• Title/Summary/Keyword: Product Defects

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Development of Spur Gear Parts for Automotive Actuators using Precision Cold Forging Technology (정밀냉간단조 기술을 적용한 자동차 액추에이터용 스퍼기어 부품개발)

  • D. H. Park;S. C. Han
    • Transactions of Materials Processing
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    • v.32 no.6
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    • pp.335-343
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    • 2023
  • Spur Gear parts for automobile actuators using existing former forging technology were produced in a total of three processes on a former forging machine. However, in order to improve cost increase due to frequent mold breakage, Spur Gear parts were designed and manufactured in the cold forging process after forming the preform through former forging. In other words, in the existing former forging mold, product seating defects occurred due to horizontal movement, resulting in many product defects and mold damage, so there was an urgent need to improve mold life and product defects. In order to improve this, we tried to improve the mold life by improving the existing 3 former forging processes to a former forging process and 2 cold forging processes. Therefore, We developed Spur Gear parts for automobile actuators were developed by applying precision cold forging technology through a former forging process and 2 cold forging processes to improve mold life.

An Exploratory Study of Consumer Return Experiences (소비자 반품경험에 관한 탐색적 연구)

  • Park Kyung-Ae
    • Journal of the Korean Society of Clothing and Textiles
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    • v.30 no.6 s.154
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    • pp.961-970
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    • 2006
  • This study attempted to understand post-purchase consumer return experiences which had not received much attention in consumer behavior research. As a first step to understand return experiences from consumers' viewpoint, the study took an exploratory approach and identified themes and patterns from subjective consumer experiences. Whenever possible, attribution theory was applied to interpret the identified patterns. A total of 99 cases were collected from an open-ended questionnaire and analyzed based on a qualitative method. The reasons of product return was classified into five groups: changing mind; product defects; unsuitable products; products not expected; and for a better deal. External attribution was observed for return decisions caused by consumers' changed mind as well as by product defects. Dissatisfaction with defected products seemed to be intensified or reduced by service failure or success in the post-purchase service encounter. Consumer expectation and situations seemed to affect this process. Overall, the study supported attribution theory in the post-purchase return experience, and insights for research questions were proposed.

Nondestructive Internal Defects Evaluation for Pear Using NIR/VIS Transmittance Spectroscopy

  • Ryu, D.S.;Noh, S.H.;Hwnag, H.
    • Agricultural and Biosystems Engineering
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    • v.4 no.1
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    • pp.1-7
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    • 2003
  • Internal defects such as browning of the flesh and blackening and rot of the ovary of pear can be easily developed because of the inadequate environmental conditions during the storage and distribution of fruit. The quality assurance system for the agricultural product is to be settled in Korea. All defected agricultural products should be excluded prior to the distribution to enhance the commercial values. However, early stage on-line defect detection of agricultural product is very difficult and even more difficult in a case of the internal defects. The goal of this research is to develop a system that can detect and classify internal defects of agricultural produce on-line using VIS/NIR transmittance spectroscopy. And Shingo pear, which is one of the famous species of Korean pear, was used for the experiment. Soft independence modeling of class analogy (SIMCA) algorithm was employed to analyze the transmittance spectroscopic data qualitatively. On-line classification system was constructed and classification model was developed and validated. As a result, the correct classification rate (CCR) using the developed classification model was 96.1 %.

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A study on the reduction of blow hole defects in aluminum sand casting (알루미늄 사형주조에서 기공 결함 감소를 위한 연구)

  • Lee, Dong-Youn;Lee, Chun-Kyu
    • Design & Manufacturing
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    • v.14 no.4
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    • pp.52-57
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    • 2020
  • In this study attempted to prevent defects due to blow holes among defects of sand casting products. It was intended to reduce the defect rate by reducing the blow hole of the inner surface. Currently, expectations and requirements for the quality level of non-ferrous aluminum casting in the casting industry are increasing. In addition, the shape is complex and the shrinkage precision is required. Among them, the test prototype is expensive to manufacture the mold, and the production time is also long, and the product is manufactured by sand casting. At this time, the highest defect rates are defects caused by shrinkage defects, surface defects, and blow holes.. At this study, the manufacturing time was shortened by using the shape of the fluid movement path in advance. Also, it is possible to reduce defects due to blow holes.

Analysis of defects caused by halo defects during injection molding (사출성형 중 달무리 현상에 의한 불량에 대한 분석)

  • Lee, Soon-Young;Park, Eun-Min;Kim, Do-Hun;Kim, Yong-Chul;Yang, Chul-Seung;Jin, Gyeong-Min;Kim, Sun-Kyoung
    • Design & Manufacturing
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    • v.13 no.4
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    • pp.57-62
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    • 2019
  • In this study, we investigated the halo surface defection of various phenomenon occurred during the injection molding process which is caused by the thinning of the product thickness and the importance of the appearance. Surface analysis was performed to observe the difference between the surface where defects appeared and the surface which did not appear. Based on these results, we analyzed the phenomenon of halo surface defects was caused by unstable flow of resin generated in injection molding and velocity change of flow front. Furthermore, we will conduct a clear analysis of halo surface defects through observations through optical microscopy and subsequent observations with atomic force microscope. It has been analyzed that halo in PP is due to the rheological difference between the crystalline and amorphous regions while that in PC/ABS is due to shear separation of PC and ABS.

