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충남 태안 철마산 일대의 지질 및 희토류 광화작용 (REE Mineralization and Geology of Chulmasan Area, Taean, Chungchungnamdo)

  • 유봉철
    • 한국광물학회지
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    • 제32권2호
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    • pp.127-143
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    • 2019
  • 철마산 일대의 지질은 하부로부터 선캠브리아기의 소근리층, 화강암질편마암, 엽리상 흑운모화강암, 엽리상 운모화강암, 염기성암맥 및 산성암맥으로 구성된다. 이 일대의 희토류 광화작용은 화강암질편마암과 엽리상 운모화강암에서 관찰된다. 이들 암석에서 소량 희토류 원소 및 토륨을 함유한 광물들은 저어콘($Y_2O_3$ 0.00~1.18 wt.%, $Gd_2O_3$ 0.00~0.59 wt.%, $Er_2O_3$ 0.00~0.22 wt.%, $Yb_2O_3$ 0.00~0.34 wt.%, $Lu_2O_3$ 0.00~0.48 wt.%, $ThO_2$ 0.00~0.33 wt.%), 토리아나이트($Nd_2O_3$ 0.00~0.24 wt.%, $Lu_2O_3$ 0.00~0.26 wt.%), 베르시에린($La_2O_3$ 0.04~0.26 wt.%, $Nd_2O_3$ 0.00~0.20 wt.%, $Tb_2O_3$ 0.04~0.12 wt.%, $Dy_2O_3$ 0.17~0.26 wt.%, $Er_2O_3$ 0.33~0.44 wt.%, $Lu_2O_3$ 0.00~0.19 wt.%, $ThO_2$ 0.61~0.93 wt.%), 녹니석($La_2O_3$ 0.44~0.68 wt.%, $Ce_2O_3$ 0.12~0.13 wt.%, $Nd_2O_3$ 0.31~0.44 wt.%, $Eu_2O_3$ 0.03~0.08 wt.%, $Dy_2O_3$ 0.09~0.21 wt.%, $Ho_2O_3$ 0.04~0.14 wt.%, $Er_2O_3$ 0.18~0.32 wt.%, $Lu_2O_3$ 0.07~0.21 wt.%, $ThO_2$ 0.00~0.97 wt.%), 흑운모($Nd_2O_3$ 0.02~0.08 wt.%, $Gd_2O_3$ 0.07~0.08 wt.%, $Tb_2O_3$ 0.02~0.07 wt.%, $Dy_2O_3$ 0.35~0.43 wt.%, $Ho_2O_3$ 0.15~0.26 wt.%, $Er_2O_3$ 0.24~0.28 wt.%, $Yb_2O_3$ 0.06~0.18 wt.%, $ThO_2$ 0.00~0.12 wt.%), 정장석($Dy_2O_3$ 0.05~0.12 wt.%, $Ho_2O_3$ 0.05~0.06 wt.%, $Er_2O_3$ 0.28 wt.%, $Yb_2O_3$ 0.06~0.12 wt.%) 및 사장석($Ho_2O_3$ 0.01~0.03 wt.%, $Er_2O_3$ 0.10~0.27 wt.%, $ThO_2$ 0.11~0.13 wt.%)이며 희토류 광물로는 바스트나사이트와 퍼구소나이트이다. 희토류 광물들은 주로 장석류, 운모류, 저어콘, 인회석 및 티탄철석의 간극을 따라 산출된다. 따라서 철마산 일대의 희토류 광화작용 산물인 바스트나사이트와 퍼구소나이트는 화강암질편마암과 엽리상 운모화강암의 형성 시 희토류 원소 및 토륨이 구성광물 내에 소량 함유되어 있었으며 그후 계속된 화성활동 및 변성작용에 의하여 기존 광물 내에 함유되어 있던 희토류 원소가 재 농집에 의해 형성된 것으로 생각된다.

