• Title/Summary/Keyword: Metal Cutting Process

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A study on excavator front support parts to minimize springback defects (굴삭기 Front Support 부품 뒤틀림 결함 최소화 방안 도출)

  • Jeon, Yong-Jun;Heo, Young-Moo;Lee, Ha-Sung;Kim, Dong-Earn
    • Design & Manufacturing
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    • v.12 no.2
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    • pp.40-45
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    • 2018
  • Recently, in construction equipment machinery production, development has focused on environmentally-friendly functions to improve existing production capacity. For excavators as well, emphasis has been placed on response to environmental regulations, miniaturization, and noise reduction, while technology is being developed considering cost reduction and safety.Accordingly, the front support, an inner reinforcement part of the excavator, as well as high-strength steel plates to improve safety and reduce weight, are being applied.However, in the case of high-strength materials, Springback occurs in the final formed part due to high residual stress during product forming. Derivation of a forming or product shaping process to reduce springback is needed. Accordingly, regarding the front support, an inner reinforcement part of the excavator, this study derived a method to improve springback and secure shape stiffness through analysis of the springback occurrence rate and springback causes through a forming analysis.As for the results of analyzing the springback occurrence rate of existing products through forming analysis, springback of -22.6 mm < z < 27.35 mm occurred on the z-axis, and it was confirmed that springback occurred due to the stiffness reinforcing bead of the upper and middle parts of the product.To control product residual stress and springback, we confirmed a tendency of springback reduction through local pre-cutting and stiffness reinforcement bead relocation.In the local pre-cutting model, springback was slightly reduced by 5.3% compared with the existing model, an insignificant reduction effect. In the stiffness reinforcement bead relocation model, when an X-shaped stiffness reinforcement bead was added to each corner portion of the product, springback was reduced by at least 80%.The X-shaped bead addition model was selected as the springback reduction model, and the level of stiffness compared to the existing model was confirmed through a structural analysis.The X-shaped bead additional model showed a stress springback of 90% and springback reduction of 7.4% compared with the existing model, indicating that springback and stiffness will be reinforced.

A Study on mold manufacture of multi-cavity dental iodine container using powder injection molding (분말사출성형을 이용한 다수 캐비티 치과용 요오드 용기 금형제작에 관한 연구)

  • Choi, Jae-Hoon
    • Journal of the Korea Academia-Industrial cooperation Society
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    • v.15 no.1
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    • pp.21-26
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    • 2014
  • When iodine container for dental mouth treatment is opened, thread for treatment is cut by the blade in cap of container. Due to the problem of corrosion in a short period time after the reaction of metal blade to iodine solution, it gives impact on patient hygiene. In order to solve the problem, alternative products such as ceramic blade are developed and produced recently. In case of ceramic blade, it is produced by handwork and machine work. In this study, for the quantity production of ceramic blade with powder injection molding, we proposed a delivery system to have uniform charge of 20 cavity. Using Moldflow, simulation on 20 Cavity flow was performed. And then the mold was obtained through mold production and modification.(based on simulation) After injection molding, debinder, sintering process was achieved for ceramic blade, and the cap product was completed via insert injection on ceramic blade. In this study, we verified possibility of quantity production of ceramic blade which showed effective performance for cutting.

Study of Optimal Machining Conditions of Ultrasonic Machining By Taguchi's Method (다구찌 방법을 이용한 초음파 가공의 최적가공조건에 관한 연구)

  • Liu, Jun Wei;Jin, Jian;Ko, Tae Jo;Baek, Dae Kyun
    • Transactions of the Korean Society of Mechanical Engineers A
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    • v.37 no.2
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    • pp.213-218
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    • 2013
  • Ultrasonic machining (USM) is a new method used in metal cutting. This process does not involve heating or any electrochemical effects, causes low surface damage, has small residual stress, and does not rely on the conductivity of the workpiece. These characteristics are suitable for the machining of brittle materials such as glass or ceramics. However, the use of USM for brittle materials generates cracks on the workpiece. Therefore, in this study, Taguchi's method was used to optimize the processing conditions of micro holes drilled in glass and ceramics. This method was used to successfully reduce the number of cracks at the entrance and the exit of the micro holes.

