• Title/Summary/Keyword: Vortex Cavitation

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Visualization of Unstable Vortical Structure in a Propeller Wake Affected by Simulated Hull Wake (재현된 반류의 영향을 받는 프로펠러 후류 내 불안정한 날개끝 보오텍스 구조에 대한 정량적 가시화)

  • Kim, Kyung-Youl;Paik, Bu-Geun;Ahn, Jong-Woo
    • Journal of the Society of Naval Architects of Korea
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    • v.45 no.6
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    • pp.620-630
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    • 2008
  • The characteristics of complicated propeller wake influenced by hull wake are investigated by using a two-frame PIV (Particle Image Velocimetry) technique. As the propeller is significantly affected by the hull wake in a real marine vessel, the measurements of propeller wake under the hull wake would be certainly necessary for more reliable validation and the prediction of numerical simulation with wake modeling. Velocity field measurements have been conducted in a medium-size cavitation tunnel with a hull wake. Generally, the hull wake generated by the boundary layer of ship's hull produces the different loading distribution on the propeller blade in both upper and lower propeller planes. The difference of the propeller wake behaviors caused by the hull wake is discussed in terms of axial velocity, vorticity and turbulence kinetic energy distribution in the present study.

Thermal Spray Coating Layer for Improvement of Erosion and Corrosion Resistance Applicable to Large Sized High Speed Ship's Rudder (대형 고속 선박용 러더의 내침식, 부식 특성 향상을 위한 용사 코팅막)

  • Lee, Yu-Song;Heo, Seong-Hyeon;Kim, Jin-Hong;Kim, Yeo-Jung;Bae, Il-Yong;Lee, Myeong-Hun
    • Proceedings of the Korean Institute of Surface Engineering Conference
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    • 2011.05a
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    • pp.196-197
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    • 2011
  • Rudder, one of the most important component in the marine vessel, is now being decreased life time to serve due to cavitation erosion, vortex current, high flow speed suffer from ship speed going up dramatically. In this study, 10 kinds of thermal spray coating materials(2 of Zn alloy series, 3 of Al alloy series, 3 of Cu alloy series, 2 of STS alloy series) are chosen to apply on specimens and analyze micro structure, metallic composition, properties(porosity, oxidation) by using visual observation, XRD, EDX etc.. Additionally, to refine the characteristic of corrosion endurance for thermal spray coating layer, compared with thermal spray process and 5 kinds of heavy duty painting and AC paint (Anti-Corrosion Paint). Based on above mentioned experimental results, a priority of all coated specimens on corrosion-erosion endurances finalized and summarized there by desirable composition and process of thermal sprayed material properly.

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Calcium Removal from Effluent of Electronics Wastewater Using Hydrodynamic Cavitation Technology (수리동력학적 캐비테이션을 이용한 전자폐수 처리수에 함유된 칼슘저감에 관한 연구)

  • Park, Jin-Young;Kim, Sun-Jip;Lee, Yong-Woo;Lee, Jae-Jin;Hwang, Kyu-Won;Lee, Won-Kwon
    • Journal of Korean Society of Environmental Engineers
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    • v.29 no.6
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    • pp.715-721
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    • 2007
  • Residual calcium concentration is high, in general, at the effluent of the fluoride removal process in the electronics industry manufacturing semiconductor and LCD. To increase the stability of the membrane process incorporated for reuse of wastewater, the residual calcium is required to be pre-removed. Hyperkinetic Vortex Crystallization(HVC) process was installed in the electronics industry manufecturing semi conductor as a pilot scale for accelerating calcification of calcium ion. Compared to the conventional soda ash method, the 31% higher calcium removal efficiency was achieved when HVC was applied at the same sodium carbonate dosage. In order to maintain the economic calcium removal target of 70% preset by manufacturer, the dosing concentration of the soda ash was 530 mg/L based on influent flowrate. The seed concentration in the reactor was one of the critical factors and should be maintained in the range of $800\sim1,200mg$ SS/L to maximize the calcium removal efficiency. The calcite production rate was 0.30 g SS/g $Na_2CO_3$ in the average. The economic HVC passing time of the mixture was in the range of $2\sim5$ times. Relatively, stable calcium concentration was maintained in the range of $30\sim72$ mg/L(average 49 mg/L) although the calcium concentration in the feed was severely fluctuated with $74\sim359$ mg/L(average 173 mg/L). The HVC process was characterized as environment-friendly technology reducing chemical dosage and chemical sludge production and minimizing maintenance cost.