• Title/Summary/Keyword: STL File

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The dimension analysis of prepared natural teeth for developing customized zirconia block (맞춤형 지르코니아 블락 제작을 위한 삭제된 치아의 평균 크기 분석)

  • Kim, Min-Hyuk;Kim, Sung-Hun;Yeo, In-Sung;Yoon, Hyung-In;Lee, Jae-Hyun;Han, Jung-Suk
    • The Journal of Korean Academy of Prosthodontics
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    • v.55 no.4
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    • pp.381-388
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    • 2017
  • Purpose: Unpredictable shrinkage of zirconia during sintering process causes discrepancy. Therefore, there have been attempts to reduce discrepancy by milling zirconia after sintering. However, due to the hardness of sintered zirconia, milling takes longer time, causes damage to the machine and causes chip formation. With customized zirconia block using the mean dimension of prepared natural dentition, it is expected to overcome these shortcomings. Materials and methods: The mean dimension of prepared natural dentition was analyzed as STL file after scanning of prepared teeth treated at SNUDH. The transverse, frontal and sagittal planes were set using Mimics and Photoshop. 3D volume was projected on each plane, and the outer line was measured through external tangent line, and the inner line was measured through inflection point of tangent line. Results: The mean height of prepared incisal (N = 57) is $6.60{\pm}1.05mm$, mesiodistal length is $2.98{\pm}0.73mm$, buccolingual length is $2.04{\pm}0.73mm$. The mean height of prepared premolar (N = 15) is $5.37{\pm}1.49mm$, mesiodistal length is $4.10{\pm}1.78mm$, buccolingual length is $5.86{\pm}1.55mm$. And the mean height of prepared molar (N = 13) is $5.11{\pm}1.29mm$, mesiodistal length is $6.80{\pm}1.18mm$, buccolingual length is $7.34{\pm}1.40mm$. Conclusion: Using the mean dimension of prepared natural dentition, it is expected to be able to fabricate customized zirconia block.

A Study on Developing Customized Bolus using 3D Printers (3D 프린터를 이용한 Customized Bolus 제작에 관한 연구)

  • Jung, Sang Min;Yang, Jin Ho;Lee, Seung Hyun;Kim, Jin Uk;Yeom, Du Seok
    • The Journal of Korean Society for Radiation Therapy
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    • v.27 no.1
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    • pp.61-71
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    • 2015
  • Purpose : 3D Printers are used to create three-dimensional models based on blueprints. Based on this characteristic, it is feasible to develop a bolus that can minimize the air gap between skin and bolus in radiotherapy. This study aims to compare and analyze air gap and target dose at the branded 1 cm bolus with the developed customized bolus using 3D printers. Materials and Methods : RANDO phantom with a protruded tumor was used to procure images using CT simulator. CT DICOM file was transferred into the STL file, equivalent to 3D printers. Using this, customized bolus molding box (maintaining the 1 cm width) was created by processing 3D printers, and paraffin was melted to develop the customized bolus. The air gap of customized bolus and the branded 1 cm bolus was checked, and the differences in air gap was used to compare $D_{max}$, $D_{min}$, $D_{mean}$, $D_{95%}$ and $V_{95%}$ in treatment plan through Eclipse. Results : Customized bolus production period took about 3 days. The total volume of air gap was average $3.9cm^3$ at the customized bolus. And it was average $29.6cm^3$ at the branded 1 cm bolus. The customized bolus developed by the 3D printer was more useful in minimizing the air gap than the branded 1 cm bolus. In the 6 MV photon, at the customized bolus, $D_{max}$, $D_{min}$, $D_{mean}$, $D_{95%}$, $V_{95%}$ of GTV were 102.8%, 88.1%, 99.1%, 95.0%, 94.4% and the $D_{max}$, $D_{min}$, $D_{mean}$, $D_{95%}$, $V_{95%}$ of branded 1cm bolus were 101.4%, 92.0%, 98.2%, 95.2%, 95.7%, respectively. In the proton, at the customized bolus, $D_{max}$, $D_{min}$, $D_{mean}$, $D_{95%}$, $V_{95%}$ of GTV were 104.1%, 84.0%, 101.2%, 95.1%, 99.8% and the $D_{max}$, $D_{min}$, $D_{mean}$, $D_{95%}$, $V_{95%}$ of branded 1cm bolus were 104.8%, 87.9%, 101.5%, 94.9%, 99.9%, respectively. Thus, in treatment plan, there was no significant difference between the customized bolus and 1 cm bolus. However, the normal tissue nearby the GTV showed relatively lower radiation dose. Conclusion : The customized bolus developed by 3D printers was effective in minimizing the air gap, especially when it is used against the treatment area with irregular surface. However, the air gap between branded bolus and skin was not enough to cause a change in target dose. On the other hand, in the chest wall could confirm that dose decrease for small the air gap. Customized bolus production period took about 3 days and the development cost was quite expensive. Therefore, the commercialization of customized bolus developed by 3D printers requires low-cost 3D printer materials, adequate for the use of bolus.

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Comparative accuracy of implant impression techniques with different splinting materials (임플란트 인상채득 방법과 인상용 코핑 연결 고정에 따른 정확성 비교)

  • Ki-Yoon Hong;Soo-Yeon Shin
    • Journal of Dental Rehabilitation and Applied Science
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    • v.39 no.1
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    • pp.9-20
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    • 2023
  • Purpose: We investigated the effect of open tray impression using pick-up impression coping and close tray impression using transfer impression coping on the accuracy of impression in edentulous patients on their mandibular parts. the effect of material types of pick-up type impression copings for splinting in open tray impression on the accuracy of impression was also evaluated. Materials and Methods: Two implant fixtures were implanted in parallel in the left molar of the mandibular in the shape of a mandibular partial edentulous model. The 40 individual trays were fabricated using 3D printer. The prepared individual trays were classified into 4 groups (i.e., PN, PG, PH, and TN groups), and a total of 40 impression-takings were conducted. A master cast was connected to a Scan Body. The converted STL file was super-imposed on the scan images of the various groups. Results: The order of standard deviation values decreased as follows: PN (0.2343 ± 0.0844 mm), TN (0.2192 ± 0.0840 mm), indicating that the high accuracy of impression for TN group. In addition, for the comparison results between the material types used in splinting the open tray impression, the PH group showed a relatively lower standard deviation (0.1910 ± 0.1176 mm) than that of the PN group (0.2343 ± 0.0844 mm), PG group (0.2556 ± 0.1082 mm). Conclusion: The acrylic resin synthesized by light-induced polymerization exhibited a higher accuracy of impression taking than that of autopolymerizing acrylic resin. Meanwhile, the accuracy of impression taking was not dependent on the implant impression taking method or the presence of connection/fixation of impression copings.