• 제목/요약/키워드: Turbo compressor

검색결과 147건 처리시간 0.036초

퍼지 PI+D 제어기를 이용한 터보제트 엔진의 연료유량 제어 (Fuel Flow Control of Turbojet Engine Using the Fuzzy PI+D Controller)

  • 정병인;지민석
    • 한국항행학회논문지
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    • 제15권3호
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    • pp.449-455
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    • 2011
  • 본 논문에서는 연료유량이 제어 수단인 터보제트 엔진에 대해 압축기의 서지를 방지하면서 가속시간을 줄일 수 있는 제어기를 제안하였다. 퍼지이론과 PI+D 제어 알고리즘을 적용하는 터보제트 엔진 제어기를 설계하였고 Mamdani의 추론법을 적용하여 추론하고, 비퍼지화는 무게 중심법을 사용하였다. 퍼지추론 결과는 터보제트 엔진의 가감속시 서지와 flame-out 현상을 방지하기 위해 연료 유량 제어 입력으로 사용되고, 신속하고 안전하게 원하는 속도로 수렴할 수 있도록 제어기를 설계한다. MATLAB을 사용한 컴퓨터 시뮬레이션을 수행하여 제안된 제어기의 성능을 입증하였다.

부분부하제어를 위한 스크류형 과급기 개발 (Development of a screw type super-charger for part load control)

  • 배재일;배신철
    • 대한기계학회:학술대회논문집
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    • 대한기계학회 2001년도 추계학술대회논문집B
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    • pp.353-358
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    • 2001
  • Turbo-charging or Super-charging has been used to boost engine power for Gasoline Engine and Diesel Engine came to the world at the beginning of $20^{th}$ century. So far Turbo-Charger has enjoyed a high reputation in the charging filed for its technical advantages such as no demand of operation power from engine and an excellent charging effect in the event of a static operation at mid- and high engine speed. A mechanically driven Super-Charger, however, is now emerging in order to meet demands of the age of speed such as high engine power for a quick change of the driving mode - high engine torque even at low engine speed. Since Super-Charger needs driving power from engine, it cannot improve its relatively higher fuel consumption against that of Turbo-Charger. This negative point is still an obstacle to the wide use of Super-Charger. Super-Charger using Screw-type compressor which has already had a considerable base in air compressor market will fulfill this purpose of improving fuel consumption by minimizing operation power owing to no charging at idling or partially loading driving. This study aims to develop power control concept to achieve this minimization of operation power.

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Integration of the Engine Control into the Optimal Trajectory Determination for a Spaceplane

  • Matsunaga, Kensuke;Tanatsugu, Nobuhiro;Sato, Tetsuya;Kobayashi, Hiroaki;Okabe, Yoriji
    • 한국추진공학회:학술대회논문집
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    • 한국추진공학회 2004년도 제22회 춘계학술대회논문집
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    • pp.742-748
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    • 2004
  • In this paper are presented TSTO system analysis including some controlled variables on the engine operation such as a fuel flow rate and a pressure ratio of compressor, as well as variables on the trajectory. TSTO studied here is accelerated up to Mach 6 by a fly-back booster powered by air breathing engines. Three different types of engine cycle were treated for propulsion system of the booster, such as a turbo ramjet, a precooled turbojet and an EXpander cycle Air Turbo Ramjet (ATREX). The history of the controlled variables on the engine operation was optimized by Sequential Quadratic Programming (SQP) to accomplish the minimum fuel consumption. The trajectory was also optimized simultaneously. The results showed that the turbo ramjet gave the best fuel consumption. The optimal trajectory was almost the same except in the transonic range and just before reaching to Mach 6. The history of the pressure ratio of compressor considerably depended on the engine type. It is concluded that simultaneous optimization for engine control and trajectory is effective especially for a high-speed airplane propelled by turbojets like the TSTO booster.

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터보 콤프레셔용 3로브 베어링의 설계에 관한 연구 (A Study of Three Lobe Bearing Design for Turbo Compressor)

  • 이동환;김병옥
    • 한국소음진동공학회:학술대회논문집
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    • 한국소음진동공학회 2006년도 추계학술대회논문집
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    • pp.549-555
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    • 2006
  • Three lobe bearings for turbo compressor which appear inner pad damage after field operation has been analysed and redesigned in order to remove the problems. Pre-load and clearance between the pad and journal of the bearing were changed as design parameters from that of the original ones considering suitable maximum temperature and maximum pressure of the bearings. New hearings were manufactured corresponding the redesign. And vibration and temperature were measured according to the API specifications.

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전압 구동 방법에 따른 터보 압축기용 초고속 영구자석 동기 전동기의 회전자 손실 해석 (Analysis on Eddy Current Losses of High Speed Permanent Magnet Synchronous Motor for Turbo Compressor according to Voltage Source Driving)

  • 장석명;김현규;고경진;이성호;홍영희
    • 대한전기학회:학술대회논문집
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    • 대한전기학회 2009년도 제40회 하계학술대회
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    • pp.712_713
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    • 2009
  • This paper deals with the analysis on eddy current looses of high speed permanent magnet synchronous motor (PMSM) for turbo compressor according to voltage source driving. This paper presents analytical procedures for calculation of the eddy current losses using Poynting theorem. On the basis of the magnetic vector potential and a two-dimensional (2-D) cylindrical coordinate system, this paper derived analytical solutions of the eddy current looses using phase current analysis. The eddy current losses of each harmonic obtained by fast Fourier transform (FFT) analysis of phase current are with results obtained from finite-element method (FEM).

