• Title/Summary/Keyword: Mechanical tests

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Stability Analysis of Open Pit Slopes in the Pasir Coal Field, Indonesia (인도네시아 Pasir 탄전에서의 노천채탄장 사면의 안전성해석)

  • 정소걸;선우춘;한공창;신희순;박연준
    • Proceedings of the Korean Society for Rock Mechanics Conference
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    • 2000.09a
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    • pp.183-193
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    • 2000
  • A series of studies such as geological logging data analysis, detailed geological survey, rock mass evaluation, in-situ and laboratory tests, rock strength and mechanical properties of the rock were concerned. The stability of the slope were carried out inorder to design the pit slope and individual benches using the stereographic projection analysis and numerical methods in Roto Pit of Pasir coal fetid. The bedding plane was one of the major discontinuities in the Roto Pit and the dip of which is about $60^{\circ}$in the northern part and $83^{\circ}$in the southern part. The dip of bedding becomes steeper from north to south. The plane and toppling failures are presented in many slopes. In laboratory test the average uniaxial compressive strength of mudstone was 9 MPa and that of weak sandstone was 10 MPa. In-situ test showed that the rocks of Roto north mining area are mostly weak enough to be classified in grade from R2(weak) to R3(medium strong weak) and the coal is classified in grades from R1(Very weak) to R2(Weak). The detailed stability analysis were carried out on 4 areas of Roto north(east, west, south and north), and 2 areas of Roto south(east and west). In this paper, the minimum factor of safety was set to 1.2 which is a general criterion for open pit mines. Using the stereographic projection analysis and the limit equilibrium method, slope angles were calculated as 30~$36^{\circ}$for a factor of safety greater than 1.2. Then these results were re-evaluated by numerical analysis using FLAC. The final slope angles were determined by rational described abode. A final slope of 34 degrees can guarantee the stability for the eastern part of the Roto north area, 33 degrees for the western part, 35 degrees for the northern part and 35 degrees for the southern part. For the Roto south area, 36 degrees was suggested for both sides of the pit. Once the pit slope is designed based on the stability analysis and the safety measures. the stability of 니ope should be checked periodically during the mining operations. Because the slope face will be exposed long time to the rain fall, a study such aspreventive measures against weathering and erosion is highly recommended to be implemented.

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Stability Analysis of Open Pit Slopes in the Pasir Coal Field, Indonesia (인도네시아 Pasir 탄전에서의 노천채탄장 사면의 안정성 해석)

  • 정소걸;선우춘;한공창;신희순;박연준
    • Tunnel and Underground Space
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    • v.10 no.3
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    • pp.430-440
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    • 2000
  • A series of studies such as geological logging data analysis, detailed geological survey, rock mass evaluation, in-situ and laboratory tests, rock strength and mechanical properties of the rock were concerned. The stability of the slope were carried out inorder to design the pit slope and individual benches using the stereographic projection analysis and numerical methods in Roto Pit of Pasir coal field. The bedding plane was one of the major discontinuities in the Roto Pit and the dip of which is about 60$^{\circ}$ in the northern part and 83$^{\circ}$ in the southern part. The dip of bedding becomes steeper from north to south. The plane and toppling failures are presented in many slopes. In laboratory test the average uniaxial compressive strength of mudstone was 9MPa and that of weak sandstone was 10MPa. In-situ test showed that the rocks of Roto north mining area are mostly weak enough to be classified in grade from R2(weak) to R3(medium strong weak) and the coal is classified in grades from R1(Very weak) to R2(Weak). The detailed stability analysis were carried out on 4 areas of Roto north (east, west, south and north), and 2 areas of Roto south(east and west). In this paper, the minimum factor of safety was set to 1.2 which is a general criterion for open pit mines. Using the stereographic projection analysis and the limit equilibrium method, slope angles were calculated as 30∼36$^{\circ}$ for a factor of safety greater than 1.2. Then these results were re-evaluated by numerical analysis using FLAC. The final slope angles were determined by rational described above. A final slope of 34 degrees can guarantee the stability for the eastern part of the Roto north area, 33 degrees for the western part, 35 degrees for the northern part and 35 degrees for the southern part. For the Roto south area, 36 degrees was suggested for both sides of the pit. Once the pit slope is designed based on the stability analysis and the safety measures, the stability of slope should be checked periodically during the mining operations. Because the slope face will be exposed long time to the rain fall, a study such aspreventive measures against weathering and erosion is highly recommended to be implemented.

