• 제목/요약/키워드: System performance test

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50kW 마이크로 가스터빈 개발 (Development of a 50kW Micro Gas Turbine Engine)

  • 김수용;박무룡;최범석;안국영;최상규
    • 유체기계공업학회:학술대회논문집
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    • 유체기계공업학회 2002년도 유체기계 연구개발 발표회 논문집
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    • pp.314-319
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    • 2002
  • Performance analysis and test of a 50kW micro gas turbine is carried out. The present study was initiated in 1996 by KIMM researchers to develope a 50kW class turbogenerator gas turbine engine for hybrid vehicle propulsion system. but with its low emission and compactness, it seemed that it can also be applied as a source of distributed power generation. In this study, general description of the KIMM's efforts to acquire performance test skills of the self-made 50kW micro gas turbine engine. At present, non-load performance test up to 615000 rpm was accomplished and is expected to make through 80,000 rpm by the end of year. Several revisions in design and manufacture were made during the course of experiments. The resulting outputs is thought to be valuable for the further refinement of the system for eventual commercialization of the product.

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TDX-10 패킷처리기의 성능척정을 위한 트래픽발생기의 설계 (Traffic Generator for Performance Test of the TDX-10 Packet Handler)

  • 정중수;전경표
    • 전자공학회논문지A
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    • 제32A권3호
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    • pp.411-417
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    • 1995
  • Packet switching is an important aspect of ISDN. In the TDX-10 switching system, which is being developed as an ISDN exchange in Korea, the packet switching function is implemented on the basis of Case B scenario of X.31. After implementing the packet switching function the performance test must be executed to check whether the design objectives of performance are satisfied or not. However, it is not easy to set up test environment for performance measurement under full load conditions. This paper presents the design of the traffic generator which enables us to do performance test of the TDX-10 packet handler under full load conditions. To generate packet traffic we change only software programs without any change of the hardware system of the packet handler.

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가정용 연료전지시스템 계통연계형 전력변환장치의 보호기능 성능평가에 관한 연구 (A Study on the Protective Function Performance Evaluation of Grid-Connected Power Conditioning System for Residential Fuel Cell System)

  • 이정운;서원석;김영규
    • 한국신재생에너지학회:학술대회논문집
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    • 한국신재생에너지학회 2009년도 춘계학술대회 논문집
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    • pp.341-344
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    • 2009
  • In this paper, protective function evaluation was conducted to determine the performance and safety of a power conditioning system(PCS) for 1kW residential fuel cell system. It is essential to have a power quality, grid-connection and safety of PCS. Even though it is under 500ms by KGS-A410 standard, it is shown a rapid response time of 25ms from input under-voltage test. In terms of output over/under-voltage test, it is shown 29.15 and 79.4ms. Especially using anti-islanding test, it is shown all times under 100ms for combination cases of real and reactive power. We confirmed a rapid response characteristics and safety of PCS. The results of this evaluation are being used to develop a new test protocols of PCS.

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가스계 소화설비의 제한사항 및 성능평가를 위한 배관 내 약제비율에 관한 연구 (A Study on Percent Agent in Pipe as a Criterion to Evaluate Limitations and Performance of Gaseous Fire Extinguishing Systems)

  • 손봉세;김희우
    • 한국화재소방학회논문지
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    • 제21권4호
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    • pp.1-11
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    • 2007
  • 본 연구에서는 할론 1301 및 이산화탄소를 비롯한 가스계소화설비의 성능을 시험하고 평가하기 위한 가장 중요한 핵심 요소인 배관내 약제비율, 관경비 등 소화성능에 영향을 미치는 가스계소화설비의 제한사항 및 성능확보에 필요한 요소에 대하여 연구하였다. 또한 본 연구에서는 관련 국내외 기준 분석 및 국내 가스계소화설비의 성능평가에 관한 인정기준(KFIS 002)에 따른 시스템 성능시험을 실시하고 결과를 비교 분석하였다.

Orifice Inlet효과에 의한 이젝터 성능에 관한 수치해석적 연구 (Numerical Investigation of the Effects of an Orifice Inlet on the Performance of an Ejector)

  • ;김희동
    • 한국추진공학회:학술대회논문집
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    • 한국추진공학회 2009년도 제33회 추계학술대회논문집
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    • pp.318-322
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    • 2009
  • Supersonic ejectors are simple mechanical components, which generally perform mixing and/or recompression of two fluid streams. Ejectors have found many applications in engineering. In aerospace engineering, they are used for altitude testing of a propulsion system by reducing the pressure of a test chamber. It is composed of three major sections: a vacuum test chamber, a propulsive nozzle, and a supersonic exhaust diffuser. This paper aims at the improvement of ejector-diffuser performance by focusing attention on reducing exhaust back flow into the test chamber, since alteration of the backflow or recirculation pattern appears as one of the potential means of significantly improving low supersonic ejector-diffuser performance. The simplest backflow-reduction device was an orifice plate at the duct inlet, which would pass the jet and entrained fluid but impede the movement of fluid upstream along the wall. Results clearly showed that the performance of ejector-diffuser system was improved for certain a range of system pressure ratios, where as there was no appreciable transition in the performance for lower pressure ratios and the orifice plate was detrimental to the ejector performance for higher pressure ratios. It is found that an appropriately sized orifice system should produce considerable improvement in the ejector-diffuser performance in the intended range of pressure ratios.

