• Title/Summary/Keyword: Production-process Improvement

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Thermophilic Anaerobic Digestion of Polyhydroxybutyrate with and without Thermo-alkaline Pretreatment (열적-알칼리성 전처리 유무에 따른 폴리하이드록시부티레이트의 고온 혐기성 소화 영향 연구)

  • Jihyeon Lee;Joonyeob Lee
    • Journal of Environmental Science International
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    • v.33 no.2
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    • pp.121-129
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    • 2024
  • The study investigated the effect of thermo-alkaline pretreatment on the solubilization of polyhydroxybutyrate (PHB) and its potential to enhance of thermophilic anaerobic digestion, focusing on biochemical methane potential (BMP) and methane production rate, using two different particle sizes of PHB (1500 ㎛ and 400 ㎛). Thermo-alkaline pretreatment tests were conducted at 90 ℃ for 24 hours with varying NaOH dosages from 0-80% (w/w). BMP tests with untreated PHB exhibited methane production ranging from 150.4~225.4 mL CH4/g COD and 21.5~24.2 mL CH4/g VSS/d, indicating higher methane production for smaller particle sizes of PHB, 400 ㎛. Thermo-alkaline pretreatment tests achieved a 95.3% PHB solubilization efficiency when 400 ㎛ PHB particles were treated with 80% NaOH dosage at 90 ℃ for 24 hours. BMP tests with pretreated PHB showed substantial improvement in thermophilic anaerobic digestion, with an increase of up to 112% in BMP and up to 168% in methane production rate. The results suggest that a combined pretreatment process, including physical (400 ㎛ PHB particles) and thermo-alkaline (90 ℃, 40-80% NaOH dosage, and 24 hours reaction time), is required for high-rate thermophilic anaerobic digestion of PHB with enhanced methane production.

A Proposal for the Improvement Method of Order Production System in the Display Industry (디스플레이산업에서 수주생산방식의 개선 및 효율화 제고 방안)

  • Cho, Myong Ho;Cho, Jin Hyung
    • Journal of Korean Society of Industrial and Systems Engineering
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    • v.39 no.4
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    • pp.106-116
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    • 2016
  • MTO (Make to Order) is a manufacturing process in which manufacturing starts only after a customer's order is received. Manufacturing after receiving customer's orders means to start a pull-type supply chain operation because manufacturing is performed when demand is confirmed, i.e. being pulled by demand (The opposite business model is to manufacture products for stock MTS (Make to Stock), which is push-type production). There are also BTO (Build to Order) and ATO (Assemble To Order) in which assembly starts according to demand. Lean manufacturing by MTO is very efficient system. Nevertheless, the process industry, generally, which has a high fixed cost burden due to large-scale investment is suitable for mass production of small pieces or 'mass customization' defined recently. The process industry produces large quantities at one time because of the lack of manufacturing flexibility due to long time for model change or job change, and high loss during line-down (shutdown). As a result, it has a lot of inventory and costs are increased. In order to reduce the cost due to the characteristics of the process industry, which has a high fixed cost per hour, it operates a stock production system in which it is made and sold regardless of the order of the customer. Therefore, in a business environment where the external environment changes greatly, the inventory is not sold and it becomes obsolete. As a result, the company's costs increase, profits fall, and it make more difficult to survive in the competition. Based on the customer's order, we have built a new method for order system to meet the characteristics of the process industry by producing it as a high-profitable model. The design elements are designed by deriving the functions to satisfy the Y by collecting the internal and external VOC (voice of customer), and the design elements are verified through the conversion function. And the Y is satisfied through the pilot test verified and supplemented. By operating this make to order system, we have reduced bad inventories, lowered costs, and improved lead time in terms of delivery competitiveness. Make to order system in the process industry is effective for the display glass industry, for example, B and C groups which are non-flagship models, have confirmed that the line is down when there is no order, and A group which is flagship model, have confirmed stock production when there is no order.

Study on forming Process of Piston Crown Using Near Net Shaping Technology (재료이용율 향상을 위한 피스톤 크라운 성형공정 연구)