고압 금형 주조용 Al-4%Mg-0.9%Si 합금의 주조특성에 미치는 Fe, Mn 함량의 영향 (Effect of Fe, Mn Content on the Castability of Al-4%Mg-0.9%Si Alloys for High Pressure Die Casting)

  • 김헌주
    • 한국주조공학회지
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    • 제33권2호
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    • pp.55-62
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    • 2013
  • Effect of Fe and Mn contents on the castability of Al-4wt%Mg-0.9wt%Si system alloy has been studied. According to the analysis of cooling curve for Al-4wt%Mg-0.9wt%Si-0.3wt%Fe-0.3/0.5wt%Mn alloy, ${\alpha}-Al_{15}(Fe,Mn)_3Si_2$ and ${\beta}-Al_5FeSi$ phases crystallized above eutectic temperature of $Mg_2Si$. Therefore, these phases affected both the fluidity and shrinkage behaviors of the alloy during solidification. As Fe and Mn contents of Al-4wt%Mg-0.9wt%Si system alloy increased from 0.1 wt% to 0.4 wt% and from 0.3 wt% to 0.5 wt% respectively, the fluidity of the alloy decreased by 26% and 33%. When Fe content of the alloy increased from 0.1 wt% to 0.4 wt%, 23% decrease of macro shrinkage and 19% increase of micro shrinkage appeared. Similarly, Mn content of the alloy increased from 0.3 wt% to 0.5 wt%, 11% decrease of macro shrinkage and 14% increase of micro shrinkage appeared. Judging from the castability of the alloy, Al-4wt%Mg-0.9wt%Si alloy with low content of Fe and Mn, 0.1 wt% Fe and 0.3 wt% Mn, is recommendable.

고압 금형 주조용 Al-4 wt%Mg-0.9 wt%Si계 합금의 인장특성에 미치는 Fe, Mn함량의 영향 (Effect of Fe, Mn Content on the Tensile Property of Al-4 wt%Mg-0.9 wt%Si Alloy System for High Pressure Die Casting)

  • 김헌주
    • 한국주조공학회지
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    • 제33권3호
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    • pp.103-112
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    • 2013
  • Effect of Fe and Mn contents on the tensile properties of Al-4 wt%Mg-0.9 wt%Si alloy system has been studied. Common phases of Al-4 wt%Mg-0.9 wt%Si alloy system were ${\alpha}$-Al, $Mg_2Si$, ${\alpha}-Al_{12}(Fe,Mn)_3Si$ and ${\beta}-Al_5FeSi$. As Fe content of Al-4 wt%Mg-0.9 wt%Si alloy system increased from 0.15 wt% to above 0.3 wt%, ${\beta}-Al_5FeSi$ compound appeared. When Mn content of the alloy increased from 0.3 wt% to 0.5 wt%, morphology of plate shaped ${\beta}-Al_5FeSi$ compound changed to chinese script ${\alpha}-Al_{12}(Fe,Mn)_3Si$. As Fe content of Al-4 wt%Mg-0.9 wt%Si-0.3 wt%Mn alloy increased from 0.15 wt% to 0.4 wt%, tensile strength of the as-cast alloy decreased from 191 MPa to 183 MPa and, elongation of the alloy also decreased from 8.0% to 6.2%. Decrease of these properties can be explained as the formation of plate shape, ${\beta}-Al_5FeSi$ phase with low Mn/Fe ratio of the alloy. However, when Mn content of Al-4 wt%Mg-0.9 wt%Si-0.3 wt%Fe alloy increased from 0.3 wt% to 0.5 wt%, tensile strength of as-cast alloy increased from 181 MPa to 194 MPa and, elongation of the alloy increased from 6.8% to 7.0%. These improvements attribute to the morphology change from ${\beta}-Al_5FeSi$ phase to chinese script, ${\alpha}-Al_{15}(Fe,Mn)_3Si_2$ phase shape-modified from with high Mn/Fe ratio of the alloy.

