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Calculation of Unit Hydrograph from Discharge Curve, Determination of Sluice Dimension and Tidal Computation for Determination of the Closure curve (단위유량도와 비수갑문 단면 및 방조제 축조곡선 결정을 위한 조속계산)

  • 최귀열
    • Magazine of the Korean Society of Agricultural Engineers
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    • v.7 no.1
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    • pp.861-876
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    • 1965
  • During my stay in the Netherlands, I have studied the following, primarily in relation to the Mokpo Yong-san project which had been studied by the NEDECO for a feasibility report. 1. Unit hydrograph at Naju There are many ways to make unit hydrograph, but I want explain here to make unit hydrograph from the- actual run of curve at Naju. A discharge curve made from one rain storm depends on rainfall intensity per houre After finriing hydrograph every two hours, we will get two-hour unit hydrograph to devide each ordinate of the two-hour hydrograph by the rainfall intensity. I have used one storm from June 24 to June 26, 1963, recording a rainfall intensity of average 9. 4 mm per hour for 12 hours. If several rain gage stations had already been established in the catchment area. above Naju prior to this storm, I could have gathered accurate data on rainfall intensity throughout the catchment area. As it was, I used I the automatic rain gage record of the Mokpo I moteorological station to determine the rainfall lntensity. In order. to develop the unit ~Ydrograph at Naju, I subtracted the basic flow from the total runoff flow. I also tried to keed the difference between the calculated discharge amount and the measured discharge less than 1O~ The discharge period. of an unit graph depends on the length of the catchment area. 2. Determination of sluice dimension Acoording to principles of design presently used in our country, a one-day storm with a frequency of 20 years must be discharged in 8 hours. These design criteria are not adequate, and several dams have washed out in the past years. The design of the spillway and sluice dimensions must be based on the maximun peak discharge flowing into the reservoir to avoid crop and structure damages. The total flow into the reservoir is the summation of flow described by the Mokpo hydrograph, the basic flow from all the catchment areas and the rainfall on the reservoir area. To calculate the amount of water discharged through the sluiceCper half hour), the average head during that interval must be known. This can be calculated from the known water level outside the sluiceCdetermined by the tide) and from an estimated water level inside the reservoir at the end of each time interval. The total amount of water discharged through the sluice can be calculated from this average head, the time interval and the cross-sectional area of' the sluice. From the inflow into the .reservoir and the outflow through the sluice gates I calculated the change in the volume of water stored in the reservoir at half-hour intervals. From the stored volume of water and the known storage capacity of the reservoir, I was able to calculate the water level in the reservoir. The Calculated water level in the reservoir must be the same as the estimated water level. Mean stand tide will be adequate to use for determining the sluice dimension because spring tide is worse case and neap tide is best condition for the I result of the calculatio 3. Tidal computation for determination of the closure curve. During the construction of a dam, whether by building up of a succession of horizontael layers or by building in from both sides, the velocity of the water flowinii through the closing gapwill increase, because of the gradual decrease in the cross sectional area of the gap. 1 calculated the . velocities in the closing gap during flood and ebb for the first mentioned method of construction until the cross-sectional area has been reduced to about 25% of the original area, the change in tidal movement within the reservoir being negligible. Up to that point, the increase of the velocity is more or less hyperbolic. During the closing of the last 25 % of the gap, less water can flow out of the reservoir. This causes a rise of the mean water level of the reservoir. The difference in hydraulic head is then no longer negligible and must be taken into account. When, during the course of construction. the submerged weir become a free weir the critical flow occurs. The critical flow is that point, during either ebb or flood, at which the velocity reaches a maximum. When the dam is raised further. the velocity decreases because of the decrease\ulcorner in the height of the water above the weir. The calculation of the currents and velocities for a stage in the closure of the final gap is done in the following manner; Using an average tide with a neglible daily quantity, I estimated the water level on the pustream side of. the dam (inner water level). I determined the current through the gap for each hour by multiplying the storage area by the increment of the rise in water level. The velocity at a given moment can be determined from the calcalated current in m3/sec, and the cross-sectional area at that moment. At the same time from the difference between inner water level and tidal level (outer water level) the velocity can be calculated with the formula $h= \frac{V^2}{2g}$ and must be equal to the velocity detertnined from the current. If there is a difference in velocity, a new estimate of the inner water level must be made and entire procedure should be repeated. When the higher water level is equal to or more than 2/3 times the difference between the lower water level and the crest of the dam, we speak of a "free weir." The flow over the weir is then dependent upon the higher water level and not on the difference between high and low water levels. When the weir is "submerged", that is, the higher water level is less than 2/3 times the difference between the lower water and the crest of the dam, the difference between the high and low levels being decisive. The free weir normally occurs first during ebb, and is due to. the fact that mean level in the estuary is higher than the mean level of . the tide in building dams with barges the maximum velocity in the closing gap may not be more than 3m/sec. As the maximum velocities are higher than this limit we must use other construction methods in closing the gap. This can be done by dump-cars from each side or by using a cable way.e or by using a cable way.