  • Choi, H.J.;Choi, S.;Yoon, D.J.;Jung, H.S.;Choi, I.J.;Baek, D.K.;Choi, S.K.;Park, Y.B.;Lim, S.J.
    • Proceedings of the Korean Society for Technology of Plasticity Conference
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    • 2008.10a
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    • pp.197-198
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    • 2008
  • The forging process produces complicated and designed components in a die at high productivity for mass production and minimizes the machining amount for favorable material utilization; the forging products used at highly stressed sections are well accepted at a wide range of industry such as automobile, aerospace, electric appliance and et cetera. Accordingly, recent R&D activities have been emphasized on improvement of forging die-life and near net shaping technology for cost effectiveness and better performance. Usually closing and consolidation of internal void defects in a ingot is a vital matter when utilized as large forged products. It is important to develop cogging process for improvement of internal soundness without a void defect and cost reduction by solid forging alone with limited press capacity. For experiments of cogging process, hydraulic press with a capacity of 800 ton was used together with a small manipulator which was made for rotation and overlapping of a billet. Size of a void was categorized into two types; ${\phi}$ 6.0 mm and ${\phi}$ 9.0 mm to investigate the change of closing and consolidation of void defects existed in the large ingot during the cogging process. In addition for forming experiment of piston grown air drop hammer with a capacity of 16 ton was used. The experiment with piston crown was carried out to show the formability and void closing status. In this paper systematic configuration for closing process of void defects were expressed based on this experiment results in the cogging process. Also forging defects through forming process for piston crown was improved using the experiment results and FE analysis. Consequently this paper deals with the effect of radial parameters in cogging process on a void closure far large forged products and formability of piston crown.

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Improvement of the Thermochemical water-splitting IS Process Using the Membrane Technology (분리막 기술을 이용한 열화학적 수소제조 IS[요오드-황] 프로세스의 개선)

  • Hwang, Gab-Jin;Kim, Jong-Won;Sim, Kyu-Sung
    • Transactions of the Korean hydrogen and new energy society
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    • v.13 no.3
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    • pp.249-258
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    • 2002
  • Thermochemical water-splitting IS(Iodine-Sulfur) process has been investigating for large-scale hydrogen production. For the construction of an efficient process scheme, two kinds of membrane technologies are under investigating to improve the hydrogen producing HI decomposition step. One is a concentration of HI in quasi-azeotropic HIx ($HI-H_2O-I_2$) solution by elecro-electrodialysis. It was confirmed that HI concentrated from the $HI-H_2O-I_2$ solution with a molar ratio of 1:5:1 at $80^{\circ}C$. The other is a membrane reactor to enhance the one-pass conversion of thermal decomposition reaction of gaseous hydrogen iodide (HI). It was found from the simulation study that the conversion of over 0.9 would be attainable using the membrane reactor using the gas permeation properties of the prepared silica hydrogen permselective membrane by chemical vapor deposition (CVD). Design criterion of the membrane reactor was also discussed.

A Study on the Fabrication and Performance Evaluation of Worm Gear Reducer (웜기어 감속기 제작 및 성능평가에 관한 연구)

  • Lee, Dong Gyu;Zhen, Qin;Jeon, Min Hyong;Kim, Lae Sung;Lyu, Sung-Ki
    • Journal of the Korean Society of Manufacturing Process Engineers
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    • v.17 no.1
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    • pp.1-7
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    • 2018
  • We aimed to develop a high quality 3.5 ton class swing reducer by studying the efficiency improvement of the reducer through the optimum design and performance evaluation of the assembled, high efficiency, lightweight 3.5 ton swing reducer. Based on the optimal design of the worm and worm wheel, the optimal manufacturing method of the worm wheel, the optimized casing design, and the optimum design of the output pinion, Respectively. Therefore, in this paper, to improve the efficiency of the worm gear reducer system, we will develop the manufacturing technology and verify the mass production by combining the manufacturing process design, processing and assembling technology according to the optimization design. We have conducted research to realize mass production by product verification such as product efficiency, reliability and durability according to optimal design of worm gear reducer.

A study on method for reducing haze defects of head lamp for automobiles (자동차용 헤드램프의 플라스틱 소재 Haze 저감 방법에 관한 연구)

  • Lee, Seung-Wook;Lee, Chun-Kyu
    • Design & Manufacturing
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    • v.15 no.4
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    • pp.32-36
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    • 2021
  • In this study, the cause of the decrease in transmittance of the outer lens among the causes of the decrease in the amount of light in the automobile headlamp was identified, and the improvement method was selected to determine the effect. The causes of defects that lower the transmittance of the outer lens are divided into a moisture problem and a haze problem. The moisture problem is caused by the temperature difference between the inside and the outside of the head lamp, and the haze problem occurs when the heat inside the head lamp evaporates the haze component contained in the plastic material and attaches it to the outer lens. In order to improve the haze problem that occurs in plastic raw materials, the structures of the bulb light source type headlamp and the LED chip light source type headlamp were analyzed. Among them, the housing material of the LED chip light source type headlamp, which is structurally prone to haze gas, was selected as the test target. In the mass-production injection process of the housing, the drying process was selected as a method to minimize haze gas without adding a separate production process. After extracting a sample every drying time at a constant drying temperature, the sample was put into a haze tester and the residual amount of haze gas was measured. As a result, it was confirmed that the residual amount of Haze gas in the material decreased as the drying time increased.