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Suitable Conditions of Producing the LVL from Pitch Pine and its Paint Film Durability (리기다소나무 단판적층재(單板積層材)의 제조조건(製造條件)에 따른 물리적성질(物理的性質) 및 도장성능(塗裝性能))

  • Park, Sang-Bum;Kong, Young-To;Jo, Jae-Myeong
    • Journal of the Korean Wood Science and Technology
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    • v.17 no.1
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    • pp.3-11
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    • 1989
  • This study was carried out to investigate the physical and mechanical properties. durability of adhesive bond and paint film for the basic data which were required to determine the suitability as a raw material for furniture the laminated veneer lumber (LVL) with pitch pine (Pinus rigida Mill). The results obtained were as follows; 1) The proper pressing time for making the LVL was over 45 second per milimeter of LVL thickness. 2) The bending strength of the LVL was lower than that of the solid wood but the compressive strength of the LVL was similar to that of the solid wood. The strength increased with the decrease of veneer thickness. 3) The impact bending absorbed energy of the LVL was 0 to 0.3 kg.m/$cm^2$ in the direction of parallel to the grain. The energy of the LVL was lower than that of the solid wood (0.68 kg.m/$cm^2$). 4) In warm water soaking and cold-dry tests, delamination of adhered layers surface crack, swelling, and color change were not found when the hot pressing time was over 45 second per milimeter of LVL thickness. As a result of soak under vacuum test shrinkage in the direction of parallel to the grain was about -1.0 percent and. was about 3.0 percent in the direction of the perpendicular to the grain. 6) The film cacks on the LVL's surface after the wet and cold-dry test were not found at all. 7) In the use of the LVL for interior decoration it was considered that the surface of the LVL be overlaid crossly with fancy veneers of birch and paulownia, etc. This cross overlayirg methods have resulted in few cracks on the fancy veneer.

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Treatment of Artificial Sewage Using a Zeolite Column (제올라이트 칼럼에 의한 인공생활하수처리)

  • Seo, Jeoung-Yoon
    • Korean Journal of Environmental Agriculture
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    • v.21 no.3
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    • pp.178-188
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    • 2002
  • Constructed wetlands typically cost less to build and operate, and require less energy than standard mechanical treatment technology but they have similar performance to centralized wastewater treatment plants. Therefore, they were constructed especially many in rural areas, where are small villages but not industries. Plantless column tests were performed to investigate the possibility on using zeolite as a filter medium of constructed wetland for the wastewater treatment. Removal efficiency was $COD_{Cr}$ 94.63% T-P 41.41% and $NH_4^+-N$ 99.75% at hydraulic load 314 $L/m^2{\cdot}d$ and filtering height 100 cm filled with a zeolite mixture. This zeolite mixture consisted of 1 : 1 by volume of zeolites in the diameter range of 0.5 to 1 mm and 1 to 3 mm. Accordingly, hydraulic load 314 $L/m^2{\cdot}d$ was considered as optimal. Three zeolite mixtures were used to determine the optimal mixing ratio by volume of a zeolite (A) in the diameter range of 0.5 to 1 mm to a zeolite (B) in the diameter range of 1 to 3 mm 1 : 3, 1 : 1 and only B in A to B by volume were tested at hydraulic load 314 $L/m^2{\cdot}d$ and filtering height 100 cm $COD_{Cr}$ removal efficiency was more than 89% at mixing ratios of 1 : 3 and 1 : 1 in A to B. That of T-P ranged 56.42 to 58.72% and, that of T-N and $NH_4^+-N$ was 87% and 99% regardless of mixing ratios of two zeolites. Removal efficiency was lower at the column filled with only B. Removal efficiency was better at Inter medium filled with mixing ratio 1 : 1 in A to B than with the other mixing ratios. Thus, it was found that the mixture of mixing ratio 1 : 1 in A to B was appropriate far Inter medium of constructed wetland Removal efficiency was higher in down-flow than in up-flow, and all contaminants were removed most in 20 cm filter height near feeding area.

