Abstract
The purpose of this study is to find the causes of malfunctions and defective operation of printed circuit boards(PCBs) built into home refrigerators to perform power saving functions. This study performed an electrostatic test of a PCB built-in using an Auto Triggering system; lightning and impulse tests using an LSS-15AX; and an impulse test using an INS-400AX. From the analysis of a secondarily developed product, it was found that electrostatic discharge(ESD) caused more malfunctions and defective operations than electric overstress(EOS) due to overvoltage. As a result of increasing the condenser capacity of the PCB circuit, withstanding voltage was increased to 7.4 kV. In addition, this study changed the power saving mode and connected a varistor to the #2 pin of an IC chip. As a result, the system consisting of all specimens of a finally developed product was operated stably with an applied voltage of less than 10 kV. This study found it necessary to perform quality control at the manufacturing stage in order to reduce the occurrence of electrostatic accidents to IC chips built into a PCB.