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Electrochemical Reduction for trans-Complexes of Cobalt (III) with Bis(ethylenediamine) and Monodendate Ligands (한자리 리간드를 포함하는 트란스비스 (에틸렌디아민) 코발트 (III) 이온의 전극 환원반응)

  • Jung-Ui Hwang;Jong-Jae Chung;Jae-Duck Lee
    • Journal of the Korean Chemical Society
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    • v.33 no.2
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    • pp.215-224
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    • 1989
  • Electrochemical reductions of $trans-[Co(en)_2X_2](ClO_4)_n$ (where X is cyanide, nitrite, ammonia, and isothiocyanate) were investigated by cyclic voltammetry and polarography at mercury and glassy carbon electrode. $trans-[Co(en)_2(CN)_2]ClO_4$ was reduced to Co(II) complex followed by adsorption to the mercury electrode. Cyanide ion was not released from the reduced Co(II) complex but the cyanide and (en) were released after the reduction to metallic cobalt. The other complexes except $trans-[Co(en)_2(CN)_2]ClO_4$ were reduced to cobalt(II) complexes followed by release of monodendate ligand, and (en) was released at the reduction step to metallic cobalt. $trans-[Co(en)_2(NO_2)_2]ClO_4$ was reduced to cobalt(Ⅱ) complex, and $NO_2^-$ ion was released followed by electroreduction through ECE mechanism at pH 2. On glassy carbon electrode, all complexes of Co(III) were reduced to Co(II) complexes with irreversible one-electron diffusion controlled reaction in which (en) was not released at this step. Increasing absorption wave number of complexes caused to negative shift of peak potential.

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Study on reduction of power consumption in GPS embedded terminals with periodic position fix (GPS 단말기에서의 주기적 위치 측위에 따른 전력소모 최소화 방안 연구)

  • Bae, Seong-Soo;Kim, Dong-Ku;Kim, Tae-Min;Han, Chang-Moon;Kim, Byeong-Cheol
    • Journal of Advanced Navigation Technology
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    • v.11 no.3
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    • pp.239-251
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    • 2007
  • This thesis is about the reduction of the power consumption in GPS embedded terminals with periodic position fix to improve the time delay of position determination. In order to improve time delay of position determination during the wireless terminal is powered on, it needs to be set such that it can be periodically recalibrated by the GPS and those recalibrated values need to be saved in the terminal's memory so that it can reduce the time delay from the request of location. By using the trace of the information that's been saved in the terminal's memory, it can be set so that it'll be easier to determine whether the wireless terminal has gone into buildings and have the capability of checking if it has gone into a specific building. Likewise, while the terminal is turned on, in order calibrate the location, it needs to continuously work the GPS engine which leads to a rapid decrease in terminal's idle time. This thesis proposes some solutions regarding these issues - reducing 20 ~ 30% of the battery consumption for GPS visible situation that can occur when the wireless terminal periodically calibrates its location to determine the in-building status, and extending the idle time of the terminal by flexibly using the suggested GPS calibration time method according to wireless terminal's mobility.