Study on the Establishment of Barley Cultivation System using the Power Tiller (동력경운기를 중심으로한 맥류재배의 기계화 -관작업체계 확립에 관한 연구)

  • 이영렬;최규홍
    • Journal of Biosystems Engineering
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    • v.3 no.2
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    • pp.22-33
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    • 1978
  • To maintain the self-sufficiency of food production , it is required to improved the productivity and increase the effective utilization of land in the double cropping areas using improved cultivation technology. The following reasons encourage this cours of action because the overlapping rice harvest and barely seeding seasons complete for labour, the lower price of barley makes it financially less attractive to grow and these two facts together are responsible for a decrease in barley being planted in certain more seasonably marginal double cropping areas. Fro these reasons, it is desirable to carry out tests to improve the current cultivation techniques . In this interest , the following studies were carried out in the experimental field located at Banweol-myeon, Whasung-jkun, Gyeonggi-do from October 1977 to July 1978 in order to establish the mechanical method of barley cultivation using the power tiller. The summarized results are as follows. 1. The work performance in the seeding operation using the rotary barley seeder was 68 minutes per 10 ares which compares favourably with 408 min/10a using the conventional method. This is only one sixth of the time required by th conventional method. The operating costs using the rotary barley seeder was 1, 463 won per 10 areas as against 3, 486 Won per 10 ares for the conventional method, showing a saving of about 50% in comparison with the conventional method. 2. In the manure spreading operation, the work performance was 25 min/10a for the manure spreading machine , compared to 1089 min/10a for the manual operations. This is about one fourth of the time required by the conventional method, The operating costs were 810 Won/10a for the machine and 857 Won/10a for the manual labour. This cost shows little advantage by the machine over the manual labor costs. The conventional method of manure spreading will continue pending decision which will develope and improve the machine.3. Work performance in the rolling operation using the barley rolIer was 30 min/lOa which compares favourably with 135 min/10a using conventional method. This was one fourth of the time required by the conventional method. The operating costs were 514 Won/103. for the machine and 1, 003 Won/lOa for manual labour. In the weed control operation, the work performance and operating costs were 45min/lOa, 1, 399won/10a for the herbcide application using the power sprayer, 1, 149min/10a 8, 541won/lOa for the conventional method respectively. This is 26 times higher efficiency in comparison to the conventional method. 4. In the harvesting operation using the reaper binder and tiller attachment, the work performance was 60min/lOa and represents a cost of 2, 039won/10a. The con\ulcornerventional method took 640min/10a at a cost of 4, 757won/lOa. The reaper binder showns a saving of one tenth over the conventional method. The automatic thresher is already recommended for the current situations, and is now being used. 5. From a comparison of the results of the above trials, the serial cultivation system using the attachment for the power tiller such as the rotary barley seeder is now to be recommended for the current barley cultivation system. It is also recommend from these results that the mechanized technology now available must be used to improve and maintain the increase in barley production. It is seen th1t this is the only course now avaihble to solve the peak seasonal requirements of labour needed for l11rvesting and seeding between rice and barley cultivation.

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Effect of Cooling Water Capacity on the Engine Performance for Small Diesel Engine (냉각수(冷却水) 용량(容量)이 소형(小型) 디젤기관(機關)의 성능(性能)에 미치는 영향(影響))