A Study on Nano/micro Pattern Fabrication of Metals by Using Mechanical Machining and Selective Deposition Technique (기계적 가공과 무전해 선택적 증착기술을 이용한 나노/마이크로 금속패턴 제작에 관한 연구)

  • Cho S.H.;Youn S.W.;Kang C.G.
    • Proceedings of the Korean Society of Precision Engineering Conference
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    • 2005.06a
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    • pp.1507-1510
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    • 2005
  • This study was carried out as a part of the research on the development of a maskless and electroless process for fabricating metal micro/nanostructures by using a nanoindenter and an electroless deposition technique. $2-\mu{m}-deep$ indentation tests on Ni and Cu samples were performed. The elastic recovery of the Ni and Cu was 9.30% and 9.53% of the maximum penetration depth, respectively. The hardness and the elastic modulus were 1.56 GPa and 120 GPa for Ni and 1.49 GPa and 100 GPa for Cu. The effect of single-point diamond machining conditions such as the Berkovich tip orientation (0, 45, and $90^{\circ}$) and the normal load (0.1, 0.3, 0.5, 1, 3, and 5 mN), on both the deformation behavior and the morphology of cutting traces (such as width and depth) was investigated by constant-load scratch tests. The tip orientation had a significant influence on the coefficient of friction, which varied from 0.52-0.66 for Ni and from 0.46-0.61 for Cu. The crisscross-pattern sample showed that the tip orientation strongly affects the surface quality of the machined area during scratching. A selective deposition of Cu at the pit-like defect on a p-type Si(111) surface was also investigated. Preferential deposition of the Cu occurred at the surface defect sites of silicon wafers, indicating that those defect sites act as active sites for the deposition reaction. The shape of the Cu-deposited area was almost the same as that of the residual stress field.

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A Study on Nano/Micro Pattern Fabrication of Metals by Using Mechanical Machining and Selective Deposition Technique (기계적 가공과 무전해 선택적 증착기술을 이용한 나노/마이크로 금속패턴 제작에 관한 연구)

  • Cho Sang-Hyun;Youn Sung-Won;Kang Chung-Gil
    • Journal of the Korean Society for Precision Engineering
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    • v.23 no.8 s.185
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    • pp.171-177
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    • 2006
  • This study was performed as a part of the research on the development of a maskless and electroless process for fabricating metal micro/nanostructures by using a nanoindenter and an electroless deposition technique. $2-{\mu}m$-deep indentation tests on Ni and Cu samples were performed. The elastic recovery of the Ni and Cu was 9.30% and 9.53% of the maximum penetration depth, respectively. The hardness and the elastic modulus were 1.56 GPa and 120 GPa for Ni and 1.51 GPa and 104 GPa for Cu. The effect of single-point diamond machining conditions such as the Berkovich tip orientation (0, 45, and $90^{\circ}$ ) and the normal load (0.1, 0.3, 0.5, 1, 3, and 5 mN), on both the deformation behavior and the morphology of cutting traces (such as width and depth) was investigated by constant-load scratch tests. The tip orientation had a significant influence on the coefficient of friction, which varied from 0.52-0.66 for Ni and from 0.46- 0.61 for Cu. The crisscross-pattern sample showed that the tip orientation strongly affects the surface quality of the machined are a during scratching. A selective deposition of Cu at the pit-like defect on a p-type Si(111) surface was also investigated. Preferential deposition of the Cu occurred at the surface defect sites of silicon wafers, indicating that those defect sites act as active sites for the deposition reaction. The shape of the Cu-deposited area was almost the same as that of the residual stress field.

The Microstructural Properties Change Owing to the Sintering Condition of T42 High Speed Steel Produced by Powder Injection Molding Process (분말 사출 성형법으로 제조된 T42 고속도 공구강의 소결 조건에 따른 조직 특성 변화)