Design of Hexagonal Fitting Nut Preform Considering a Ductile Fracture (연성파괴를 고려한 6각 피팅 너트 예비성형체 설계)

  • 김동환;이정민;김병민
    • Transactions of Materials Processing
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    • v.13 no.4
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    • pp.359-364
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    • 2004
  • In the multi-stage former, a manufacture of hexagonal fitting nut was generated in a defective products about 70∼80% in the industry field. Products generated in defects manufactured to be a machining about 60%. Additional process increased a product cost and decreased a product rate. Therefore, it is important to predict and design a preform reducing defective products in the early stage of process design. So in the study Defects for manufacturing hexagonal fitting nut verified a cause through the finite element simulation. To reduce a defective generation. a preform designed and a designed preform verified through the finite element simulation. In conclusion, a generated defects when a hexagonal fitting nut manufactured should reduce if a round dimension of preform reduced and a part of opposition angle distributed in plenty a volume.

Automated Molding Design Methodology to Optimize Multiple defects in Injection Molded Parts

  • Park, Jong-Cheon;Kim, Byung H.
    • International Journal of Precision Engineering and Manufacturing
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    • v.1 no.1
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    • pp.133-145
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    • 2000
  • Plastic molding designers are frequently faced with optimizing multiple defects in injection molded parts. these defects are usually in conflict with each other, and thus a tradeoff needs to be made reach a final compromised solution. In this study, an automated injection molding design methodology has been developed to optimize multiple defects of injection molded parts. Two features of the proposed methodology are as follows: one is to apply the utility theory to transform the original multiple objective optimization problem into single objective optimization problem with utility as objective function, the other is an implementation of a direct search-based injection molding optimization procedure with automated consideration of process variation. The modified complex method is used as a general optimization tool in this research. The developed methodology was applied to an actual molding design and the results showed that the methodology was useful through the CAE simulation using a commercial injection molding software package. Applied to production, this study will be of immense value to industry in reducing the product development time and enhancing the product quality.

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The Review of Legal Regulations on Recall Service and Product Liability Law (리콜제도와 제조물책임법에 관한 고찰)

  • 허경옥
    • Journal of the Korean Home Economics Association
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    • v.34 no.5
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    • pp.67-84
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    • 1996
  • This study examined two laws protecting consumer's safety, the 'Product Liability Law' and 'Legal Regulations on Recall Service.' and investigated the need for and importance of the laws. Second, the requirements regarding the procedures for implementing these laws were reviewed. Regarding the 'Product Liability Law', the study considered how the damage and injury of consumers caused by defects in production would be compensated and under what conditions. Regarding the law to regulate Recall service, this study reviewed when and how producers must recall their products because of their defects. Finally, the directions for enacting these laws were suggested, and several difficulties arising from their enactment were considered. Several suggestions were made to enact these two raws in order to enhance comsumer safety, consumer sovereignty, and consumer well-being.

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A New Exploratory Testing Method for Improving the Effective IP Set-Top Box Test

  • Kim, Donghyun;Kim, Yoon
    • Journal of the Korea Society of Computer and Information
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    • v.23 no.2
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    • pp.9-16
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    • 2018
  • Recently, as various IP set-top boxes based on Android OS have been widely used in general households and public facilities, complaints about services and set-top boxes have continued to increase as much as other smart devices. In order to reduce this problem, the manufacturer performs the testing work before the product is commercialized. However, the testing can reduce potential defects in the product, but it can not prove that the product is free of defects. Therefore, the quality of the product can vary depending on how effective testing techniques are introduced. In this paper, we propose a new exploratory testing method that minimizes test case creation time and makes it easier to plan and execute test while simultaneously learning how to run the product under test. Using the first proposed method, the test time is reduced by about 16.7 hours and the defect detection rate is 25.4% higher than the formal specification-based testing method. Informally, the test time was shortened by about 4.7 hours and the defect detection rate was 13% higher than the informal experience-based testing method.

Case study of riser design using casting simulation in gravity cast method (중력주조 공법에서 주조해석 시뮬레이션을 이용한 압탕설계 사례 연구)

  • Ko, Sang-Bae;Han, Ki-Won;Kim, Hyung-Jun;Han, Tae-Soo;Han, Seong-Ryeol;Kim, kyung-A;Choi, Kye-Kwang;Yun, Jae-Woong;Lee, Chun-Kyu
    • Design & Manufacturing
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    • v.15 no.2
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    • pp.30-35
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    • 2021
  • The casting method uses a mold to solidify a liquid metal to make a solid metal. Since it uses a liquid metal with the least deformation resistance, it has the characteristic that it can easily manufacture even a complex shape. However, the process of solidifying a liquid metal into a solid metal inevitably involves a volume change and contains internal defects such as shrinkage holes. Therefore, in the design of the casting plan, an excess volume called a pressurization compensates for the volume shrinkage. in the product, and it induces the shrinkage hole defects to occur in parts other than the product1). In this study, casting analysis was performed using casting analysis software (anycasting) in order to optimize the design of the tilting gravity casting method for automobile brackets. In particular, the filling and solidification analysis according to the shape and volume of the pressurized metal was conducted, and applied to the actual product to study the effect of the pressurized metal on the shrinkage defect. Through this study, it is possible to understand the effect of the pressure metal on shrinkage defects in the actual product and propose a design of the pressure metal that improves reliability and productivity.