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Mg-Al합금의 조성비율에 따른 발화온도특성

  • Han, U-Seop;Lee, Geun-Won
    • Proceedings of the Korea Institute of Fire Science and Engineering Conference
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    • 2013.04a
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    • pp.77-77
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    • 2013
  • 최근의 산업활동에서는 신규 원료 개발과 생산 효율성을 높이기 위하여 분체 공정이 증가하고 있는데, 미세 분진의 취급으로 분진운의 형성과 착화가 용이해지므로 분진폭발이나 화재 위험성이 증가하고 있다. 분진을 안전하게 사용하고 저장, 취급하기 위해서는 착화 전의 위험성 지표로서 최저발화온도(MIT ; Minimum Ignition Temperature)를 사전에 파악해 두는 것이 중요하다. 분진농도의 발화온도는 장치 내의 발화위험성이나 분진 취급 공정의 사고예방대책 관리를 위한 실용적 관점에서 중요하게 활용되는 폭발특성값이다. 또한 분진의 발화온도는 분진농도에 의존하며 농도변화에 따른 가장 낮은 온도를 MIT라고 한다. 본 연구에서는 화재폭발사고 빈도가 줄지 않고 있는 Mg 및 Mg-Al합금(60:40 wt%, 50:50 wt%, 40:60 wt%)을 대상으로 조성비율에 따른 최저발화온도를 실험적으로 조사하였다. Mg 및 Mg-Al(60:40 wt%), Mg-Al(50:50 wt%), Mg-Al(40:60 wt%) 시료의 평균입경은 142, 160, 151, $152{\mu}m$이다. MIT실험장치는 IEC 61241-2-1(Methods for Determining the Minimum Ignition Temperatures of Dust, 1994)에 준거하여 제작하여 사용하였다. 실험장치는 가열로, 분진운 시료홀더, 온도조절장치, 압축공기 제어장치 등으로 구성되어 있다. 구체적인 실험방법은 시험분진를 분진홀더에 장착하고 0.5 bar의 압축공기를 0.3 sec 동안 사용하여 일정 온도로 가열된 로의 내부로 분진운을 부유시킬 때에 분진운이 발화하여 가열로 하단부의 개방구에까지 화염이 전파하는지를 디지털비데오카메라로 기록, 평가하여 발화 유무를 판정하였다. Mg합금에 대한 MIT를 측정한 결과 $740^{\circ}C$가 얻어졌으며, Mg-Al(60:40 wt%)의 MIT는 $820^{\circ}C$로 조사되었다. 그러나 Mg-Al(50:50 wt%) 및 Mg-Al(40:60 wt%)에 대해서는 최대 가열로의 설정온도를 $890^{\circ}C$까지로 하여 농도를 변화시키면서 조사하였으나 발화가 일어나지 않았다. 문헌에 따르면 Mg입자 표면의 산화피막은 다공성으로 일정 온도에서 산화반응이 시간에 따라 직선적으로 증가하는데 반하여, Al의 산화피막은 보호 작용을 하여 일정 온도에서 산화반응속도가 표면과 내부의 농도 기울기에 의한 확산속도에 의존한다고 보고하고 있다. 본 연구결과를 토대로 Mg-Al합금의 발화특성을 고찰해 보면, Mg-Al합금에서 자기 전파성이 작은 Al성분의 증가는 착화지연이 증가하여 연소성이 감소하여 최저발화온도의 증가로 이어지는 것으로 추정되었다. 또한 발화온도는 주어진 조건의 온도장에서 분진이 존재하는 시간 길이에 따라 변화하므로, 발화온도를 실험적으로 측정하는 경우에는 측정장치나 방법에 따라 달라지므로 사업장의 현장에 발화온도를 적용하는 경우에는 장치 내의 분진의 존재시간을 고려할 필요가 있다.

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Comparative Analysis of Structural Damage Potentials Observed in the 9.12 Gyeongju and 11.15 Pohang Earthquakes (9.12 경주지진 및 11.15 포항지진의 구조손상 포텐셜 비교연구)

