• Title/Summary/Keyword: Turbo engine

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A study on the reduction of the flow-induced noise in turbo-charger diesel engines (터보 차져 디젤 엔진에서의 기류음 감소를 위한 연구)

  • Kang, Woong;Kim, Hyung-Jin;Sung, Hyung-Jin
    • Proceedings of the KSME Conference
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    • 2007.05b
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    • pp.2913-2917
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    • 2007
  • Turbocharger has been widely used in many passenger cars in application with diesel engines because of high power and fuel efficiency. However, flow-induced noise (whoosh or hissing noise) which is generated within the compressor during its operation at marginal surge line can deteriorate noise characteristics. Hissing noise excitation was associated with the generation of turbulence within the turbocharger compressor and radiated through the transmission path in turbocharger system. In this study, a sharp-edged reactive-type muffler was devised and installed in the transmission path to reduce the hissing noise. Acoustic and fluid dynamic characteristics for the muffler were investigated which is related to the unsteadiness of turbulence and pressure in turbocharger system. A transfer matrix method was used to analyze the transmission loss of the muffler. Simple expansion muffler with extended tube of the reactive type is proposed for the reduction of high frequency component noise. Turbulence computation was carried out by a standard ${\kappa}-{\varepsilon}$ model. An optimal design condition of the muffler was obtained by extensive acoustic and fluid dynamic analysis on the engine dynamometer with anechoic chamber. A significant reduction of the hissing noise was achieved at the optimal design of the muffler as compared with the conventional turbocharger system.

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A Development of an Intake RCV System for the Low Noise Turbo Engine (터보엔진의 저소음 흡기 RCV 시스템 개발)

  • Lee, Jong-Kyu;Kim, Jae-Heon;Kang, Sang-Kyu;Kang, Koo-Tae
    • Transactions of the Korean Society for Noise and Vibration Engineering
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    • v.20 no.8
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    • pp.734-741
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    • 2010
  • In this paper, an intake RCV system for low noise turbo engine was developed through optimization process of a geometric path of compressor housing and an open rate of recirculation valve. At first, the critical customer requirement from voice of customer was defined and quality function deployment of an intake RCV system was executed. And then, the renovative concept design using pugh matrix method was selected as final concept for satisfaction of requirement. Simultaneously, system analysis was carried by function diagram and fishbone diagram. Next, control factors and levels for the optimal design were performed. And, the optimal design of an intake RCV system was studied using design of experiment. Conclusively, we achieved not only cancellation tip-out noise at the driving condition but also improvement of NVH commodity through optimization process of an intake RCV system, which is optimal configuration of compressor housing and recirculation valve.

Sensorless vector control for super-high speed PMSM drive

  • Bae Bon-Ho;Sul Seung-Ki;Kwon Jeong-Hyeck;Shin Jong-Sub
    • Proceedings of the KIPE Conference
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    • 2001.10a
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    • pp.773-778
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    • 2001
  • This paper describes the implementation of the vector control schemes for a variable-speed 131kW PMSM (Permanent Magnet Synchronous Motor) in super-high speed application. The vector control with synchronous reference frame current regulator has been implemented with the challenging requirements such as the extremely low stator inductance$(28^{\mu}H)$, the high dc link voltage(600V) and the high excitation frequency(1.2kHz). Because the conventional position sensor is not reliable in super-high speed, a vector control scheme without any position sensor has been proposed. The proposed sensorless algorithm is implemented by processing the output voltage of the PI current regulator, and hence the structure is simple and the estimated speed is robust to the measurement noise. The experimental system has been built and the proposed control has been implemented and evaluated. The test result, up to the speed of 60,000 r/min, shows the validity of the proposed control.

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Detonation Wave Studies for CVC Engines of TBCC (TBCC를 위한 CVC 엔진의 데토네이션 현상 기초 연구)

  • Choi, J.Y.;Parent, Bernard;Cho, D.R.;Kang, K.;Shin, J.R.;Lee, S.H.;Yi, T.H.
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2008.11a
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    • pp.326-329
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    • 2008
  • DARPA's hypersonic propulsion program VULCAN is aimed for development of Mach 4+ capable engine by combining current production turbofan engine such as F119 with CVC (Constant Volume Combustion) engine. Final goal is a TBCC(Turbo-based Combined Cycle) engine by combining with dual mode ramjet/scramjet engine. CVC is a common designation of new concept of high efficiency engines, such as Pulse Detonation Engine (PDE) or Continuous Detonation Engine (CDE), which use the detonation as a combustion mechanism. Present paper introduces the internationally collaborative research activities carried out in Aerospace Combustion and Propulsion Laboratory of the department of Aerospace Engineering of the Pusan national University.

