• Title/Summary/Keyword: USC(Ultra Super Critical)

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Root Cause and Countermeasure on the Spike Vibration of a 550MW Class USC(Ultra Super Critical) Steam Turbine (550MW급 초초임계압(USC, Ultra Super Critical) 증기터빈의 Spike Vibration 에 관한 원인 규명 및 대책)

  • Yang, Seong-Heon;Kim, Yong-Seok;Nah, Un-Hak
    • Proceedings of the Korean Society for Noise and Vibration Engineering Conference
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    • 2007.05a
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    • pp.442-447
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    • 2007
  • A very abnormal vibration was occurred at the LP(low pressure) turbine continuously during the pre-operation for a 550MW class USC(ultra super critical) steam turbine. This vibration was initiated at the rotating speed of about 3,450rpm and then the vibration amplitude was highly increased the number by $2{\sim}3$ times with the increase of the rotating speed to the rated speed(3,600rpm). In this paper, this abnormal vibration named spike vibration. This spike vibration was caused by the rubbing between the rotating bucket tip seal and the Lower Half of spill strip. Also, this paper presents the mechanism of the spike vibration and the proper method to eliminate this abnormal vibration problem. This result would be good practice to find the solution of similar high vibration in the USC steam turbines for power plant as well as industrial rotating machineries.

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Root Cause and Countermeasure on the Spike Vibration of a 550MW Class USC(ultra super critical) Steam Turbine (550MW급 초초임계압(USC, ultra super critical) 증기터빈의 Spike Vibration에 관한 원인 규명 및 대책)

  • Yang, Seong-Heon;Kim, Yong-Seok;Nah, Un-Hak;Park, Jong-Geun
    • Transactions of the Korean Society for Noise and Vibration Engineering
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    • v.17 no.12
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    • pp.1238-1245
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    • 2007
  • A very abnormal vibration was occurred at the LP(low pressure) turbine continuously during the pre-operation for a 550MW class USC(ultra super critical) steam turbine. This vibration was initiated at the rotating speed of about 3,450 rpm and then the vibration amplitude was highly increased the number by $2{\sim}3$ times with the increase of the rotating speed to the rated speed (3,600 rpm). In this paper, this abnormal vibration named spike vibration. This spike vibration was caused by the rubbing between the rotating bucket tip seal and the lower half of spill strip. Also, this paper presents the mechanism of the spike vibration and the proper method to eliminate this abnormal vibration problem. This result would be good practice to find the solution of similar high vibration in the USC steam turbines for power plant as well as industrial rotating machineries.

Unit Response Optimizer mode Design of Ultra Super Critical Coal-Fired Power Plant based on Fuzzy logic & Model Predictive Controller (퍼지 로직 및 모델 예측 제어기 적용을 통한 초초임계압 화력발전소 부하 응답 최적화 운전 방법 설계)

  • Oh, Ki-Yong;Kim, Ho-Yol
    • The Transactions of The Korean Institute of Electrical Engineers
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    • v.57 no.12
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    • pp.2285-2290
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    • 2008
  • Even though efficiency of coal-fired power plant is proportional to operating temperature, increasement of operating temperature is limited by a technological level of each power plant component. It is an alternative plan to increase operating pressure up to ultra super critical point for efficiency enhancement. It is difficult to control process of power plant in ultra super critical point because that point has highly nonlinear characteristics. In this paper, new control logic, Unit Response Optimizer Controller(URO Controller) which is based on Fuzzy logic and Model Predictive Controller, is introduced for better performance. Then its performance is tested and analyzed with design guideline.

The creep rupture properties on welded joints of Cr-W pipe steels for boiler in advanced thermal power plant (석탄화력발전소 보일러 배관용 Cr-W계 강 용접부의 크리프 파단특성)

  • 이연수;유석현;공병욱;이경운;김정태
    • Proceedings of the KWS Conference
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    • 2004.05a
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    • pp.149-151
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    • 2004
  • 고효율, 대용량의 친환경적이며 경제적인 발전소건설을 위해 초초임계압(USC: Ultra Super Critical) 석탄화력발전소의 건설이 세계적인 추세이다. 이러한 USC발전소는 효율향상을 위해 증기온도와 압력의 상승, 경제적 운용을 위해 부하변동운전 적용확대가 필수적이다. (중략)

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Investigation on the forging process of HIP rotor for USC power plant (USC 발전용 HIP Rotor의 단조 공정 연구)

  • Kim D. K.;Kim Y. D.;Kang S. T.;Kim D. Y.
    • Proceedings of the Korean Society for Technology of Plasticity Conference
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    • 2005.05a
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    • pp.479-482
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    • 2005
  • To improve the efficiency of fossil power plant, the higher steam temperature and pressure are required. Ultra super critical(USC) system meets very well this requirement. The HIP rotor is one of the most important parts of turbine in USC system and its material is easy to crack during hot forging. In this study, the upsetting and cogging process far $12\%Cr$ ESR ingot was analyzed and it is suggested a optimum process to avoid surface crack. The results were verified by test product with 4,200 tonnage press.

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Development of Ultra-Supercritical (USC) Power Plant (초초임계압(USC) 화력발전기술 개발)

  • Chang, Sung-Ho;Kim, Bum-Soo;Min, Taek-Ki
    • Transactions of the Korean Society of Mechanical Engineers B
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    • v.36 no.2
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    • pp.205-210
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    • 2012
  • For environmental reasons and because of our limited energy resources, high-efficiency power generation technology will be necessary in the future. Ultra-supercritical (USC) power generation technology is the key to managing the greenhouse gas problems and energy resource problems discussed in the Kyoto Protocol to the United Nations Framework Convention on Climate Change. Other countries and manufacturers are trying to build commercial power plants. In this paper, an efficient method of achieving near-zero emission operation of a high-efficiency fossil power plant using USC power generation is discussed. Development of USC power generation in Korea has been supported by the Korean government in two phases: Phase I was USC key technology development from 2002 to 2008, and Phase II is USC development and technology optimization from 2010 to 2017.