A Study on the Optimization of Servo System Originating to High-Speed Fixed Duty Processing (고속 고정도가공에 기인하는 Servo System의 최적화와 기능특성에 관한 연구)

  • Lee, Hong-Gil;Kim, Won-il;Choi, Myung-Hwan;Baek, Sang-Yeob
    • Journal of the Korean Society of Manufacturing Process Engineers
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    • v.8 no.2
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    • pp.18-24
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    • 2009
  • The most dominate aspect in machine works using CNC devices in industrial production processes is the precision of the product and the Cycle Time. To this day, many studies on the external factors of the technology to reduce the Cycle Time have advanced amid to the advancements in cam soft development for manual programs and the numerous studies on high speed and precision machining. This study experimented various functions of the sequence pattern flow and arranged system development technologies of past few years to develop and applicate various usage of adjustment factors within the CNC, so it would be more understandable to the user and would enable them to make high speed and precision products more faster develop and. In order to reduce the Cycle Time, the mechanism of machine tools has to be analysed and applied, in addition to program reduction and improvement of the manufacture process.

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A Study on the Manufacturing of Die and Improvement of Process in Fiorging Work of Alternator Rotor Pole (앨터네이터 로터폴의 단조가공에서 공전개선과 금형제작에 관한 연구)

  • 김세환
    • Proceedings of the Korean Society of Machine Tool Engineers Conference
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    • 1997.04a
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    • pp.54-61
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    • 1997
  • Furthermore the rothor pole, with a solid type, manufactured by cold forging process at present should dmploy 3 press lines which consist of total 7 processes. Since A.S.B. treatment is prerequisite for the press line, the 3 times of A.S.B. treatment requires a long lead time, with little contribution to the reduction in cost. The author has investigated, through this researach, the possibility of a new forging method for a rotor pole production with (1) 2 pass instead of 3 press lines (2) only one A.S.B. treatment instead of 3 ones (3) solid type instead of sectional type, and (4) improvment of material property during process using a modified forging process and a specially designed die.

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High Brightness Prism Light-guide Plate for TFT-LCDs Using Optical Simulation and Novel Injection Mold Process (광학시뮬레이션과 새로운 사출성형법을 사용한 TFT-LCD용 고휘도 프리즘 도광판)

  • Han, Jeong-Min;Shon, Jin-Geun
    • The Transactions of the Korean Institute of Electrical Engineers P
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    • v.61 no.2
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    • pp.93-96
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    • 2012
  • We have designed high performance prism light-guide plate (LGP) in 17 inch TFT-LCD. In test result to embody high brightness BLU in case of LGP of base and upper surface with 17 inch, thickness 8mm adding prism construct. Using optical simulation, we forecast the brightness and uniformity in LGP with prism structure. And we adopted novel injection mold method and Nickel stamper to make actual evolution sample. Novel injection mold process has steady heating time zone in heat cycle time of injection mold process. For this novel heat cycle control, we achieved above 90[%] height prism structure as our design. It is superior brightness improvement than previous that of printing form about some 20[%] and in this course to embody actual material it succeeded prism LGP production by 17 inch injection form process.

Evaluation of Physical Shear Pre-treatment and Biogas Characteristics using Mixed Sludge (물리적 파쇄 가용화를 이용한 혼합슬러지의 가용화 효율 및 바이오가스 특성 평가)

  • Choi, Jae-Hoon;Jeong, Seong-Yeob;Kim, Ji-Tae
    • Journal of Korean Society on Water Environment
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    • v.35 no.4
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    • pp.362-369
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    • 2019
  • In this study, biodegradation efficiency improvement of mixed sludge for the anaerobic digestion process in wastewater treatment plant was investigated. In order to release the organic material contained in the sludge cell and promote the hydrolysis step, mixed sludge of 7% TS (Total Solids) was physically shear-treated at a shear strength of 1,000 ~ 4,000 rpm and a maximum of 120 mins. As a result of the comparison between mixed sludge before and after the treatment, the concentration of $SCOD_{Cr}$(Soluble Chemical Oxygen Demand-chromium method) was increased through the conversion of granular organic matter into dissolved organic matter as shear strength and treatment time increases. The solubilization efficiency increased rapidly after 30 min of solubilization application time, and they were 11.23 %, 20.10 %, 22.52 % and 25.43% at 120 min for each shear strength conditions, respectively. Additionally, the BMP(Biochemical Methane Potential) test was conducted with the optimized samples to determine the increase of methane production by the shear pre-treatment. Consequently, methane production of each samples were 0.275, 0.310, 0.323 and $0.335m^3/kg\;VS_{add}$, which indicates that methane production was increased to a maximum of 21.28% compared to the control without the solubilization process ($0.262m^3/kg\;VS_{add}$). As a result, the physical shear-treatment is a promising process for sewage sludge pre-treatment to reduce the organic waste and increase the energy production.