtain design informations for the development of actual scale dryer of holding capacity of 10 tons. Three drying tests were conducted at two temperature levels of $100^{\circ}C\;and\;120^{\circ}C$, and two air flow rates levels of $28.5cmm/m^2\;and\;57.1cmm/m^2$. Drying conditions for Test-1, Test-2 and Test-3 were $100^{\circ}C\;-28.5cmm/m^2,\;120^{\circ}C-28.5cmm/m^2\;and\;120^{\circ}-57.1cmm/m^2}$ respectively. Drying rates were 0.73%(w.b./h) for Test-1, 0.90%(w.b./h) for Test-2 and 1.46%(w.b./h) for Test-3. The crack ratios of brown rice after drying ranged from 2.4% to 8.4%, and increased with the increase of drying rate and airflow rate. The energy consumptions were from 6,225 kJ/kg to 6,993 kJ/kg which was higher than that of conventional cross-flow rice circulating type dryer used in Korea. This results were due to the lower ambient air temperatures of $4.5^{\circ}C\;to\;13.4^{\circ}C$ during drying tests.

Modification of Conventional Freeze Dryer (진공동결 건조기의 개발에 관한 연구)

  • Park, Noh-Hyun;Kim, Byeong-Sam;Kang, Tong-Sam;Shin, Dong-Hwa
    • Korean Journal of Food Science and Technology
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    • v.20 no.3
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    • pp.350-356
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    • 1988
  • A pilot plant scale freeze dryer was designed and manufactured and its performance was tested. Freezing capacity of water vapor in the developed freeze dryer was 8㎏/batch and heating and defrosting methods were conduction and hot gas types, respectively. And exhausting time of vacuum pump was 7-8 minutes and temperature of cold trap was kept below $-50^{\circ}C$. In the freeze drying of fruits and vegetables, its optimum and maximum drying capacities were 2 and 4㎏/batch, respectively. Performance of the new freeze dryer was compared quite well with a foreign made freeze dryer.

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Efficient Drying Conditions for a Condensing Clothes Dryer (응축식 의류건조기의 효율적인 건조 조건)

  • Chung, Hae-Won;Kim, Hyo-Jeong;Hwang, So-Yeon
    • Fashion & Textile Research Journal
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    • v.10 no.6
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    • pp.1058-1063
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    • 2008
  • The use of clothes dryers is increasing in Korea and throughout Asia, because of preference for the drum type washer dryer. Clothes dryers consume more energy than almost any other home appliance. This paper suggests efficient ways for drying laundry with condensing clothes drier. We dried cotton fabrics with the condensing clothes dryers and observed the energy input, temperature and RH of the dryer during the drying process. In the early stages of drying process, the air temperature inside the clothes dryer decreased and the RH and the drying time increased as the weight of fabrics increased. We found that it was important to consider the total weight of the fabrics that included heat-sensitive fibers. It took more than half the drying time and the energy input for a 2.5 kg load that it did for a 5 kg load. Therefore, drying larger one load was more efficient than divided smaller loads, because increasing the weight of the fabrics reduced the energy input per kg of drying clothes. The lower the initial moisture regains of the fabrics were, the lower the energy input and the drying time were. The energy input for spinning after washing was much less than that for drying in the dryer. Consequently, it is more efficient to reduce the moisture content of the clothes by lengthening the spinning time of the washer to reduce the energy consumption and the drying time. During the drying process opening the door twice for 30 seconds each time lowered the air temperature and the RH of the dryer, but did not affect the moisture regain of the fabrics, the drying time, and the energy input.

Reuse of Exhaust Heat and Improvement in Fuel Efficiency of Grain Dryer (곡물(穀物) 건조기(乾燥機)의 배기열(排気熱) 재이용(再利用) 및 열효율(熱効率) 개선(改善)에 관(關)한 연구(硏究))

  • Keum, Dong Hyuk;Lee, Yong Kook;Lee, Kyou Seung;Han, Jong Ho
    • Journal of Biosystems Engineering
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    • v.9 no.2
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    • pp.65-73
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    • 1984
  • While most of researches on the performance of high temperature grain dryer have dealt mainly with improving dryer capacity and drying speed during the last twenty years, energy efficiency, in fact, has not been emphasized. Current fuel supplies and energy cost have shifted the emphasis to reducing the energy consumption for grain drying while maintaining dryer capacity and grain quality. Since the energy input for drying is relatively large, the recovery and reuse of at least part of the exhaust energy can significantly reduce the total energy consumption in existing drying systems. Unilization of exhaust heat in grain dryer either through direct recycling or by a thermal coupling in heat exchanger have been subject of a number of investigators. However, very seldom research in Korea has been done in this area. Three drying tests(non-recycling, 0.22 recycle ratio, and 0.76 recycle ratio)were performed to investigate the thermal efficiency and heat loss factors of continuous flow type dryer, and to analyze the effect of recycle ratio (weight of exhaust air recycled/total weight of input air) on the energy requriements for rough rice drying. The test results showed that when the exhaust air was not recycled, the energy lost from furnace was 15.3 percent of input fuel energy, and latent and sensible heat of exhaust air were 61.4 percent and 11.2 percent respectively. The heat which was required in raising grain temperature and stored in dryer was relatively small. As the recycle ratio of exhaust air was increased, the drying rate was suddenly decreased, and thermal efficiency of the kerosene burner was also decreased. Drying test with 0.76 recycle ratio resulted in 12.4% increase in fuel consumption, and 38.4% increase in electric power consumption as compared to the non-recycled drying test. Drying test of 0.22 recycle ratio resulted in 6.8% saving in total energy consumption, 8.0% reduction in fuel consumption, and 2.5% increase in electric power consumption as compared to the non-recycled drying test.