  • Lee, Cheol-Ho;Kim, Sung-Yong;Park, Ji-Hun;Kim, Dong-Kwan;Kim, Tae-Jin;Park, Kyoung-Hoon
    • Journal of the Earthquake Engineering Society of Korea
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    • v.22 no.3
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    • pp.175-184
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    • 2018
  • In this paper, comparative analysis of the 9.12 Gyeongju and 11.15 Pohang earthquakes was conducted in order to provide probable explanations and reasons for the damage observed in the 11.15 Pohang earthquake from both earthquake and structural engineering perspectives. The damage potentials like Arias intensity, effective peak ground acceleration, etc observed in the 11.15 Pohang earthquake were generally weaker than those of the 9.12 Gyeongju earthquake. However, in contrast to the high-frequency dominant nature of the 9.12 Gyeongju earthquake records, the spectral power of PHA2 record observed in the soft soil site was highly concentrated around 2Hz. The base shear around 2 Hz frequency was as high as 40% building weight. This frequency band is very close to the fundamental frequency of the piloti-type buildings severely damaged in the northern part of Pohang. Unfortunately, in addition to inherent vertical irregularity, most of the damaged piloti-type buildings had plan irregularity as well and were non-seismic. All these contributed to the fatal damage. Inelastic dynamic analysis indicated that PHA2 record demands system ductility capacity of 3.5 for a structure with a fundamental period of 0.5 sec and yield base shear strength of 10% building weight. The system ductility level of 3.5 seems very difficult to be achievable in non-seismic brittle piloti-type buildings. The soil profile of the PHA2 site was inversely estimated based on deconvolution technique and trial-error procedure with utilizing available records measured at several rock sites during the 11.15 Pohang earthquake. The soil profile estimated was very typical of soil class D, implying significant soil amplification in the 11.15 Pohang earthquake. The 11.15 Pohang earthquake gave us the expensive lesson that near-collapse damage to irregular and brittle buildings is highly possible when soil is soft and epicenter is close, although the earthquake magnitude is just minor to moderate (M 5+).

Analysis of Specific Contaminated Status and Pollutant Loads Contribution Rate of the Tributaries in Gumho and Nam River Basin (금호강, 남강 중권역 지류·지천의 상세오염 현황 및 오염기여율 조사)

  • Na, Seungmin;Kwon, Heongak;Kim, Gyeong Hoon;Shin, Dongseok;Im, Tae Hyo
    • Journal of Wetlands Research
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    • v.18 no.4
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    • pp.363-377
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    • 2016
  • This study was investigated the pollutant load, contamination properties, pollution condition of the fine parts of tributary, the influence of Nakdong river watershed and etc. in the tributaries. The contaminated tributaries were that among the Kumho and Nam river or were too far from site of water quality monitoring stations, regularly. As a result, the water quality level was almost similar between Nam and Kumho River, except for certain parameter including TN(Total Nitrogen), Chl-a(Chlorophyll-a) and SS(Suspended Solid) in which Kumho river were 20~120%. The point discharge load(kg/day) and load density ($kg/day/km^2$) of tributaries were different the pollution level according to the flow-rate ($m^3/sec$) and stream influence area($km^2$), and the difference of these was observed highly at Nam river. Specific contamination investigation of tributaries in Nam and Kumho river watershed was conducted from two to nine points of the fine parts of tributaries depending on the confluence sites and shapes. This result observed high at the Dalseocheon and Uriyeongcheon, respectively. Beside, the pollutant load contribution rate of Nakdong watershed was high about 10% at the Dalseocheon and Uiryeongcheon. This was due to the differences of the environments about the industrial complex, metropolis residence property, agricultural cultivation, livestock pen and the downstream of non-point source.

Analysis of epididymal sperm from Korean native bull (Hanwoo) aged at 8 and 15 months before freezing and after thawing

  • Kang, Sung-Sik;Cho, Sang-Rae;Kim, Ui-Hyung;Park, Chang-Seok;Kim, Hyeong-Cheol;Chung, Ki-Yong;Lee, Seok-Dong;Jang, Sun-Sik;Jeon, Gi-jun;Kim, Sidong;Lee, Myeong-Suk;Yang, Byoung-Chul
    • Journal of Embryo Transfer
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    • v.31 no.2
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    • pp.109-116
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    • 2016
  • The recovery of epididymal sperm in animals is considered as one of the important tools to preserve high value or endangered species. However, there are no appropriate castrating indicators such as months of age in bull, sperm morphology, and motility, particularly in young Korean native bull (Hanwoo). Therefore, this study aimed to investigate sperm number, morphology, and motility of sperm in the epididymis tail of young Hanwoo bulls at 8 and 15 months of age. After castration, epididymal tails were collected and minced with blades to recover sperm. In experiments 1 and 2, sperm number, morphology, and motility were examined. Total number of sperm and percentage of normal sperm from bulls at 8 months of age was lower than that of bulls at 15 months of age after collection (P<0.05). Percentage of abnormal head, tail, proximal cytoplasmic droplet, dead and damaged acrosome of sperm from bulls at 8 months of age were higher than those of bulls at 15 months of age (P<0.05). In experiment 3, sperm motility from bulls at 8 and 15 months of age were examined before freezing and after thawing. Frozen-thawed sperm at 8 months of age showed low total motility and motile sperm with ${\geq}25{\mu}m/sec$ compared to those at 15 months of age and commercially-used sperm (P<0.05). In conclusion, sperm derived from the epididymal tail of bulls at 8 months of age showed high abnormal morphology and poor motility, which are not adequate for AI and IVF. On the other hand, sperm derived from the epididymal tail of bulls at 15 months of age showed high normal morphology and motility.

