• Title/Summary/Keyword: Wolsong Unit 2

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Assessment on Aging Management of Delayed Neutron Monitoring System Tubing for Continued Operation of Wolsong Unit 1 (월성1호기 계속운전 관련 결함연료위치탐지계통 배관의 열화관리평가)

  • Song, Myung Ho;Kim, Hong Key;Lee, Young Ho
    • Transactions of the Korean Society of Pressure Vessels and Piping
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    • v.7 no.2
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    • pp.14-20
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    • 2011
  • The end of design lifetime for Wolsong unit 1 will be reached on 20th November in 2012. So the license renewal documents for the continuous operation of Wolsong unit 1 is under reviewing now. Major components of primary system such as pressure tubes, feeder pipes including delayed neutron monitoring system tubing are being replaced and many components of secondary system are also being repaired. In this paper, the assessment on the wear degradation of delayed neutron monitoring system tubing(on the other hand, DN tube was called) was performed for the ageing management of the same component. The wear defects of this component was one of causes that resulted in heavy water leakage accidents. Therefore design specifications of Wolsong uint 1 and heavy water leakage accidents of pressurized heavy water reactors were reviewed and causes of wear defect for DN tubes were analyzed. Wear propagation equations based on the heavy water leakage history were made and the proper repairing time was possible to be expected if the continued operation was considered. Finally design change items of DN tubes that were conducted for the long term operation of Wolsong unit 1 are introduced.

Wolsong Unit 1 Steam Generator Aging Management for Continued Operation (월성 1호기 계속운전을 위한 증기발생기 열화관리)

  • Song, Myung Ho;Kim, Hong Key;Lee, Jung Min
    • Transactions of the Korean Society of Pressure Vessels and Piping
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    • v.6 no.2
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    • pp.28-33
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    • 2010
  • As a part of license renewal for the continued operation of Wolsong unit 1, the periodic safety review report was submitted near the end of design lifetime, 2012, and now is under reviewing. Major components of primary system such as pressure tubes, feeder pipes and so on are being replaced and many components of secondary system are also being repaired. So the license renewal of Wolsong unit 1 is expected to be acquired without significant issues. But on the other hand, steam generators of Wolsong unit 1 had the good performance and therefore the replacement and repair for the steam generator are not needed. Recently it is reported that some cracks were detected in a few of european steam generator with Alloy 800 tubes and the cause of cracks was the outer diameter stress corrosion cracking(ODSCC) due to the concentration of chemical impurities on the outer surface of tube. Accordingly the overall review on this issue was performed. The long-term operation is likely to results to form the concentration mechanism for the tube corrosion as the sludge build-up in the secondary side of steam generator and the crack in the crevice between tube and tube-sheet and expansion transitions is apt to be occurred. In this paper, the history of steam generator inspection and operation of Wolsong unit 1 are reviewed and the reliability of steam generator tube is evaluated and the steam generator aging management program for Wolsong unit 1 is introduced.

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Prediction of Tritium Release from Wolsong Unit during the WTRF Operation (월성원전 TRF 가동에 따른 삼중수소 방출량 예측)

  • 송규민;이성진;이숙경;손순환;엄희문
    • Proceedings of the Korean Radioactive Waste Society Conference
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    • 2003.11a
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    • pp.484-490
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    • 2003
  • The amount of the tritium released from Wolsong units during the WTRF operation is predicted. The profiles of tritium concentration in moderators and PHTs as variation of WTRF service allotment for each Wolsong unit are calculated, and the tritium releases are obtained from these tritium concentration profiles. The tritium concentration in moderator will be decreased down under 10 Ci/kg in 2013 and the yearly tritium release will be reduced below 25% of WTRF start year.

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Periodic Safety Review of Wolsong Unit 1 - Environmental Impact as gaseous and liquid effluents (월성 1호기 주기적안전성평가 - 기체 및 액체 방사성폐기물에 의한 환경영향)

  • 김성민;이은미;김미자;이갑복;정양근;엄희문
    • Proceedings of the Korean Radioactive Waste Society Conference
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    • 2003.11a
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    • pp.455-462
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    • 2003
  • According to Korean nuclear code requires Periodic Safety Review(PSR) every 10 years should be perform for operating reactor, and selects the eleven PSR safety factors. Among them the review objective of the environmental impact is to determine whether the operator has an adequate programme for surveillance of the environmental impact of the nuclear power plant based on current safety standards. In this paper, the environmental impact in PSR of Wolsong Unit 1 was reflected current safety standards as of the evaluation date. As a result, all items generally satisfied the standards, and the staff also verified that the population dose due to the operation of Wolsong Unit 1 was controlled safely as of the evaluation date.