  • Myung, Byung Soo;Kim, Soung Rai
    • Korean Journal of Agricultural Science
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    • v.13 no.2
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    • pp.265-278
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    • 1986
  • This study was attempted to improve the thermal efficiency of 6 kW water-cooled diesel engine on power tiller. The engine performance tests were conducted to find out the effect of cooling water capacity of 2700cc, 2800cc, 2900cc, 3000cc, 3100cc on power, brake specific fuel consumption (BSFC), torque, temperature of cooling water and lubricating oil and friction losses of the engine with D. C. dynamometer. The results obtained in the study are summarized as follows: 1. The performance of the engine tested was adequated to Korea Industrial Standard but actual economy power was 10% higher than the labeled rated power of the engine. The BSFC of the engine tested 297.8g/kW-h which is belong a little higher level than hreign products. The temperature of cooling water was $101^{\circ}C$ which is higher than SAE standard ($88^{\circ}C$) 2. The friction losses of engine tested was 3.656 kW at 2200 rpm of rated rpm (piston speed 6.97m/sec) and is higher than those of foreign products. 3. When the cooling water capacity was increased from 2700cc to 3100cc the power output of the engine was increased from 6.7 kW to 7.13 kW at the rate of 6.4% and also the torque of the engine was increased from 28.85 N.m to 30.76 N.m at the rate of 6.39%. 4. When the cooling water capacity was increased from 2700cc to 3100cc, the BSFC was decreased 6.9g/kW-h from 310.9g/kW-h to 304.1g/kW-h, and after one half hour operation with full load, the temperature of cooling water was decreased $13^{\circ}C$ from $101^{\circ}C$ to $88^{\circ}C$ and also the temperature of lubricant oil was decreased $6.4^{\circ}C$ from $76.7^{\circ}C$ to $70.4^{\circ}C$. 5. The mechanical efficiency was increased from 70.08% to 71.08% when the cooling water capacity was increased from 2700cc to 3100cc.

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Development of Liquid Cadmium Cathode Structure for the Inhibition of Uranium Dendrite Growth (수지상 우라늄 성장억제를 위한 액체카드뮴 음극구조 개발)

  • Paek, Seung-Woo;Yoon, Dal-Seong;Kim, Si-Hyung;Shim, Jun-Bo;Ahn, Do-Hee
    • Journal of Nuclear Fuel Cycle and Waste Technology(JNFCWT)
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    • v.8 no.1
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    • pp.9-17
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    • 2010
  • The LCC (Liquid Cadmium Cathode) structure to be developed for inhibiting the formation and growth of the uranium dendrite has been known as a key part in the electrowinning process for the simultaneous recovering of uranium and TRU (TRans Uranium) elements from spent fuels. A zinc-gallium (Zn-Ga) experimental system which is able to be functional in aqueous condition and normal temperature has been set up to observe the formation and growth phenomena of the metal dendrites on liquid cathode. The growth of the zinc dendrites on the gallium cathode and the performance of the existing stirrer type and pounder type cathode structure were observed. Although the mechanical strength of the dendrites appeared to be weak in the electrolyte and easily crashed by the various cathode structures, it was difficult to effectively submerge the dendrite into the bottom of the liquid cathode. Based on the results of the aqueous phase experiments, a lab-scale electrowinning experimental apparatus which are applicable to the development of LCC srtucture for the electrowinning process was established and the performance tests of the different types of LCC structure were conducted to prohibit the uranium dendrite growth on LCC surface. The experimental results of the stirrer type LCC structures have shown that they could not effectively remove the uranium dendrites growing at the inner side of the LCC crucible and the performances of the paddle and harrow type LCC structure were similar. Therefore a mesh type LCC structure was developed to push down the uranium dendrites to the bottom of the LCC crucible growing on the LCC surface and at the inner side of the crucible. From the experimental results for the performance test of the mesh type LCC structure, the uranium was recovered over 5 wt% in cadmium without the growth of uranium dendrites. After completion of the experiments, solid precipitates of the bottom of the LCC crucible were identified as an intermetallic compound (UCd11) by the chemical analysis.

Swelling and Mechanical Property Change of Shale and Sandstone in Supercritical CO2 (초임계 CO2에 의한 셰일 및 사암의 물성변화 및 스웰링에 관한 연구)

  • Choi, Chae-Soon;Song, Jae-Joon
    • Tunnel and Underground Space
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    • v.22 no.4
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    • pp.266-275
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    • 2012
  • In this study, a method is devised to implement a supercritical $CO_2$ ($scCO_2$) injection environment on a laboratory scale and to investigate the effects of $scCO_2$ on the properties of rock specimens. Specimens of shale and sandstone normally constituting the cap rock and reservoir rock, respectively, were kept in a laboratory reactor chamber with $scCO_2$ for two weeks. From this stage, a chemical reaction between rock surface and the $scCO_2$ was induced. The effect of saline water was also investigated by comparing three conditions ($scCO_2$-rock, $scCO_2-H_2O$-rock and $scCO_2$-brine(1M)-rock). Finally, we checked the changes in the properties before and after the reaction by destructive and nondestructive testing procedures. The swelling of shale was a main concern in this case. The experimental results suggested that $scCO_2$ has a greater effect on the swelling of the shale than pure water and brine. It was also observed that the largest swelling displacement of shale occurred after a reaction with the $H_2O-scCO_2$ solution. The results of a series of the destructive and nondestructive tests indicate that although each of the property changes of the rock differed depending on the reaction conditions, the $H_2O-scCO_2$ solution had the greatest effect. In this study, shale was highly sensitive to the reaction conditions. These results provide fundamental information pertaining to the stability of $CO_2$ storage sites due to physical and chemical reactions between the rocks in these sites and $scCO_2$.

