• Title/Summary/Keyword: coiled tubing

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Mechanical behavior of coiled tubing over wellhead and analysis of its effect on downhole buckling

  • Zhao, Le;Gao, Mingzhong;Li, Cunbao;Xian, Linyun
    • Steel and Composite Structures
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    • v.44 no.2
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    • pp.199-210
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    • 2022
  • This study build finite element analysis (FEA) models describing the bending events of coiled tubing (CT) at the wellhead and trips into the hole, accurately provide the state of stress and strain while the CT is in service. The bending moment and axial force history curves are used as loads and boundary conditions in the diametrical growth models to ensure consistency with the actual working conditions in field operations. The simulation diametrical growth results in this study are more accurate and reasonable. Analysis the factors influencing fatigue and diametrical growth shows that the internal pressure has a first-order influence on fatigue, followed by the radius of the guide arch, reel and the CT diameter. As the number of trip cycles increase, fatigue damage, residual stress and strain cumulatively increase, until CT failure occurs. Significant residual stresses remain in the CT cross-section, and the CT exhibits a residual curvature, the initial residual bending configuration of CT under wellbore constraints, after running into the hole, is sinusoidal. The residual stresses and residual bending configuration significantly decrease the buckling load, making the buckling and buckling release of CT in the downhole an elastic-plastic process, exacerbating the helical lockup. The conclusions drawn in this study will improve CT models and contribute to the operational and economic success of CT services.

Fluidelastic instability of a curved tube array in single phase cross flow

  • Kang-Hee Lee;Heung-Seok Kang;Du-Ho Hong;Jong-In Kim
    • Nuclear Engineering and Technology
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    • v.55 no.3
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    • pp.1118-1124
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    • 2023
  • Experimental study on the fluidelastic instability (FEI) of a curved tube bundle in single phase downward cross flow is investigated for the design qualification and analysis input preparation of helical coiled steam generator tubing. A 6×9 normal square curved tube array with equal and different vertical/horizontal pitch-to-diameter ratio was under-tested up to 6 m/s in term of gap flow velocity to measure the critical velocity for FEI. The critical velocity for FEI was measured at the turning point from the vibration amplitude plot along the gap flow velocity. Our test results were compared with straight tube results and published data in the design guideline. The applicability of the current design guidelines to a curved tube bundle is also assessed. We found that introducing frequency difference in a curved tube array increases the critical velocity for fluidelastic instability.

Development of Novel Joint Device for a Disposal Canister in Deep Borehole Disposal (고준위폐기물 심부시추공 처분을 위한 처분용기 접속장치의 개발)

  • LEE, Minsoo;LEE, Jongyoul;JI, Sung-Hoon
    • Journal of Nuclear Fuel Cycle and Waste Technology(JNFCWT)
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    • v.16 no.2
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    • pp.261-270
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    • 2018
  • In this study, to replace the 'J-slot joint', a joint device between a disposal canister and an emplacement jig in Deep Borehole Disposal process, a novel joint device was designed and tested. The novel joint device was composed of a wedge on top of a disposal canister and a hook box at the end of a winch system. The designed joint device had merits in that it can recombine an emplaced canister freely without the replacement of the joint component. Moreover, it can be applied to various emplacement jigs such as drill pipes, wire-lines, and coiled tubing. To demonstrate the designed joint device, the joint device (${\Phi}110mm$, H 148 mm), a twin canister string (${\Phi}140mm$, H 1,105 mm), and a water tube (${\Phi}150mm$, H 1,500 mm) as a borehole model were manufactured at 1/3 scale. As deployment muds, Na-type bentonite (MX-80) and Ca-type (GJ II) bentonite muds were prepared at solid contents of 7wt% and 28wt%, respectively. The manufactured joint device showed good performance in pure water and viscous muds, with an operation speed of $10m{\cdot}min^{-1}$. It was concluded that the newly developed joint device can be used for the emplacement and retrieval of a deep disposal canister, below 3~5 km, in the future.