• Title/Summary/Keyword: MLG(Main Landing Gear)

Search Result 2, Processing Time 0.177 seconds

A Study of the Effects of Hard Landing on Aircraft Structure (Hard Landing이 항공기 구조물에 미치는 영향성 연구)

  • Oh, Yong-Kyu;Sim, Sang-Ki;Shin, Ki-Su
    • Journal of the Korea Institute of Military Science and Technology
    • /
    • v.14 no.5
    • /
    • pp.805-811
    • /
    • 2011
  • Aircraft MLG and wing structures have been recognized as fatigue critical structures and exposed to the risk of fatigue crack initiation and propagation. Furthermore, these structures are frequently subjected to serious dynamic loading condition during a Hard Landing which may lead to their failure. Especially, structural integrity of MLG and wing components is decreased as the flight time increased because of the fatigue damage accumulated on the aircraft. In this study, the effects of Hard Landing on the MLG and wing components of aging aircraft were evaluated by using numerical approach. To achieve the aim, a finite element model has been developed and simulations were conducted by varying the landing conditions. As a result, it was revealed that the high stress concentration phenomenon was occurred at the lower Side Brace of MLG. Thereby, the intensified inspection for the lower Side Brace should be considered to prevent unexpected aircraft mishap.

A Improvement Study on Safety Assurance of Main Landing Gear Failure for Rotary Wing Aircraft (회전익 항공기 안전 확보를 위한 주륜완충장치 결함 개선연구)

  • Choi, Jae Hyung;Chang, Min Wook;Lim, Hyun-Gyu;Lee, Je Suk
    • Journal of the Korean Society for Aeronautical & Space Sciences
    • /
    • v.45 no.6
    • /
    • pp.490-497
    • /
    • 2017
  • The Main Landing Gear(MLG) of Rotary Wing Aircraft is an essential equipment in Landing System for pilot to perform a flight mission. It supports the fuselage at ground and absorbs the impact from the ground when landing, thereby, these functions sustain operational capability for pilot and crew. However, the A aircraft caused asymmetry and leakage hydraulic when it was stationed on the ground. Therefore, this paper summarizes pilot comments in operation which are classified by cause of occurrence and the troubleshooting process about each comment. It also describes design improvements which was derived from troubleshooting and suggests verification results of flight test.