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터보압축기의 소음특성 및 개선방안 (The Noise property and Its improvement of the Turbo Compressor)

  • 천광욱;신범식;최연선
    • 한국소음진동공학회:학술대회논문집
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    • 한국소음진동공학회 2009년도 춘계학술대회 논문집
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    • pp.282-287
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    • 2009
  • In this paper, 3-stage centrifugal turbo compressor was measured and analyzed numerical simulation for find noise source and was reduced noise with changing designs. For this purpose, it was measured noise level and was analyzed noise frequency at each stage. In order to Find where is noise source, the study was investigated about structure borne noise by using modal analysis and also was checked sound radiation and leakage of noise at inlet and outlet by result of sound intensity. In order to reduce of noise, sound insulation rings were maded and were adhered at joint and noise reduction effects were verified by measurement and numerical simulation. From the analysis results of leakage of noise, this study presented new joint designs, also it was verified by result of numerical simulation.

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터보 압축기용 초고속 영구자석형 동기전동기의 설계 및 특성 해석 (Design and Characteristics Analysis of High-Speed Permanent Magnet Synchronous Motor for Turbo Compressor)

  • 장석명;고경진;유대준;박지훈;이운호;이성호
    • 대한전기학회:학술대회논문집
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    • 대한전기학회 2008년도 제39회 하계학술대회
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    • pp.731-732
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    • 2008
  • This paper deals with design and characteristics analysis of 7.5-kW, 60,000-rpm class permanent magnet synchronous motor for turbo compressor. In order to determine the design parameters of rotor, torque per rotor volume method is applied. And, to analyze the magnetic field distribution and estimate the electrical parameters such as back EMF constant, inductance and torque constant, electromagnetic transfer relations theorem is employed. We compare the characteristics analysis results of model designed by proposed method with those by nonlinear FEA. As a result of this, the design have been validated.

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A Simplified Method to Calculate the EMF Characteristics of Multi-disk Axial-gap PM Motor using 2-D & 3-D FEM

  • Kim, Young-Kwan;Lee, Ju
    • 조명전기설비학회논문지
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    • 제22권3호
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    • pp.34-39
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    • 2008
  • The purpose of this paper is characteristic analysis of multi-disk axial-gap pm motor for turbo compressor. The axial-gap permanent magnet motor has shown a growing interest in high-speed application for its high-efficiency, compact size and low vibration characteristics due to core-less structure. To achieve high-power, the axial-gap PM motor has multi-disk structure of stator and rotor disk. Because of its complicated magnetic flux path, it is not easy to calculate a dynamic characteristics using finite element analysis. In this paper, the simplified 2-D unfolded model to predict EMF characteristic is presented. To verify thesuggested 2-D unfolded model analysis of back-EMF characteristic was calculated and compared 3-D finite element. Finally the proposed method is verified by experimental results and shows good agreement with test results.

정압베어링을 적용한 터보팽창기의 회전체 동역학 해석 및 구동시험 (Rotordynamic Analysis and Operation Test of Turbo Expander with Hydrostatic Bearing)

  • 이동현;김병옥;정준하;임형수
    • Tribology and Lubricants
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    • 제38권2호
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    • pp.33-40
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    • 2022
  • In this study, we present rotor dynamic analysis and operation test of a turbo expander for a hydrogen liquefaction plant. The turbo expander consists of a turbine and compressor wheel connected to a shaft supported by two hydrostatic radial and thrust bearings. In rotor dynamic analysis, the shaft is modeled as a rigid body, and the equations of motion for the shaft are solved using the unsteady Reynolds equation. Additionally, the operating test of the turbo expander has been performed in the test rig. Pressurized helium is supplied to the bearings at 8.5 bar. Furthermore, we monitor the shaft vibration and flow rate of the helium supplied to the bearings. The rotor dynamic analysis result shows that there are two critical speeds related with the rigid body mode under 40,000 rpm. At the first critical speed of 36,000 rpm, the vibration at the compressor side is maximum, whereas that of the turbine is maximum at the second critical speed of 40,000 rpm. The predicted maximum shaft vibration is 3 ㎛, whereas sub-synchronous vibration is not presented. The operation test results show that there are two critical speeds under the rated speed, and the measured vibration value agrees well with predicted value. The measured flow rate of the helium supplied to the bearing is 2.0 g/s, which also agrees well with the predicted data.

Real operation of 2 kW class reverse-Brayton refrigeration system with using scroll compressor package

  • Kim, Hyobong;Yeom, Hankil;Choo, Sangyoon;Kim, Jongwoo;Park, Jiho;In, Sehwan;Hong, Yong-Ju;Park, Seong-Je;Ko, Junseok
    • 한국초전도ㆍ저온공학회논문지
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    • 제22권4호
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    • pp.40-44
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    • 2020
  • This paper describes the real operation of 2 kW class reverse-Brayton refrigeration system with neon as a working fluid. The refrigeration cycle is designed with operating pressure of 0.5 and 1.0 MPa at low and high pressure side, respectively. Compressor package consists of several helium scroll compressors witch are originally used for driving GM cryocooler. Three segments of plate heat exchanger are adopted to cover the wide temperature range and the refrigeration power is produced by turbo expander. The developed refrigeration system is successfully operated at its target temperature of 77 K. In experiments, all parameters such as pressure, temperature, mass flow rate and valve opening are measured to investigate characteristics during cool-down process and normal state. The difference between design and real operation is discussed with measured experimental data. At normal state of 77 K operation, the developed reverse-Brayton refrigeration system shows 1.83 kW at 68.2 K of cold-end temperature.