  • Do, Kyoung-Rok;Choi, Sung-Hyun;Kwon, Young-Sam;Cho, Kwon-Koo;Ahn, In-Shup
    • Journal of Powder Materials
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    • v.17 no.4
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    • pp.312-318
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    • 2010
  • High speed steels (HSS) were used as cutting tools and wear parts, because of high strength, wear resistance, and hardness together with an appreciable toughness and fatigue resistance. Conventional manufacturing process for production of components with HSS was used by casting. The powder metallurgy techniques were currently developed due to second phase segregation of conventional process. The powder injection molding method (PIM) was received attention owing to shape without additional processes. The experimental specimens were manufactured with T42 HSS powders (59 vol%) and polymer (41 vol%). The metal powders were prealloyed water-atomised T42 HSS. The green parts were solvent debinded in normal n-Hexane at $60^{\circ}C$ for 24 hours and thermal debinded at $N_2-H_2$ mixed gas atmosphere for 14 hours. Specimens were sintered in $N_2$, $H_2$ gas atmosphere and vacuum condition between 1200 and $1320^{\circ}C$. In result, polymer degradation temperatures about optimum conditions were found at $250^{\circ}C$ and $480^{\circ}C$. After sintering at $N_2$ gas atmosphere, maximum hardness of 310Hv was observed at $1280^{\circ}C$. Fine and well dispersed carbide were observed at this condition. But relative density was under 90%. When sintering at $H_2$ gas atmosphere, relative density was observed to 94.5% at $1200^{\circ}C$. However, the low hardness was obtained due to decarbonization by hydrogen. In case of sintering at the vacuum of $10^{-5}$ torr at temperature of $1240^{\circ}C$, full density and 550Hv hardness were obtained without precipitation of MC and $M_6C$ in grain boundary.

The Influence of Microwave Sintering Process on the Adaptation of CAD/CAM Zirconia Core (마이크로 웨이브 소결 과정이 CAD/CAM 지르코니아 코아의 적합도에 미치는 영향)

  • Kim, Keun Bae;Kim, Jee Hwan;Lee, Keun-Woo
    • Journal of Dental Rehabilitation and Applied Science
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    • v.25 no.2
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    • pp.95-107
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    • 2009
  • The purpose of this research was to examine the fitness of zirconia cores that were made by different sintering methods; generic electricity furnace and microwave furnace. Firstly, 12 cores for each group were made by using each different sintering process and attached them to a metal die with silicon. The internal and marginal gap of sintered zirconia was measured by using Skyscan 1076 micro-CT, then it was reorganized by CT-An software. To each samples, we extracted B-L image, M-D image of cutting side, and cross-sectional side of tooth long axis and calculated the mean value of marginal, axial, and occlusal gap each side. Results: 1. The mean marginal gap of sintered zirconia was $36.20{\mu}m$ for EVE, $47.67{\mu}m$ for LAV, $52.47{\mu}m$ for DEN, and $54.63{\mu}m$ for CER. 2. For the axial wall, the research showed the largest value of $63.49{\mu}m$ for EVE, but there were no statistical significance. 3. In related to the occlusal internal measurement, DEN showed the smallest value ($77.06{\mu}m$), EVE and CER showed significantly high value. From this study, it is suggested that CAD/CAM zirconia core which was made in the process of microwave sintering has clinically acceptable values in marginal and internal gap.

Manufactures of dental casting Co-Cr-Mo based alloys in addition to Sn, Cu and analysis of infrared thermal image for melting process of its alloys (Sn 및 Cu를 첨가한 치과 주조용 Co-Cr-Mo계 합금제조 및 용해과정 분석)

  • Kang, Hoo-Won;Park, Young-Sik;Hwang, In;Lee, Chang-Ho;Heo, Yong;Won, Yong-Gwan
    • Journal of Technologic Dentistry
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    • v.36 no.3
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    • pp.141-147
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    • 2014
  • Purpose: Dental casting #Gr I (Co-25Cr-5Mo-3Sn-1Mn-1Si), #Gr II (Co-25Cr-5Mo-5Cu-1Mn -1Si) and #Gr III (Co-25Cr-5Mo-3Sn-5Cu-1Mn-1Si) master alloys of granule type were manufactured the same as manufacturing processes for dental casting Ni-Cr and Co-Cr-Mo based alloys of ingot type. These alloys were analyzed melting processes with heating time of high frequency induction centrifugal casting machine using infrared thermal image analyzer. Methods: These alloys were manufactured such as; alloy design, the first master alloy manufatured using vacuum arc casting machine, melting metal setting in crucible, melting in VIM, pouring in the mold of bar type, cutting the gate and runner bar and polishing. These alloys were put about 30g/charge in the ceramic crucible of high frequency induction centrifugal casting machine and heat, Infrared thermal image analyzer indicated alloys in the crucible were set and operated. Results: The melting temperatures of these alloys measuring infrared thermal image analyzer were decreased in comparison with remanium$^{(R)}$ GM 800+, vera PDI$^{TM}$, Biosil$^{(R)}$ f, WISIL$^{(R)}$ M type V, Ticonium 2000 alloys of ingot type and vera PDS$^{TM}$(Aabadent, USA), Regalloy alloys of shot type. Conclusion: Co-Cr-Mo based alloy in addition to Sn(#Gr I alloy) were decreased the melting temperature with heating time of high frequency induction centrifugal casting machine using infrared thermal image analyzer.