Development trend of material and manufacturing process for fossil power generation (화력발전 소재 및 제조기술 개발)

  • Lee, Kyongwoon;Kong, Byeongook;Kim, Minsoo;Kang, Chung Yun
    • Transactions of the Korean Society of Pressure Vessels and Piping
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    • v.12 no.1
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    • pp.141-148
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    • 2016
  • This paper presents an overview of worldwide electric power development and National $700^{\circ}C$ Hyper Supercritical coal-fired power generation(HSC) focus on materials and manufacturing process. To Increase the efficiency of electric power generation, It is necessary to increase steam temperature and pressure. In that case, New material and manufacturing process shall be developed for boiler and turbine component in high temperature and pressure operating condition. Therefore, Much Efforts in worldwide are progressing to develop materials and manufacturing technology and to build and operate an HSC.

초초임계 화력발전용 터빈 및 보일러소개

  • Gong, Byeong-Uk;Gang, Seong-Tae;Lee, Yeon-Su
    • 기계와재료
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    • v.22 no.2
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    • pp.20-30
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    • 2010
  • 석탄화력발전소의 효율향상은 스팀온도 및 압력의 증가를 통해 꾸준하게 이루어지고 있으며, 이러한 고효율의 화력발전은 사용 연료의 감소 뿐 아니라 $SO_x$, $NO_x$, $CO_2$ 등의 환경 가스배출을 감소시키는 효과도 있다. 이에 따라 운전조건을 고온, 고압화하려는 노력이 전 세계적으로 꾸준히 전개되고 있으며, 경제성 있고 높은 고온특성을 갖는 터빈 및 보일러 소재확보 여부가 발전소 건설 가능성을 결정하는 가장 주요한 요소 중 하나로 작용하고 있다. 본 고에서는 USC(Ultra Super Critical) 조건에 사용하기 위한 소재의 개발과정과 현대 사용되고 있는 다양한 발전용 고온소재의 특징에 대해 기술하고자 한다.

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Formation of Multi-Component Boride Coatings Containing V and/or Cr and Evaluation of Their Properties (바나듐 및 크롬을 포함하는 다 성분 Boride 코팅의 생성 및 특성 평가)

  • Lee, Euiyeol;Yoon, Sanghyun;Kim, Jongha
    • Journal of the Korean institute of surface engineering
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    • v.49 no.2
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    • pp.211-217
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    • 2016
  • Boride coating applied on steam turbine parts of power plants has provided good particle erosion resistance under temperature of $550^{\circ}C$, but it isn't able to protect the parts effectively any more in ultra super critical (USC) steam turbine which is being operated up to temperature of $650^{\circ}C$. To ensure stable durability for USC steam turbine parts, an alternative coating replacing boride coating should be developed. In this study, multi-component boride coatings containing elements such as chromium (Cr) and vanadium (V) were formed on base metal (B50A365B) using thermochemical treatment method called by pack cementation. The thermochemical treatments involve consecutive diffusion of boron(B) and Cr or/and V using pack powders containing diffusion element sources, activators and diluents. The top layer of Cr-boride coating is primarily consisted of $Cr_2B_3$ and $Cr_5B_3$, while that of V-boride coating is mostly consisted of $VB_2$ and $V_2B_3$. The (Cr,V)-boride coating is consisted of $Cr_2B_3$, $Cr_5B_3$ and $V_2B_3$ mostly. The top surfaces of 3 multi-component boride coatings show hardness of $3200-3400H_v$, which is much higher than that of boride, about $1600-2000H_v$. In 5 wt.% NaCl solution immersion tests, the multi-component boride coatings show much better corrosion resistance than boride coating.

A Study on the Oxidation Behaviors of Power Plant Valve Materials under the Ultra Super Critical Condition (초초 임계 화력 발전소용 밸브 소재의 산화 거동)

  • Lee, J.S.;Cho, T.Y.;Yoon, J.H.;Joo, Y.G.;Song, K.O.;Cho, J.Y.;Kang, J.H.;Lee, S.H.;Uhm, K.W.;Lee, J.W.
    • Journal of the Korean institute of surface engineering
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    • v.42 no.1
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    • pp.26-33
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    • 2009
  • Recently ultra-supercritical steam power plants operate at $1000^{\circ}F$ ($538^{\circ}C$) and 3500 psi (24.1 MPa). Thermal efficiency of power plant will be increased about 2% if steam temperature increases from $1000^{\circ}F$ to $1150^{\circ}F$ ($621^{\circ}C$). In this study valve materials Incoloy901 (IC901) and Inconel718 (IN718) were nitrided to improve the surface hardness and solid lubrication function of the valve materials. The hardness of both IC901 and IN718 increased about two times by ion nitriding. IC901, IN718 and their nitrided specimens were corroded under ultra super-critical condition (USC) of $621^{\circ}C$. and 3600 psi (24.8 MPa) for 2000 hours. Oxidations of both IC901 and IN718 were very small due to the formation of protective oxide layer on the surface. But the corrosion resistance of both nitrided specimens decreased because of the formation of non-protective nitride layer of $Fe_{4}N$, $Fe_{2}N$ and CrN on the surface layer. The hardness of both nitrided IC901 and IN718 at $20{\mu}m$ depth from the surface decreased about 30% and 20% respectively by USC 2000 hours.