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수중함 자유항주모형 개발 및 기본 성능 분석 (Submarine Free Running Model Development and Basic Performance Analysis)

  • 이주호;김선홍;신지환;안진형
    • 대한조선학회논문집
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    • 제60권4호
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    • pp.256-265
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    • 2023
  • This paper describes the results of the development of the submarine Free Running Model (FRM). First, the goal of development was set based on the test conditions and the test environment, and the system was obtained accordingly. The target submarine, Joubert BB2 submarine, was selected with a scale of 18.35 in accordance with the development goal. In order to conduct a submarine FRM test underwater, where communication is impossible, the FRM must operate at least semi-autonomously. For this purpose, an Extended Kalman Filter (EKF) based underwater integrated navigation system and control system using a sailplane and an X-shaped sternplane were designed respectively. In addition, a ballast system was designed to enable the model to float to the water surface in case of an emergency. To verify its propulsion, navigation, and control performance, the FRM tests were conducted in both indoor and outdoor basins. As a result, the relationship between propeller RPM and vehicle speed was derived, and it was confirmed that the navigation and control performance met the target value.

극초음속 충격파 풍동 설계/구축 및 성능시험 Part II : 극초음속 충격파 풍동 구축 및 성능 시험 (Design/Construction and Performance Test of Hypersonic Shock Tunnel Part ii : Construction and Performance Test of Hypersonic Shock Tunnel)

  • 이형진;이복직;김세환;정인석
    • 한국항공우주학회지
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    • 제36권4호
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    • pp.328-336
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    • 2008
  • 극초음속으로 비행하는 추진기관이 직면하는 고속 유동 등 제반 현상을 모사하기 위한 지상시험 설비로 충격파 풍동을 설계, 구축한 후 성능 시험을 수행하였다. 개발된 준 일차원 작동 해석을 이용하여 설계점을 파악한 후, 가압식 극고속 시험 구축을 위한 개념 설계를 완료하였다. 이어 단위 해석 코드를 이용하여 구체적인 성능 설계 및 각 구성품에 대한 설계를 완료, 구축한 후, 다양한 운용조건에서 성능시험을 수행하였다. 본 논문에서는 각 구성품 설계 및 구축방법, 구축 후 수행된 다양한 성능 시험 결과를 자세히 제시하였다.

터널 물분무소화설비의 살수밀도분포에 대한 실험연구 (Experimental study on the spray density distribution of water spray system in road tunnel)

  • 소수현;박경환
    • 한국터널지하공간학회 논문집
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    • 제13권1호
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    • pp.1-8
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    • 2011
  • 장대 도로터널 및 위험도가 높은 도로터널에 설치되고 있는 물분무소화설비는 성능과 관계된 단위면적당 방수밀도에 대한 검증과정이 없이 사용되어 왔다. 본 연구는 도로터널에 물분무소화설비에 노즐을 설치하여 기준압력에서 방수시험을 실시하여 기준을 만족하는지 여부를 확인하였다. 결론적으로 모든 노즐이 기준을 만족하지 못하였다. 이런 결과는 도로터널용 물분무노즐을 검증하는 시험기준이 없고, 실제 시험을 통한 검증 과정이 존재하지 않았기 때문이라고 판단된다. 따라서 물분무노즐의 성능을 시험할 수 있는 기준의 마련과 설치된 시설을 검증하는 제도적인 보완이 필요하다.

가스터빈 엔진의 입구 유동 왜속 시험 (Inlet Distortion Test of Gas Turbine Engine)

  • 이진근;이경재;고성희;곽재수
    • 항공우주시스템공학회지
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    • 제1권1호
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    • pp.53-59
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    • 2007
  • Inlet distortion test was performed at Korea Aerospace Research Institute in order to evaluate the degradation of engine performance under the distorted inlet condition. In this paper, only the inlet pressure distortion was taken into consideration. During the development process of the inlet distortion test technique, variable distortion screen was designed and evaluated under various test conditions to establish the experimental database of distortion for engine test. The result of inlet distortion test for engine shows that the operating point was changed toward the worse direction and the degradation of engine performance by inlet distortion was verified.

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6자유도 MEMS 관성센서 정적성능 자동 평가 시스템 구현에 관한 연구 (A Study on Implementation of Automatic Evaluation System for Static Performance of 6 DOF MEMS Inertial Sensor)

  • 박지원;딘 후사무드;이병렬
    • 반도체디스플레이기술학회지
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    • 제22권3호
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    • pp.62-66
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    • 2023
  • With the advancement in technology and rapid increase in the demand for microelectromechanical systems (MEMS) based inertial measurement units (IMUs), high-volume production and test system remain a major challenge for the MEMS industry. To compete with the challenging market of Industry 4.0, here we developed an automatic test system to evaluate the performance of the ovenized IMU sensors as well as analyze the data. The automatic test system was developed by interfacing a commercial MEMS IMU (BMI 088) using LabVIEW. The BMI 088 was tested experimentally for long-term bias stability, ON/OFF bias repeatability, and root mean square (rms) noise. Furthermore, the data was analyzed through the developed test system. The results show that the automatic test system has improved the test time and reduced human effort. The developed automatic test system is a significant approach to MEMS research and development (R&D) to increase and improve the mass production of IMUs.

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