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A Study on Performance Improvement of a Heat Pump Dryer with an Extra Evaporator Outside (보조 외부 증발기를 이용한 히트펌프 건조기 성능 향상에 관한 연구)

  • Lee, Young-Lim;Park, Sang-Jun;Hwang, Il-Sun
    • Korean Journal of Air-Conditioning and Refrigeration Engineering
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    • v.24 no.10
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    • pp.711-717
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    • 2012
  • A heat pump dryer for the frozen food needs to preheat the air to a certain temperature where condensation can efficiently occur. In this study, an analysis of a heat pump dryer performance with operating conditions, an analysis of supplying heat with internal and external evaporators and a warm-up experiment with the evaporators have been performed. The results showed that the external evaporator can significantly accelerate the warm-up time of the dryer, so that it can reduce power consumption greatly. The use of the external evaporator is more efficient for higher ambient temperature. In addition, it was found that COP decreases and the range of evaporating pressure for the evaporator becomes narrower as the condensing temperature of the condenser increases.

Numerical Analysis of the Inner Flow of a 3-pass Rotary Dryer (3단 회전식 건조기의 내부 유동에 관한 수치해석)

  • Kim, T.S.;Kim, Y.K.;Choi, Y.H.;Choi, K.;Lee, Y.W.
    • Journal of Power System Engineering
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    • v.9 no.4
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    • pp.51-57
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    • 2005
  • In order to prevent the environmental pollution, the dryers are commonly used to treat sludge that one of sewages is polluting the quality of water. Generally, the drying method is various as to the property of material and use. Rotary dryer is a good apparatus to treat them. The rotary dryer is the way that is to make substance transmission and heating using hot air between sludge particles and heated gas. In this paper, we performed a numerical analysis of the inner air flow of the 3-pass rotary dryer through the changing rotational speed from 3rpm to 10rpm. In this result, we found that 3rpm is effective to dry material in terms of heat transfer because large scale velocity fluctuation is occurred inside the first and second drum. Also we confirmed that 5rpm and 8rpm showed up uniform flow at the center area of the first drum.

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Progress in hybrid greenhouse solar dryer (HGSD): A review

  • Singh, Pushpendra;Gaur, Manoj K.;Kushwah, Anand;Tiwari, G.N.
    • Advances in Energy Research
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    • v.6 no.2
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    • pp.145-160
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    • 2019
  • The world population reaches to about 7.7 billion in 2018 from 6.2 billion in 2000. This much growth in population results in increased energy demand and increased food supply. As the conventional energy sources are limited. These may deplete soon if consumed at this rate. So, the world is switching towards the utilization of non-conventional sources of energy. Energy from sun is the best method as it can not only solve the energy issue but also helps in meeting food demand by conserving it. Greenhouses are made for the purpose of food conservation. Various types of solar dryers are developed by researchers till now and still the effort is being putted to make them more efficient. Hybrid greenhouse is also effort toward utilization of solar energy in more efficient way. The paper presents the heat and mass transfer analysis of hybrid greenhouse solar dryer developed by different researchers till now. The review helps the researcher in understanding the heat and mass transfer taking place inside the hybrid greenhouse and how it can be further improved.

Studies on the Drying Methods of Sea Foods 1 . Fixed Bed Drying of Squid (수산식품의 건조방법에 관한 연구 1 . 오정어의 고정층건조)

  • HUR Jong-Wha
    • Korean Journal of Fisheries and Aquatic Sciences
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    • v.15 no.1
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    • pp.107-110
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    • 1982
  • Fixed bed drying method was selected to reduce the initial drying time of squid and the effects of drying air temperature and bed height on the drying rate were investigated, with following results. 1. The drying rate in the fixed bed dryer was faster than that of natural convection type dryer heated indirectly and that of hot air dryer heated directly. 2, Shirai-equation was applicable to squid being dried. Using the equation, drying rate constant obtained was as shown in table 1.

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Thermal Analysis of Solar Utilization Dryer for Redpepper Drying (고추건조를 통한 태양열 건조기의 열성분석)

  • Lee, Tai-Kyu;Cho, Suh-Hyun;Jo, Duk-Ki;Chea, Young-Hi;Auh, Paul J.
    • Solar Energy
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    • v.9 no.2
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    • pp.14-21
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    • 1989
  • The heat transfer analysis is performed on unloaded solar utilization dryer, and thermal performance for a prototype model while drying red-pepper is also investigated. Results of theoretically derived thermal equations are in good agreement with experimental data. This constructed feature of the prototype demonstrates the excellent technical drying performance. Finally, this paper recommends the further work to develop advanced and economic solar utilization multi-purpose dryer.

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An Evaluation of Welded Drying Equipment (건조장치 제작 및 사용성능 평가)

  • Choi Gwang
    • Proceedings of the KWS Conference
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    • 2006.05a
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    • pp.146-147
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    • 2006
  • In order to prevent the environmental pollution, the dryers are commonly used to treat sludge that one of sewages is polluting the quality of water. Rotary dryer is a good apparatus to treat them. The rotary dryer is the way that is to make substance transmission and heat using hot air between sludge particle and heated gas. In this paper, a numerical analysis was performed for the structural analysis of the 3-pass rotary dryer through the finite elemeny method and an experiment was done for the structural stability. And reasonable relation was found between analysis and experiment.

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