U-10wt%Zr 합금의 미세조직에 미치는 합금원소 첨가의 영향에 관한 연구

  • 김기환;안현석;이종탁;김창규;강영호;백경욱
    • 한국원자력학회:학술대회논문집
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    • 한국원자력학회 1995년도 춘계학술발표회논문집(2)
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    • pp.745-752
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    • 1995
  • 고연소도 액체금속로용 금속연료를 개발하고자 U-l0wt%Zr 합금중 Zr 원소 대신에 X(:Si, Ta, Nb, W, Mo) 원소를 첨가한 U-7wt%Zr-3wt%X(:Si, Ta, Nb, W, Mo) 합금을 제조하여 미세조직에 미치는 합금원소 첨가의 영향을 조사하였다. 그 결과 U-7 wt%Zr-3wt%Si 합금을 제외한 모든 U-7wt%Zr-3wt%X(:Ta, Nb, W, Mo) 합금은 Matrix에 있어서 Laminar Structure를 그대로 유지하였다. U-7wt%Zr-3wt%Si 함금을 제외한 모든 U-7wt%Zr-3wt%X(:Ta, Nb, W, Mo) 합금의 주요한 상은 U-l0wt% Zr 합금과 마찬가지로 $\alpha$-U 및 $\delta$-UZr$_2$ 상이었다. U-7wt%Zr-3wt%X(:Ta, Nb, W, Mo) 합금은 U-l0wt%Zr 합금에 비해 Lamina Thickness가 크게 감소되었다. 특히 U-7wt%Zr-3wt%Mo 합금의 경우에 있어서는 U-l0wt%Zr 합금에 비해 1/3배 정도까지 Lamina Thickness가 크게 감소하였다. 이와 같은 합금원소 첨가에 의한 Laminar Structure의 미세화는 액체금속로강 금속연료내 Fission Gas의 Inter-connected Path가 보다 더 잘 형성됨으로 인해 Fission Gas Bubble에 대한 방출속도를 크게 증가시켜서 궁극적으로는 Fission Gas Bubble에 의한 Swelling을 저감시킬 것으로 기대된다.

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가스분사법으로 제조된 Mg-6 wt.% Al-1 wt.% Zn 합금의 시효특성 (The Aging Characteristics of Mg-6 wt.% Al-1 wt.% Zn Alloy Prepared by Gas Atomization)

  • 이두형;김보식;장시영
    • 한국분말재료학회지
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    • 제16권4호
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    • pp.275-279
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    • 2009
  • The aging characteristics of gas atomized Mg-6 wt.% Al-1 wt.% Zn alloy were investigated and compared to those of cast Mg-6 wt.% Al alloy. The gas atomized Mg-6 wt.% Al-1wt.% Zn alloy powders had spherical morphology between 1 and 100 $\mu m$ in diameter. After compaction under the pressure of 700 MPa at $320^{\circ}C$ for 10 min, the Mg-6 wt.% Al-1 wt.% Zn alloy showed a grain size of approximately 40 $\mu m$ which is smaller than that of the cast Mg-6 wt.% Al alloy, and a relative compact density of approximately 93%. After ageing, the Mg-6 wt.% Al-1 wt.% Zn alloy showed much faster peak hardness than cast Mg-6 wt.% Al alloy. The Mg-6 wt.% Al-1 wt.% Zn alloy showed the new fine precipitations with ageing time, while the cast Mg-6 wt.% Al alloy was almost similar morphology.

고신율 금형주조용 Al-9wt%Si-Mg계 합금의 주조특성에 미치는 Fe, Mn함량의 영향 (Effect of Fe, Mn Content on the Castability in Al-9wt%Si-Mg System Alloys for High Elongation)

  • 김헌주;정창열
    • 한국주조공학회지
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    • 제33권6호
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    • pp.233-241
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    • 2013
  • Effect of Fe and Mn contents on the castability of Al-9wt%Si-xMg-yFe-zMn alloy has been studied. The alloy was composed of ${\alpha}$-Al phase, Al+eutectic Si phase, ${\beta}$-Al5FeSi compound and chinese script ${\alpha}$-$Al_{15}(Mn,Fe)_3Si_2$ compound. ${\beta}$-$Al_5FeSi$ and ${\alpha}$-$Al_{15}(Mn,Fe)_3Si_2$ compounds assumed to effect the fluidity and shrinkage behaviors of the alloy during solidification due to the crystallization of ${\alpha}$-$Al_{15}(Fe,Mn)_3Si_2$ and ${\beta}$-$Al_5FeSi$ compounds above eutectic temperature. As Fe and Mn contents of Al-9wt%Si-0.3wt%Mg system alloy increased from 0.15wt% to 0.6wt% and from 0.3wt% to 0.7wt%, fluidity of the alloy decreased by 5.7% and 3.3%, respectively. And as Mg content of Al-9wt%Si-0.45wt%Fe-0.5wt%Mn system alloy increased from 0.3wt% to 0.4wt%, fluidity of the alloy decreased by 8.6%. When Fe content of the alloy increased from 0.15wt% to 0.6wt%, macro shrinkage ratio decreased from 6.1% to 4.1%, and micro shrinkage ratio increased from 0.04% to 0.24%. Similarly, Mn content of the alloy increased from 0.3wt% to 0.7wt%, macro shrinkage ratio decreased from 6.0% to 4.5% and micro shrinkage ratio increased from 0.12% to 0.18%. Judging from the castability of the alloy, Al-9wt%Si-0.3wt%Mg alloy with low content of Fe and Mn, 0.1wt% Fe and 0.3wt% Mn, is recommendable.