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Hydrogen Absorption Behavior of Zr-2.5Nb Pressure Tubes in Wolsong Unit 1

  • Choo, Kee-Nam;Kwon, Sang-Chul;Kim, Young-Suk
    • Nuclear Engineering and Technology
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    • v.30 no.4
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    • pp.318-327
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    • 1998
  • The deuterium uptake behavior of Zr-2.5Nb pressure tubes in Wolsong Unit 1 was analyzed in terms of longitudinal location, operation time, and coolant temperature. The results were compared with those obtained from Canadian CANDU reactors. The amount of deuterium uptake was higher at the outlet part than at the inlet part and was also higher when subjected to a longer operation time and a higher coolant temperature. The hydrogen uptake of Zr-2.5Nb in a hydrogen gas atmosphere was dependent on the microstructure of the alloy. The aged Zr-2.5Nb consisting of $\alpha$-Zr and $\beta$-Nb phases showed higher hydrogen uptake than that consisting of $\alpha$-Zr and $\beta$-Zr phases. The hydrogen in the alloy decreased the rate of oxidation. This could be explained in terms of the cathodic controlled reaction of Zr-2.5Nb oxidation.

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Design on SDS2 On-line Poison Concentration Monitoring in CANDU

  • Kim, Seog-Nam;Jung, Ho-Chang;Kim, Sung;Kim, Ji-Hyeon;Han, Sang-Joon
    • Nuclear Engineering and Technology
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    • v.28 no.5
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    • pp.500-505
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    • 1996
  • At the reference plant(Wolsong unit No. 1) a manual poison sampling system is provided to periodically sample gadolinium from each tank and analyze it in the laboratory to provide assurance that adequate poison concentration in each tank is maintained. The AECB required a continuous, on-line monitoring system. On Wolsong unit No. 2, process piping adapter and new instrument loops added to the Liquid Injection Shutdown System(LISS) which is part of SDS2. The new instrument loops continuously monitor SDS2 poison conductivity and initiate an alarm when the poison concentration is too low.

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Design of Improved Detection Instrumentation for the Annulus Gas System for Wolsong 2

  • Kim, Seog-Nam;Koo, Jun-Mo;Chang, Ik-Ho;Jung, Ho-Chang;Han, Sang-Joon
    • Nuclear Engineering and Technology
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    • v.28 no.4
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    • pp.423-430
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    • 1996
  • The improved and advanced Annulus Gas System(AGS) has been developed for Wolsong 2 to satisfy the requirements of the regulatory body. The Atomic Energy Control Board(AECB) required a shorter detection time following a small leak from a pressure tube and/or calandria tube. This paper describes licensing requirements, functional requirements and detail design description for the AGS. The Wolsong unit No. 1 AGS was designed to operate as a stagnant system normally requiring only pressure regulation and having provisions for purging. no improved AGS involves the adoption of gas recirculation in AGS, duplication of dew point indicators with additional instrumentation and sampling provisions to prompt operator action. The improved system operates in the recirculation mode with continuous dew point measurement for leak detection. An AGS with improved detection instrumentation is provided.

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Microstructure and Mechanical Property of Irradiated Zr-2.5Nb Pressure Tube in Wolsong Unit-1

  • 김영숙;안상복;오동준;김성수;정용무
    • Transactions of Materials Processing
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    • v.8 no.3
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    • pp.241-241
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    • 1999
  • With the aim of assessing the degradation of Zr-2.5Nb pressure tubes operating in the Wolsong unit-1 nuclear power plant, characterization tests are being conducted on irradiated Zr-2.5Nb tubes removed after 10-year operation. The examined tube had been exposed to temperatures ranging from 264 to 306℃ and a neutron fluence of 8.9×$10^{21}$ n/cm²(E>1 MeV) at the maximum. Tensile tests were carried out at temperatures ranging from RT to 300℃. The density of a-type and c-type dislocations was examined on the irradiated Zr-2.5Nb tube using a transmission electron microscope. Neutron irradiation up to 8.9×$10^{21}$ n/cm²(E>1 MeV) yielded an increase in a-type dislocation density of the Zr-2.5Nb pressure tube to 7.5×$10^{14} m^{-2}$, which was highest at the inlet of the tube exposed to the low temperature of 275℃. In contrast, the c-component dislocation density did not change with irradiation, keeping an initial dislocation density of 0.8×$10^{14} m^{-2}$ over the whole length of the tube. As expected, the neutron irradiation increased mechanical strength by about 17-26% in the transverse direction and by 34-39% in the longitudinal direction compared to that of the unirradiated tube at 300℃. The change in the mechanical properties with irradiation is discussed in association with the microstructural change as a function of temperature and neutron fluence.