• Title/Summary/Keyword: Liquid Rocket

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Study of Lay-out Design Concept for Liquid Rocket Engine System (액체로켓엔진 시스템 Lay-out 설계 개념 연구)

  • Chung, Yong-hyun;Lee, Eun-Seok
    • Journal of Aerospace System Engineering
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    • v.1 no.4
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    • pp.42-45
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    • 2007
  • The process of Lay-out design and assembly for liquid rocket engine was presented and the Lay-out design for main components of liquid Rocket engine system was studied. Vertical direction is recommended in the case of turbopump's arrangement. If the length of pipe between gas-generator with turbopump's turbine is shorter, gas-generator is stable. The arrangements of main valves are recommended as near disposition to combustion chamber, because shut-down process time is shorter. Interference with launch vehicle and structural strength considering gimbal actuator's force and control performance is considered in the case of gimbal actuator's supporter design.

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A Correction Method for Operating Mode Analysis of Gas Generator Cycle Liquid Propellant Rocket Engine (가스발생기 사이클 액체로켓엔진작동 모드 해석의 보정 방법)

  • Nam, Chang-Ho;Moon, Yoonwan;Park, Soon Young;Chung, Enhwan
    • Journal of the Korean Society of Propulsion Engineers
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    • v.22 no.6
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    • pp.104-110
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    • 2018
  • Operating mode analysis of a liquid propellant rocket engine(LRE) is a crucial tool through the development of an engine. The operating mode analysis of an engine based on a collection of the acceptance tests of components shows discrepancies when compared to the test results. We propose a correction method for performance parameters to develop an engine analysis model for the gas generator cycle of an LRE. In order to simulate engine behavior, the performance parameters for the analysis model are tuned based on the test results of the 75tf engine of KSLV-II.

Performance Evaluation of C/SiC Composites (C/SiC 복합재료의 내열성능 평가)

  • Kim, Yun-Chul
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2007.04a
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    • pp.185-188
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    • 2007
  • The main objective of this research effort was to develope the performance of C/SiC composites manufactured by LSI (Liquid Silicon Infiltration) method for solid and liquid rocket propulsion system and ensure the performance analysis technique. The various carbon preform were manufactured by filament winding, tape rolling, involute layup and stack molding process. For the best performance of thermal and mechanical properties, many process conditions were tested and selected by varying preform, the content of SiC, temperature, impregnation resin and chemical vapour reaction. In conclusion, the high performance and reliability of C/SiC composite were proved for solid and liquid rocket propulsion system. And the performance analysis technique related to mathematical ablation model was originated.

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Investigation of Chill Down Characteristics of Liquid Oxygen Feeding System in 75 Tonf-class Liquid Rocket Engine Firing Test (75톤급 액체로켓엔진 연소시험에서의 액체산소 공급부 예냉특성 고찰)

  • Seo, Daeban;Cho, Namkyung;Han, Yeoungmin
    • Journal of the Korean Society of Propulsion Engineers
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    • v.22 no.4
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    • pp.108-116
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    • 2018
  • A firing test of the 75 tonf-class liquid rocket engine to be used as the first and second stage engines of the KSLV-II was carried out at the rocket engine test facility(RETF). Since this engine uses liquid oxygen as the oxidizer, which is a cryogenic fluid, it is essential that the chill down of the supply pipe line and engine proceed for the firing test; thus, the given inlet requirements must be met. Moreover, it is important to understand the chill down characteristics of the facility and the engine and the amount of liquid oxygen consumed in the chill down process for efficient test operation in the future. In this paper, chill down characteristics of the supply pipe and the engine were evaluated through the investigation of the chill down process of the 75 tonf-class liquid rocket engine at each stage before and after run tank pressurization. In addition, the amount of liquid oxygen consumed was also evaluated.

Technology Trend of Additive Manufacturing for Fabrication of Liquid Rocket Engines (액체로켓엔진 제작을 위한 적층제조 기술 동향)

  • Yoo, Jaehan
    • Journal of Aerospace System Engineering
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    • v.14 no.5
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    • pp.73-82
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    • 2020
  • Recently, there has been an increase in additive manufacturing for the fabrication of liquid rocket engines. This technology can innovate conventional fabrication methods to reduce the lead time and manufacturing cost and can enhance the performances such as weight reduction. In this study, a literature survey is presented that includes types, advantages, disadvantages, and foreign government-based projects of the technology related to liquid rocket engine manufacturing. The present survey focuses on the technology that has been applied to various components such as turbopumps and valves while much larger efforts are made for combustion chambers with regenerative cooling channels and diverging nozzles, as the advantages of the technology are maximized for the applications.