BGK 수치기법을 이용한 로켓 노즐 내의 유동장 해석

  • 신동신;이재성
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2000.04a
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    • pp.16-16
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    • 2000
  • 충격파를 포함하는 초음속 유동을 해석하는 수치해법 중에서 많이 사용되어진 것은 엄밀 및 근사 리만 해법과 플럭스 분할 기법들로서 이들은 Euler 방정식에 기반을 두고 선형 또는 비선형파의 상호작용을 풍상 차분법으로 기술하는 방법들이다. 이러한 수치기법들은 과거 광범위하게 사용되어 왔으나 최근 여러 가지 단점이 발견되었다. 이와 같은 문제점을 극복하고자 입자의 통계적인 운동을 기술하는 기체 운동론에 근거하여 BGK 수치기법이 제시되었다. 이는 비충돌 볼츠만 방정식으로부터 입자의 수준에서 플럭스 분할 기법 형태의 풍상차분법을 구현하는 것으로 볼츠만 방정식의 충돌항을 BGK 모델로 대치하고 이것의 적분해로부터 수치 플럭스를 구한다. 이 수치기법은 기존의 리만해법에 비하여 수치적으로나 물리적으로 매우 타당한 성질인 강건성, 정확성, 엔트로피 조건, 양수보존성 등을 가지고 있음이 밝혀졌다. 이와 같은 수치기법을 사용하여 로켓 노즐 내의 아음속, 천이음속, 초음속에서의 유동장 해석을 위한 프로그램을 작성하였다. 시간 적분에 대하여는 정상 상태의 계산을 위하여 내재적 시간 적분 방법을 사용하였으며, 공간 이산화 방법으로는 임의의 제어체적에 대하여 적분형 보존 방정식을 적용하는 유한 체적법을 사용하였다. 초음속 입구 유동과 출구에서 초음속과 저음속 유동의 두가지 경우를 고려하여 얻은 결과를 기존의 연구 결과와 비교하여 본 결과 잘 일치하였다. 입구 유동이 저음속이고 출구 유동이 초음속인 경우에 대하여도 해석결과가 실험결과와 잘 일치하였다. 상대적으로 낮은 온도, 압력 조건과 높은 온도, 압력 조건을 가지는 고체 로켓 모터 노즐 내의 유동을 해석하였다. 이들 해석 결과를 전압, 전온도로 표준화시킨 결과 서로 일치하였으며, 파라서 저온, 저압에서 얻은 결과도 표준화시킬 경우, 고온, 고압에서도 사용될 수 있음을 알 수 있었다.의 영향에 초점을 맞추었다.다고 판단되며 배기 가스 자체에 대기 공기중에 함유되어 있던 습기가 얼어붙는(Icing화) 문제가 발생하기 때문에 배기가스의 Icing을 방지하기 위하여 압축기 끝단에서 공기를 추출하여 배기부분에 송출할 필요성이 있는 것으로 판단되었다. 출구가스의 기체 유동속도가 매우 빠르므로 (100-l10m.sec) 이를 완화하기 위한 디퓨저의 설계가 요구된다고 판단된다. 또 연소기 후방에 물을 주입하는 경우 열교환기 및 기타 부분품에 발생할 수 있는 부식 및 열교환 효율 저하도 간과할 수 없는 문제로 파악되었다. 이러한 기술적 문제가 적절히 해결되는 경우 비활성 가스 제너레이터는 민수용으로는 대형 빌딩, 산림, 유조선 등의 화재에 매우 적절히 사용되어 질 수 있을 뿐 아니라 군사적으로도 군사작전 중 및 공군 기지의 화재 그리고 지하벙커에 설치되어 있는 고급 첨단 군사 장비 등의 화재 뿐 아니라 대간첩작전 등에 효과적으로 활용될 수 있을 것으로 판단된다.가 작으며, 본 연소관에 충전된 RDX/AP계 추진제의 경우 추진제의 습기투과에 의한 추진제 물성 변화는 미미한 것으로 나타났다.의 향상으로, 음성개선에 효과적이라고 사료되었으며, 이 방법이 편측 성대마비 환자의 효과적인 음성개선의 치료방법의 하나로 응용될 수 있으리라 생각된다..7%), 혈액투석, 식도부분절제술 및 위루술·위회장문합술을 시행한 경우가 각 1례(2.9%)씩이었다. 13) 심각한 합병증은 9례(26.5%)에서 보였는데 그중 식도협착증이 6례(17.6%), 급성신부전증 1례(2.9%), 종격동기흉과 폐염이 병발한 경우와 폐염이 각 1례(2.9%)였다. 14) 식도경 시행회수는 1회가 17례(54.8%), 2회가 9례(29.0%), 3회 이상이 5례(16.1%)였다.EX>$IC_{50}$/ 값이 210 $\mu\textrm{g}$<