A Study on the Estimation of Compression Index in the East-Southern Coast Clay of Korea (동남해안 점토의 압축지수 추정에 관한 연구)

  • Park, Choon-Sik;Kim, Sung-Su
    • Journal of the Korean Geotechnical Society
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    • v.35 no.8
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    • pp.43-56
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    • 2019
  • This research has been conducted to suggest an estimation equation of compression index to be practically applied to the southeastern areas by finding out physical and mechanical characteristics of 229 points on the southeastern coast areas (Busan area: 78 points, Gimhae area: 103 points, Geoje area: 18 points, Changwon area: 30 points) through indoor tests and analyzing its relation to the compression index. From the results, we could not only find out correlation between natural water content, liquid limit and initial void ratio versus compression index for soft ground on each of the southeastern coast areas, but also an integrated correlation equation of the southeastern coast areas. In addition, we have performed a comparative analysis of the existing estimated equation of compression index and that found in this paper. As a result, the existing estimated equation suggested by foreign researchers has shown considerable error to be applied to the soft ground on the southeastern coast areas in Korea. The estimated equation of compression index with the water content out of the existing estimated equations has shown minimum 10.8% to maximum 48.1% of error rate, minimum 13.4% to maximum 288.5% of error rate with liquid limit or minimum 9.4% to maximum 211.4% of error rate with initial void ratio. On the other hand, error rates calculated with the estimated equations of compression index from this research have shown minimum 10.5% to maximum 13.4% with water content, minimum 11.6% to maximum 21.3 with liquid limit or minimum 7.1% to maximum 11.7% with initial void ratio, for better results than those with existing estimated equations. In addition, relation between compression index and expansion index has shown Cs = (1/5 ~ 1/12)Cc similar to the existing relation of Cs = (1/5 ~ 1/10)Cc.

Review of Erosion and Piping in Compacted Bentonite Buffers Considering Buffer-Rock Interactions and Deduction of Influencing Factors (완충재-근계암반 상호작용을 고려한 압축 벤토나이트 완충재 침식 및 파이핑 연구 현황 및 주요 영향인자 도출)

  • Hong, Chang-Ho;Kim, Ji-Won;Kim, Jin-Seop;Lee, Changsoo
    • Tunnel and Underground Space
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    • v.32 no.1
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    • pp.30-58
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    • 2022
  • The deep geological repository for high-level radioactive waste disposal is a multi barrier system comprised of engineered barriers and a natural barrier. The long-term integrity of the deep geological repository is affected by the coupled interactions between the individual barrier components. Erosion and piping phenomena in the compacted bentonite buffer due to buffer-rock interactions results in the removal of bentonite particles via groundwater flow and can negatively impact the integrity and performance of the buffer. Rapid groundwater inflow at the early stages of disposal can lead to piping in the bentonite buffer due to the buildup of pore water pressure. The physiochemical processes between the bentonite buffer and groundwater lead to bentonite swelling and gelation, resulting in bentonite erosion from the buffer surface. Hence, the evaluation of erosion and piping occurrence and its effects on the integrity of the bentonite buffer is crucial in determining the long-term integrity of the deep geological repository. Previous studies on bentonite erosion and piping failed to consider the complex coupled thermo-hydro-mechanical-chemical behavior of bentonite-groundwater interactions and lacked a comprehensive model that can consider the complex phenomena observed from the experimental tests. In this technical note, previous studies on the mechanisms, lab-scale experiments and numerical modeling of bentonite buffer erosion and piping are introduced, and the future expected challenges in the investigation of bentonite buffer erosion and piping are summarized.