• 제목/요약/키워드: PCB manufacturing

검색결과 191건 처리시간 0.019초

기하학적 텍스쳐 정보를 이용한 금속 패드 변색영상 분류 알고리즘 (Metal pad Discolored Image Classification Algorithm using Geometric Texture Information)

  • 최학남;김학일
    • 제어로봇시스템학회논문지
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    • 제16권5호
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    • pp.469-475
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    • 2010
  • This paper presents a method of classifying discolored defects of metal pads using geometric texture for AFVI (Automated Final Vision Inspection) systems. In PCB manufacturing process, the metal pads on PCB can be oxidized and discolored partly due to various environmental factors. Nowadays the discolored defects are manually detected and rejected from the process. This paper proposes an efficient geometric texture feature, SUTF (Symmetry and Uniformity Texture Feature) based on the symmetric and uniform textural characteristics of the surface of circular metal pads for automating AFVI systems. In practical experiments with real samples acquired from a production line, 30 discolored images and 1232 roughness images are tested. The experimental results demonstrate that the proposed method using SUTFs provides better performance compared to Gabor feature with 0% FNR (False Negative Rate) and 1.46% FPR (False Positive Rate). The performance of the proposed method shows its applicability in the real manufacturing systems.

병렬기계로 구성된 인쇄회로기판 제조공정에서의 스케쥴링에 관한 연구 (Unrelated Parallel Machine Scheduling for PCB Manufacturing)

  • 김대철
    • 산업경영시스템학회지
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    • 제27권4호
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    • pp.141-146
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    • 2004
  • This research considers the problem of scheduling jobs on unrelated parallel machines with a common due date. The objective is to minimize the total absolute deviation of job completion times about the common due date. This problem is motivated by the fact that a certain phase of printed circuit board manufacturing and other production systems is bottleneck and the processing speeds of parallel machines in this phase are different for each job. A zero-one integer programming formulation is presented and two dominance properties are proved. By these dominance properties, it is shown that the problem is reduced to asymmetric assignment problem and is solvable in polynomial time.

PCB산업현장의 능동소음제어 (Active Noise Control in PCB Industry)

  • 박진홍;남명우
    • 대한전자공학회논문지TE
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    • 제42권4호
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    • pp.41-46
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    • 2005
  • 현대사회에서 소음과 진동은 일상생활뿐 아니라 산업현장에서도 흔히 접하게 되는 환경오염원으로, 이에 대한 관심이 점차 증가하고 있다. 산업현장에서 소음은 중요한 안전요소의 하나이며, 근로자의 청력에 영향을 미칠 뿐 아니라 정신적으로도 많은 영향을 미쳐 최종적으로 업무효율을 떨어뜨리게 되는 중요한 원인이 된다. PCB 산업 현장에서는 제조공정상 필요한 기계들로부터 다양한 소음들이 발생된다. PCB 산업현장의 소음원은 주로 공조기와 제조 기기에서 발생되며, 발생된 소음제어를 위해서는 소음의 전달경로를 막아 소음을 줄이는 방법과 제조기기의 소음을 저감시키는 방법, 수음자에 대한 제어방법 등이 있다. 본 논문에서는 PCB 산업현장에 쉽게 적용할 수 있는 헤드셋(headset)을 이용한 부대역 feedback 능동소음제어(subband feedback active noise control) 방법에 인간의 청각기능을 모델링한 멜 척도를 적용하여 보다 효과적인 소음제어 방법을 제안하였다. 실험결과 멜 척도를 적용하지 않은 부대역 feedback 능동소음제어방법 보다 동일한 구조를 가지면서도 빠른 수렴속도와 향상된 소음제거 결과를 얻을 수 있었다.

5 차원 변위 측정용 원판형 정전용량 센서 (A Disk-type Capacitive Sensor for Five-dimensional Motion Measurements)

  • 안형준;박정호;엄창용
    • 한국소음진동공학회:학술대회논문집
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    • 한국소음진동공학회 2007년도 춘계학술대회논문집
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    • pp.655-662
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    • 2007
  • This paper presents a disk-type capacitive sensor for simultaneous measurement of five-dimensional motions of a target. The sensor can be manufactured with a printed circuit board (PCB) such that the sensor can be integrated with its electronics in a single PCB board, whereby the manufacturing costs is considerably reduced. The sensor is optimally designed through an error analysis of possible mechanical errors. Furthermore, the sensor can correct the horizontal motion measurement errors due to the sensor installation tilting error. A proto-type PCB sensor, electronics and a test rig were built, and the effectiveness of the developed sensor was proved through experiments.

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적층구조로 형성된 PCB형 태양전지용 BusBar의 성능에 관한 연구 (The Research on Performance of PCB type of Solar cell BusBar Formed by Layer Structure)

  • 전택종;조남철;이채문
    • 한국태양에너지학회:학술대회논문집
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    • 한국태양에너지학회 2012년도 춘계학술발표대회 논문집
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    • pp.102-107
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    • 2012
  • The purpose of thesis is to improve output of solar cell module by enhancing transmission efficiency. To improve transmission efficiency, transmission interconnection ribbon which is used to connect solar cells and busbar which contacts with it has been improved. To secure reliability, comparison research on output of solar cell modules has been conducted by manufacturing PCB module formed by laminated metal with the same output. The result of this research is based on a output efficiency test of modules by comparing electric conductivity of soldering busbar and laminated PCV type of busbar.