A Study on Na Removal Method in H2WO4(Aq) by Electrodialysis in APT(S) Manufacturing (APT(S) 제조 시 전기투석법을 이용한 H2WO4(Aq)내의 Na 제거 방법에 관한 연구)

  • Kang, Yong-Ho;Hyun, Soong-Keun
    • Resources Recycling
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    • v.26 no.6
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    • pp.65-72
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    • 2017
  • APT (Ammonium paratungstate) is widely used in various industries such as metal cutting tools, drill bits, mining tools, and military inorganic materials. In order to produce high purity APT(S), an impurity purification step in an aqueous $Na_2WO_4$ convert $H_2WO_4$ solution is required. It is difficult to remove impurity Na of 200 ppm or less when $H_2WO_4(S)$ is prepared by adding HCl(Aq) to an aqueous solution of $Na_2WO_4$, which is a well-known conventional wet method. However, in this study, a more economical and efficient method of removing Na through electrodialysis using a cationic membrane was studied. A large amount of Na in aqueous solution of $H_2WO_4$ due to $Na_2CO_3(S)$ which was added to dissolve waste tungsten carbide drill and scrap was removed to 20ppm or less through electrodialysis process, and it was confirmed that the effect of Na removal was great when using electrodialysis.

Microbiological Hazard Analysis for HACCP System Application to Vinegared Pickle Radishes (식초절임 무의 HACCP 시스템 적용을 위한 미생물학적 위해 분석)

  • Kwon, Sang-Chul
    • Journal of Food Hygiene and Safety
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    • v.28 no.1
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    • pp.69-74
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    • 2013
  • This study has been performed for 150 days from February 1 - June 31, 2012 aiming at analyzing biologically hazardous factors in order to develop HACCP system for the vinegared pickle radishes. A process chart was prepared as shown on Fig. 1 by referring to manufacturing process of manufacturer of general vinegared pickle radishes regarding process of raw agricultural products of vinegared pickle radishes, used water, warehousing of additives and packing material, storage, careful selection, washing, peeling off, cutting, sorting out, stuffing (filling), internal packing, metal detection, external packing, storage and consignment (delivery). As a result of measuring Coliform group, Staphylococcus aureus, Salmonella spp., Bacillus cereus, Listeria Monocytogenes, E. coli O157:H7, Clostridium perfringens, Yeast and Mold before and after washing raw radishes, Bacillus cereus was $5.00{\times}10$ CFU/g before washing but it was not detected after washing and Yeast and Mold was $3.80{\times}10^2$ CFU/g before washing but it was reduced to 10 CFU/g after washing and other pathogenic bacteria was not detected. As a result of testing microorganism variation depending on pH (2-5) of seasoning fluid (condiment), pH 3-4 was determined as pH of seasoning fluid as all the bacteria was not detected in pH3-4. As a result of testing air-borne bacteria (number of general bacteria, colon bacillus, fungus) depending on each workplace, number of microorganism of internal packing room, seasoning fluid processing room, washing room and storage room was detected to be 10 CFU/Plate, 2 CFU/Plate, 60 CFU/Plate and 20 CFU/Plate, respectively. As a result of testing palm condition of workers, as number of general bacteria and colon bacillus was represented to be high as 346 $CFU/Cm^2$ and 23 $CFU/Cm^2$, respectively, an education and training for individual sanitation control was considered to be required. As a result of inspecting surface pollution level of manufacturing facility and devices, colon bacillus was not detected in all the specimen but general bacteria was most dominantly detected in PP Packing machine and Siuping machine (PE Bulk) as $4.2{\times}10^3CFU/Cm^2$, $2.6{\times}10^3CFU/Cm^2$, respectively. As a result of analyzing above hazardous factors, processing process of seasoning fluid where pathogenic bacteria may be prevented, reduced or removed is required to be controlled by CCP-B (Biological) and threshold level (critical control point) was set at pH 3-4. Therefore, it is considered that thorough HACCP control plan including control criteria (point) of seasoning fluid processing process, countermeasures in case of its deviation, its verification method, education/training and record control would be required.