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The Effects of Pulsating Flow on Volumetric Efficiency in the Intake and Exhaust System in a Turbocharged Diesel Engine (흡.배기 시스템의 맥동류가 과급디젤기관의 체적효율에 미치는 영향)

  • Kim, K.H.;Kang, H.Y.;Koh, D.K.
    • Journal of Power System Engineering
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    • v.13 no.4
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    • pp.11-17
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    • 2009
  • This paper deals with the effects of pulsating flow on volumetric efficiency, which may be generated during the gas exchange procedure, due to piston motion, valve event on intake and exhaust stroke and unsteady flow of turbocharger of a three-cylinder four stroke turbo-charged diesel engine. Consequently, volumetric efficiency affects significantly the engine performance; torque characteristics, fuel economy and further to emission and noise level. As the expansion ratio became larger the engine speed varies and torque increases, the pressure pulsation in an exhaust gas pipe acts as an increasing factor of intake air charging capacity totally. The phase and amplitude of pressure pulsation in the intake system only affects volumetric efficiency favorably, if it is well matched and tuned effectively to the engine. Thus, to verify the exact phase and amplitude of the pressure variation is the ultimate solution for the air-flow ratio assessment in the intake stroke. Some experimental results of pressure diagrams in the intake pipe and gas-flow of turbine in-outlet are presented, under various kinds of operating condition.

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Design of Fuzzy-PID Controller for Turbojet Engine of UAV Using LabVIEW (LabVIEW를 이용한 무인항공기용 소형 터보제트 엔진의 Fuzzy-PID 제어기 설계)

  • Shin, Haeng-Cheol;Jie, Min-Seok
    • Journal of Advanced Navigation Technology
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    • v.20 no.3
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    • pp.190-195
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    • 2016
  • In this paper, Propose to prevent compressor surge and improve the transient response of the fuel flow control system of turbojet engine. Turbojet engine controller is designed by applying Fuzzy-PID control algorithm. To prevent any surge or a flame out event during the engine acceleration or deceleration, the Fuzzy-PID controller effectively controls the fuel flow input of the control system. Fuzzy-PID results are used as the fuel flow control inputs to prevent compressor surge and flame-out for turbo-jet engine and the controller is designed to converge to the desired speed quickly and safely. Using LabVIEW to perform computer simulations verified the performance of the proposed controller. Response characteristics pursuant to the gain were analyzed by simulation.

Development of the Condition Monitoring Test Cell Using the Micro Gas Turbine Engine (초소형 가스터빈을 이용한 상태감시 시험장치 개발)

  • Kho, Seong-Hee;Ki, Ja-Young;Koo, Young-Ju;Kong, Chang-Duk;Lee, Eun-Woo
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2009.05a
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    • pp.345-349
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    • 2009
  • This test cell is developed to the institutes or laboratories research and study gas turbine engine for academic purpose with this test data to provide the fundamentals of operational mechanism and structural configuration, and further to verify thermodynamic calculation The test cell is installed to monitor and compare real-time data with reference engine model performance simulation data. using by NI DAQ(Data acquisition)device and LabVIEW program based on 30lbf-micro turbojet engine.

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Development of Transient Simulation Program for Smart UAV Propulsion System (스마트 무인기 추진기관의 천이 모사 프로그램 개발)

  • Lee, Chang-Ho;Ki, Ja-Young
    • Journal of the Korean Society of Propulsion Engineers
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    • v.15 no.6
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    • pp.63-69
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    • 2011
  • The Smart UAV must have the control characteristics of propulsion system necessary for both rotary aircraft and fixed wing aircraft though it equips turbo-shaft engine. To develop an electronic engine controller in the future, it is necessary to accumulate the experience of engine operation and data of tilt rotor aircraft. For this purpose, the computer programs which predict engine performance in the steady state and transient state can be utilized for the supplementation of flight test data. In this work, we developed a dynamic analysis program using engine performance data gathered during the flight tests. In addition the accuracy of the program was verified through comparison with flight test data and the results of steady-state performance analysis program.

Development of the Performance Test Cell Using the Small Gas Turbine Engine of 80 lbf-Thrust (80lbf급 소형 가스터빈 엔진의 성능 시험장치 개발)

  • Jin, Hak-Su;Kho, Seong-Hee;Ki, Ja-Young;Yong, Seong-Ju;Kang, Myoung-Cheol;Lee, Eun-Woo
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2010.11a
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    • pp.495-498
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    • 2010
  • This test cell is developed to the institutes or laboratories research and study gas turbine engine for academic purpose with this test data to provide the fundamentals of operational mechanism and structural configuration, and further to verify thermodynamic calculation The test cell is installed to monitor and compare real-time data with reference engine model performance simulation data. using by NI DAQ(Data acquisition)device and LabVIEW program based on 80 lbf-micro turbojet engine.

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Evaluation on a Miller Cam for Improving the Fuel Consumption of a Large Diesel Engine (대형 디젤 엔진의 연비 향상을 위한 Miller Cam 평가)

  • Song, Changhoon;Wang, Tae Joong;Im, Heejun
    • Transactions of the Korean Society of Automotive Engineers
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    • v.24 no.1
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    • pp.47-52
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    • 2016
  • Miller timing is one of the promising ways which can improve the fuel consumption of internal combustion engines. Indeed, Miller timing employing an early intake valve close is widely applied to large diesel and gas engines to enhance performance and reduce NOx emissions. In this study, performance evaluation is carried out by 1-D cycle simulation in order to estimate the effect of Miller CAM timing before BDC for a 32 L turbocharged diesel engine. To optimize Miller CAM timing, a single stage turbocharger is matched with an early intake valve close since boost pressure is a significant parameter that can control compression work in a turbocharged engine. The engine simulation result shows that there is enough potential to improve fuel consumption rate and also reduce NOx emissions at the same time.Abstract here.