Measurement of Heat Flux in Rocket Combustors Using Plug-Type Heat Flux Gauges

  • Kim, Min Seok;Yu, I Sang;Kim, Wan Chan;Shin, Dong Hae;Ko, Young Sung
    • International Journal of Aeronautical and Space Sciences
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    • v.18 no.4
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    • pp.788-796
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    • 2017
  • This paper proposes a new measurement method to improve the shortcomings of an existing integral method for measuring heat flux in plug-type heat flux gauges in the high-temperature and high-pressure environments of liquid-rocket combustors. Using the existing integral measurement method, the calculation of the surface area for the heat flux in the gauge exhibits error in relation to the actual surface area. To solve this problem, transient profiles obtained from ANSYS Fluent were used to calculate unsteady heat flux as it adjusted to the measured temperature. First, a heat flux gauge was designed and manufactured specifically for use in the high-temperature and high-pressure conditions that are similar to those of liquid rocket combustors. A calibration test was performed to prove the reliability of the manufactured gauge. Then, a combustion experiment was conducted, in which the gauge was used to measure unsteady heat flux in a liquid rocket combustor that used kerosene and liquid oxygen as propellants. Reasonable heat flux values were obtained using the gauge. Therefore, the proposed measurement method is considered to offer significant improvement over the existing integral method.

Comparison of Effectiveness for Performance Tuning of Liquid Rocket Engine

  • Cho, Won Kook;Kim, Chun Il
    • International Journal of Aerospace System Engineering
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    • v.5 no.2
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    • pp.16-22
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    • 2018
  • An analysis has been made on the performance variation due to pressure drop change at propellant supply pipes of liquid rocket engine. The objective is to compare the effectiveness of control variables to tune the liquid rocket engine performance. The mode analysis program has been used to estimate the engine performance for different modes which is realized by controlling the flow rate of propellant. The oxidizer of combustion chamber, the fuel of combustion chamber, the oxidizer of gas generator and the fuel of gas generator are the independent variables to control engine thrust, engine mixture ratio and temperature of gas generator product gas. The analysis program is validated by comparing with the powerpack test results. The error range of compared variables is order of 4%. After comparison of tuning effectiveness it is turned out that the pressure drop at oxidizer pipe of gas generator and pressure drop at combustion chamber fuel pipe and the pressure drop at the fuel pipe of gas generator can effectively tune the thrust of engine, mixture ratio of engine and temperature of product gas from gas generator respectively.

Analysis of Pintle Tip Thermal Damage in the Combustion Hot Firing Test with a 1.5-tonf Class Liquid-Liquid Pintle Injector (1.5톤급 액체-액체 핀틀 분사기 연소시험에서의 핀틀 팁 열손상 원인 분석)

  • Kang, Donghyuk;Hwang, Dokeun;Ryu, Chulsung;Ko, Youngsung
    • Journal of the Korean Society of Propulsion Engineers
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    • v.24 no.6
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    • pp.1-9
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    • 2020
  • Using kerosene and liquid oxygen, 1.5-tonf class liquid-liquid pintle injector with rectangular two-row orifice was designed and manufactured. The combustion test of the pintle injector was carried out to verify the combustion performance and combustion stability under a supercritical condition which is the actual operation condition of the liquid rocket engine. The combustion test result showed that the pintle tip was damaged by the high temperature combustion gas in the high-mixed ratio recirculation zone of the combustion chamber. To solve this problem, the insert nozzle was installed in the pintle injector to increase cooling performance at the pintle tip. As a result of the hot firing test, installation of the insert nozzle, AR and BF had a great effect on pintle tip cooling performance.

Conceptual Design of KSLV-II 3rd Stage Engine Test Facility (한국형발사체 3단 엔진 연소시험설비 개념설계)

  • Kim, Seung-Han;Chung, Yong-Gap;Han, Yeoung-Min
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2012.05a
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    • pp.484-488
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    • 2012
  • Korea Aerospace Research Institute (KARI) performed the conceptual design of rocket engine test facility for the development and qualification of the 3rd stage liquid rocket engine for KSLV-II. The 3rd stage rocket engine test facility, which are to be constructed at Naro Space Center, will supply propellants and high-pressure gases to engine for firing test at ground and altitude conditions. The altitude test condition is obtained using a supersonic diffuser operated by the self-ejecting jet from the liquid rocket engine.

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Combustion instability during engine start at the propulsion test facility for KSR-III rocket (KSR-III Rocket 종합 시험 설비에서 발생한 초기 연소 불안정에 관한 연구)

  • Cho S.;Kang S.;Ha S.;Cho I.;Oh S.
    • Proceedings of the KSME Conference
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    • 2002.08a
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    • pp.267-270
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    • 2002
  • Combustion instability, which is one of the most undesirable phenomena in the development of liquid Propellant rocket engine, can cause serious damage to the rocket itself, and must be evaded by all means. Unfortunately, KSR-III rocket went through the combustion instability during engine start at the propulsion test article No.2. To resolve the problem, time sequence has been changed, and the baffle system has been applied. In consequence of the change, stable combustion was achieved.

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