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음향공에 의한 LOX-RP1 고주파 음향-연소안정화에 관한 연구

  • 이길용;윤웅섭;조용호
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2000.04a
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    • pp.5-5
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    • 2000
  • 액체 추진 로켓 엔진의 고주파 연소 불안정 관련 이론은 대체로 연소기 내부의 음향 공명 모드와 분무 연소 과정의 상호 작용을 구동 메커니즘으로 전제하며 Rayleigh Criterion의 재해석에 기초하여 불안정성 평가를 위한 매개변수를 도입하고 연소 불안정성을 예측한다. 여기에는 음향장 분석 이론, 음향 불안정 이론, 연소응답 및 기화반응 이론 등이 포함된다. 본 연구에서는 LOX/RPl 추진제 조합의 액체 추진 로켓 엔진 연소기를 대상으로 다차원 순수 음향장 해석과 연소-음향장 분석을 통해 대상 엔진의 고주파 연소 불안정 특성을 예측하였다. 수동 제어 기기인 음향공 설치에 따른 연소기의 음향장 및 연소-음향장의 특성 변화를 고찰하고 위 결과를 종합하여 음향공의 연소 불안정 억제 성능 및 대상 엔진의 연소 불안정성을 평가하였다. 연소기 형상 및 음향공 설치에 따른 다차원 순수 음향장 해석은 상용코드인 ANSYS를 사용하여 수행하였다. 내부 유체는 압축성, 비점성 유체로 유체의 평균 유동은 무시하며 위치에 관계없이 균일한 물성치를 부여하였다. 정상상태 연소과정을 가정하고 평형 화학을 이용한 분석 결과로부터 연소 기체의 관련 물성치를 결정하였다. 연소기 길이 방향, 반경 방향, 원주 방향 격자점들의 음향 특성을 주파수 영역에 대해 해석하고 3차원 음향 모드 형상을 토대로 음향장을 분석하였다. 연소-음향장 해석은 음향 불안정 이론 중 n- $\tau$ 2 매개변수 기법을 사용하였다. 연료 액적의 분무 연소 과정을 1차원적으로 가정하고 정상상태의 평형 화학 계산 결과를 이용하여 엔진의 연소면을 1차원적으로 설정하였다. 상류 연소응답과 중립 안정 곡선을 토대로 대상 엔진의 연소 불안정 특성을 분석하였다.구 분석 결과 기술적 문제점으로는 배기 가스온도가 낮은데 따른 출구 부분의 Bearing, Sealing이 문제가 될 수 있다고 판단되며 배기 가스 자체에 대기 공기중에 함유되어 있던 습기가 얼어붙는(Icing화) 문제가 발생하기 때문에 배기가스의 Icing을 방지하기 위하여 압축기 끝단에서 공기를 추출하여 배기부분에 송출할 필요성이 있는 것으로 판단되었다. 출구가스의 기체 유동속도가 매우 빠르므로 (100-l10m.sec) 이를 완화하기 위한 디퓨저의 설계가 요구된다고 판단된다. 또 연소기 후방에 물을 주입하는 경우 열교환기 및 기타 부분품에 발생할 수 있는 부식 및 열교환 효율 저하도 간과할 수 없는 문제로 파악되었다. 이러한 기술적 문제가 적절히 해결되는 경우 비활성 가스 제너레이터는 민수용으로는 대형 빌딩, 산림, 유조선 등의 화재에 매우 적절히 사용되어 질 수 있을 뿐 아니라 군사적으로도 군사작전 중 및 공군 기지의 화재 그리고 지하벙커에 설치되어 있는 고급 첨단 군사 장비 등의 화재 뿐 아니라 대간첩작전 등에 효과적으로 활용될 수 있을 것으로 판단된다.가 작으며, 본 연소관에 충전된 RDX/AP계 추진제의 경우 추진제의 습기투과에 의한 추진제 물성 변화는 미미한 것으로 나타났다.의 향상으로, 음성개선에 효과적이라고 사료되었으며, 이 방법이 편측 성대마비 환자의 효과적인 음성개선의 치료방법의 하나로 응용될 수 있으리라 생각된다..7%), 혈액투석, 식도부분절제술 및 위루술·위회장문합술을 시행한 경우가 각 1례(2.9%)씩이었다. 13) 심각한 합병증은 9례(26.5%)에서 보였는데 그중 식도협착증이 6례(17.6%), 급성신부전증 1례(2.9%), 종격동기흉과 폐염이 병발한 경우와 폐염이 각 1례(2.9%)였다. 14)