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Copper thickness and thermal reliability of microvias produced by laser-assisted seeding (LAS) process in printed circuit board (PCB) manufacture

  • Leung, E. S.W.;Yung, W. K.C.
    • International Journal of Quality Innovation
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    • 제2권2호
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    • pp.69-92
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    • 2001
  • The laser-assisted seeding (LAS) process has potential to replace conventional electroless copper plating in Printed Circuit Board (PCB) manufacturing since it combines the steps of laser drilling and plating into one single process. In the LAS process, the single extra LAS step can metallize a microvia. Thus, the process steps can be greatly reduced and the productivity enhanced, but also the high aspect ratio microvias can be metallized. The objectives of this paper are to study the LAS copper thickness within PCB microvias and the thermal reliability of the microvias produced by this process. It was found that results were satisfactory in both the reliability test and also the LAS copper thickness which both comply with IPC standard, the copper thickness produced by the LAS process is sufficient for subsequent electro-plating process. The reliability of the microvias produced by LAS process is acceptable which are free from any voids, corner cracks, and distortion in the plated copper.

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PCB 조립 공정의 작업 투입 순서 및 부품함 배치 문제에 관한 연구 (A Study on Job Sequence and Feeder Allocation Problem in PCB Assembly Line)

  • 유성열;이강배
    • 산업경영시스템학회지
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    • 제29권1호
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    • pp.63-71
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    • 2006
  • In this paper, we consider a planning problem arising from printed circuit board manufacturing industries. Given a set of several types of PCBs, component feeders and surface mounting machines in series in a PCB assembly line, the problem is to define the feeder allocation and job sequence with the objective of minimizing the total operation time of the line. We formulate the problem as a mathematical model. And, the problem is proven to be NP-hard, so a genetic algorithm is developed. Finally, we give test results to evaluate the performance of the genetic algorithm.

SMD Detection and Classification Using YOLO Network Based on Robust Data Preprocessing and Augmentation Techniques

  • NDAYISHIMIYE, Fabrice;Lee, Joon Jae
    • Journal of Multimedia Information System
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    • 제8권4호
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    • pp.211-220
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    • 2021
  • The process of inspecting SMDs on the PCB boards improves the product quality, performance and reduces frequent issues in this field. However, undesirable scenarios such as assembly failure and device breakdown can occur sometime during the assembly process and result in costly losses and time-consuming. The detection of these components with a model based on deep learning may be effective to reduce some errors during the inspection in the manufacturing process. In this paper, YOLO models were used due to their high speed and good accuracy in classification and target detection. A SMD detection and classification method using YOLO networks based on robust data preprocessing and augmentation techniques to deal with various types of variation such as illumination and geometric changes is proposed. For 9 different components of data provided from a PCB manufacturer company, the experiment results show that YOLOv4 is better with fast detection and classification than YOLOv3.

PCB판의 위상 최적화를 위한 재료혼합법의 개발 (Development of a Material Mixing Method for Topology Optimization of PCB Substrate)

  • 한석영;김민수;황준성;박재용;최상혁;이병주
    • 한국공작기계학회논문집
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    • 제16권1호
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    • pp.47-52
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    • 2007
  • A material mixing method to obtain an optimal topology for a structure in a thermal environment was suggested. This method is based on Evolutionary Structural Optimization(ESO). The proposed material mixing method extends the ESO method to a mixing several materials for a structure in the multicriteria optimization of thermal flux and thermal stress. To do this, the multiobjective optimization technique was implemented. The overall efficiency of material usage was measured in terms of the combination of thermal stress levels and heat flux densities by using a combination strategy with weighting factors. Also, a smoothing scheme was implemented to suppress the checkerboard pattern in the procedure of topology optimization. It is concluded that ESO method with a smoothing scheme is effectively applied to topology optimization. Optimal topologies having multiple thermal criteria for a printed circuit board(PCB) substrate were presented to illustrate validity of the suggested material mixing method. It was found that the suggested method works very well for the multicriteria topology optimization.

전기시스템의 절전모드에 적용되는 PCB의 오작동 원인 개선에 관한 연구 (Study on the Causes of Malfunctions of PCBs Applied to the Power Saving Mode of Electrical Systems and its Solution)

  • 박형기;최충석
    • 한국안전학회지
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    • 제28권3호
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    • pp.51-55
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    • 2013
  • The purpose of this study is to find the causes of malfunctions and defective operation of printed circuit boards(PCBs) built into home refrigerators to perform power saving functions. This study performed an electrostatic test of a PCB built-in using an Auto Triggering system; lightning and impulse tests using an LSS-15AX; and an impulse test using an INS-400AX. From the analysis of a secondarily developed product, it was found that electrostatic discharge(ESD) caused more malfunctions and defective operations than electric overstress(EOS) due to overvoltage. As a result of increasing the condenser capacity of the PCB circuit, withstanding voltage was increased to 7.4 kV. In addition, this study changed the power saving mode and connected a varistor to the #2 pin of an IC chip. As a result, the system consisting of all specimens of a finally developed product was operated stably with an applied voltage of less than 10 kV. This study found it necessary to perform quality control at the manufacturing stage in order to reduce the occurrence of electrostatic accidents to IC chips built into a PCB.