Improvement of Hydrogen Storage Properties of Mg by Addition of NbF5 via Mechanical Milling under H2

  • Kwak, Young Jun;Song, Jiyoung;Mumm, Daniel R.
    • 한국재료학회지
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    • 제23권10호
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    • pp.562-567
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    • 2013
  • A 90 wt% Mg-10 wt% $NbF_5$ sample was prepared by mechanical milling under $H_2$ (reactive mechanical grinding). Its hydriding and dehydriding properties were then examined. Activation of the 90 wt% Mg-10 wt% $NbF_5$ sample was not required. At n=1, the sample absorbed 3.11 wt% H for 2.5 min, 3.55 wt% H for 5 min, 3.86 wt% H for 10 min, and 4.23 wt% H for 30 min at 593K under 12 bar $H_2$. At n=1, the sample desorbed 0.17 wt% H for 5 min, 0.74 wt% H for 10 min, 2.03 wt% H for 30 min, and 2.81 wt% H for 60 min at 593K under 1.0 bar $H_2$. The XRD pattern of the 90 wt% Mg-10 wt% $NbF_5$ after reactive mechanical grinding showed Mg, ${\beta}-MgH_2$ and small amounts of ${\gamma}-MgH_2$, $NbH_2$, $MgF_2$ and $NbF_3$. The XRD pattern of the 90 wt% Mg-10 wt% $NbF_5$ dehydrided at n=3 revealed Mg, ${\beta}-MgH_2$, a small amount of MgO and very small amounts of $MgH_2$ and $NbH_2$. The 90 wt% Mg-10 wt% $NbF_5$ had a higher initial hydriding rate and a larger quantity of hydrogen absorbed for 60 min than the 90 wt% Mg-10 wt% MnO and the 90 wt% Mg-10 wt% $Fe_2O_3$, which were reported to have quite high hydriding rates and/or dehydriding rates. The 90 wt% Mg-10 wt% $NbF_5$ had a higher initial dehydriding rate (after an incubation period) and a larger quantity of hydrogen desorbed for 60 min than the 90 wt% Mg-10 wt% MnO and the 90 wt% Mg-10 wt% $Fe_2O_3$.

철강 하니콤구조의 접합강도 (Bond Strength of Steel honeycomb Structure)

  • 송건;홍영환
    • 열처리공학회지
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    • 제16권4호
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    • pp.197-204
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    • 2003
  • Honeycomb structure has been fabricated by brazing method using 0.1 wt%C and 1.0wt%C carbon steel core and STS304 stainless steel face sheet. Core shear strength ratio in W and L directions was 1:1.03 in 7 mm cell size, whereas 1:1.45 in 4 mm cell size. Flexural strength on face sheet was 166.4 MPa (0.1 wt%C, W direction), 171.1 MPa (0.1 wt%C, L direction), and 120.2 MPa (1.0 wt%C, W direction) in 7 mm cell size. And in 4mm cell size specimen, it was 169.2 MPa (0.1 wt%C, W direction), 224.2 MPa (0.1 wt%C, L direction). This means that flexural strength of 0.1 wt%C core material was higher than that of 1.0wt%C core material, which was contrary to expectation. SEM and EDS analysis represented that grain boundary diffusion had occurred in0.1 wt%C core, but no grain boundary diffusion in 1.0 wt%C core. And corrugated surface of 0.1 wt%C core was flat, whereas that of 1.0 wt%C core was not flat. As a result, contact area between two 1.0 wt%C cores was much less than that of 0.1 wt% cores, It is thought to be main reason for lower flexural strength of 1.0 wt%C core.