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Effect of Different Heel Plates on Muscle Activities During the Squat (스쿼트 동작 시 발뒤꿈치 보조물 경사각에 따른 하지근과 척추기립근의 근육활동 비교)

  • Chae, Woen-Sik;Jeong, Hyeun-Kyeong;Jang, Jae-Ik
    • Korean Journal of Applied Biomechanics
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    • v.17 no.2
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    • pp.113-121
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    • 2007
  • The purpose of this study was to determine the effect of three different plates($0^{\circ}$, $10^{\circ$}, $20^{\circ}$)under heels on the lower limb muscles and erector spinae during squat exercise. Ten high school korean traditional wrestling players(age: $18.5{\pm}0.7$, weight: $1972.2{\pm}128.5N$, height: $177.8{\pm}6.0cm$, weight of barbell: $1004.5{\pm}132.4N$) performed squat exercise using three different tilting plates under heels at a cadence of 40beats/sec with 80% one repetition maximum load. Surface electrodes were placed on the participants' left and right erector spinae, and rectus femoris, vastus medialis, vastus lateralis, tibialis anterior, biceps femoris, medial gastrocnemius, and lateral gastrocnemius in the right lower extremity. One S-VHS camcorder(Panasonic AG456, 60fields/s) was placed 10m to the side of the participant. To synchronize the video and EMG data, a synchronization unit was used for this study. Average and Peak IEMG values were determined for each participant. For each variable, a one-way analysis of variance was used to determine whether there were significant differences among three different tilting plates under heels. When a significant difference was found in plates type, post hoc analyses were performed using the Tukey procedure. A confidence level of p<.05 was used to determine statistical significance. As a result of this study, maximum nEMG values of the tibialis anterior in $0^{\circ}$ plates was significantly higher than the corresponding values for the other plates during the knee extension. This increased activation in the tibialis anterior muscle indicates an increase in displacement of center of gravity of body. It is very likely that additional muscle activation are needed to stop the forward and backward movement. The results also showed that muscular activities of quadriceps femoris and erector spinae were decreased with increasing angle of plates. This suggests that increasing angle of plate may help to sustain the balance and posture of squat exercise. It is considered that very few significant differences were found among three different plates($0^{\circ}$, $10^{\circ}$, $20^{\circ}$) since elite players with much experience in squat exercise, were chosen as a participant of this study. In order to obtain meaningful results regarding the tilting angle of heel plates in squat exercise, kinetic and 3D kinematic analysis will be needed in the future study.