• Title/Summary/Keyword: High performance engine

Search Result 1,057, Processing Time 0.033 seconds

The Effect of Lubricant Containing Copper Alloy Fine Particles on a Marine Diesel Engine (극미세 구리합금입자(NICO)를 이용한 특수윤활유가 박용기관 성능에 미치는 영향)

  • 소병두;임희성;박권하
    • Proceedings of the Korean Society of Marine Engineers Conference
    • /
    • 2000.11a
    • /
    • pp.61-67
    • /
    • 2000
  • Many research works for improving a boundary lubrication performance have been executed by using solid lubricants, and been tried to apply an engine lubrication. However those general lubricants like MoS$_2$ or PTFE have not been applied on engines due to the extreme conditions such as very high temperature and pressure by combustion process in a cylinder. A copper nickel alloy fine particle has been introduced and studied. In this Paper the lubricant using the alloy Particles is applied on a marine diesel engine and assessed by the engine performance test The results showed the increase of cylinder pressure related strongly to the engine efficiency as well as the improving the engine lubrication performance.

  • PDF

Safety Assessment for Aircraft Engines (항공기 엔진 안전성 평가기술)

  • Lee, Kang-Yi;Yoo, Seung-Woo;Kim, Kui-Soon
    • Journal of the Korean Society of Propulsion Engineers
    • /
    • v.11 no.6
    • /
    • pp.26-34
    • /
    • 2007
  • The efforts to develop high performance aircraft engines are successively progressed with development of recent technology. The reliability of individual parts and the safety of engine systems are reduced if high efficiency components, high strength materials, and precise controls are applied to the engine with complexity to increase engine performance. In this paper, the regulation requirements and assessment technique for aircraft engine safety are considered, and the result of safety assessment on a turbine case cooling system of high efficiency turbofan engine is presented.

A Study on Performance Diagnostics of Turbo-Shaft Engine Using Thermodynamic Sensitivity (열역학적 민감도를 이용한 터보축 엔진의 성능진단 연구)

  • Lee Dae-Won;Roh Tae-Seong;Choi Doeg-Whan
    • Proceedings of the Korean Society of Propulsion Engineers Conference
    • /
    • 2005.11a
    • /
    • pp.289-292
    • /
    • 2005
  • Because of accumulation of operation time, the performance of main components(compressor, combustor, turbine, etc.) come to be deteriorated in gas-turbine engine. So, high reliability and minimun of expense are important problem for engine manufacturer and user in operation of gas-turbine engine. In this study, the diagnostic code of the engine performance using the thermodynamic sensitivity between the sensed parameters and the health parameters has been developed without an application of the commercial program. The single performance deterioration of the turbo-shaft engine has been estimated with this code.

  • PDF

A driving performance prediction of the vehicle mounted with automatic transmission at idle start (공회전 출발시 자동변속기탑재 차량의 구동성능예측)

  • 김태진;정순배
    • Proceedings of the Korean Society of Precision Engineering Conference
    • /
    • 1996.11a
    • /
    • pp.1063-1066
    • /
    • 1996
  • On the prediction of driving performance, an acceleration performance is normally simulated in stall starting condition which is the engine status of full-throttle and high-speed. The lack of transient engine torque data makes the difficulty of predicting an acceleration performance on engine-idle start condition. A experimental equation of transient engine torque is derived from vehicle performance test data. It is applied to simulation the accleration performance prediction on idle starting condition.

  • PDF

Silencer structure for exhaust noise attenuation performance in the high frequency range (500 Hz 이상 고주파수 영역에서 배기소음 저감을 위한 소음기 구조)

  • KIM, Sang-Am
    • Journal of the Korean Society of Fisheries and Ocean Technology
    • /
    • v.54 no.3
    • /
    • pp.255-261
    • /
    • 2018
  • High power trends in the diesel engines due to engine downsizing do not provide noise attenuation that can be satisfied with the performance of the existing silencer on account of high frequency increases in the exhaust noise. This study improves the attenuation performance of the exhaust silencer of the diesel engine and suggests silencer structure that performs best attenuation performance, especially at the high frequency range in the exhaust noise. It proposes dual silencer structure with an average attenuation performance of 6.4 dB and a maximum of 10.7 dB in the high frequency range (over 500 Hz), and analyzes its characteristics compared with the existing silencer. The performance analysis is performed according to 'Measurements on silencers in situation-ISO 11820:1996 Acoustics' and describes the results of comparative analysis with the existing silencer.

Study on the Humidity Effect on Gas turbine Engine Performances (습도가 엔진성능에 미치는 영향에 대한 실험적 고찰)

  • Lee, Bo-Hwa;Lee, Kyung-Jae;Yang, Soo-Seok;Kim, Chun-Taek
    • Aerospace Engineering and Technology
    • /
    • v.9 no.2
    • /
    • pp.98-104
    • /
    • 2010
  • The moisture in the atmosphere exerts a lot of influence upon Gas turbine engine performances. There is a noticeable influence of wet air at the summer sea level, high flight mach number and low engine rpm increasingly. An altitude Engine Test Facility is used to accomplish the engine performance tests at dry air condition and wet air condition, through which engine performance results is revealed. Also, Gas turbine Simulation Program is used to predict the variation of engine performance due to inlet humidity. In the result, net thrust and specific fuel consumption measured -2.826% and 1.325%, respectively at wet air condition compared to dry air condition.

NOx Emission Characteristic according to Aging of EGR Cooler in Non-Road Diesel Engine (EGR 적용 비도로 엔진의 쿨러 열화에 따른 질소산화물 배출특성)

  • Lee, Kyoung-Bok;Oh, Kwang-Chul
    • Journal of Power System Engineering
    • /
    • v.20 no.5
    • /
    • pp.37-45
    • /
    • 2016
  • Exhaust gas recirculation has the advantage of being low-cost and easy to control of NOx emission. Therefore, it is most generally used to reduce NOx emission according to strengthen regulation. In the case of a non-road engine, such as the agricultural engine, since it mainly operate a middle or high-load state, NOx emission is decreased in accordance with the mapping range of the EGR rate, but results in an increase in the particulate matter which is caused to deposit and fouling problem of the EGR system. This problem has become an important issue for maintaining the performance of the engine, as well as emission performance. This study had examined the effects of cooler aging on the performance of heat transfer efficiency and NOx emission in non-road diesel engine. As a result of the EGR cooler aging during 200 hours engine operation, the cooling performance decreased about 25% compared with that of fresh cooler and the NOx emission increased about 14.6% on NRSC(non-road steady cycle) and 20% on NRTC(non-road transient cycle) compared with that of fresh cooler respectively.

The introduction of Engine Performance Test for Miniature Turbojet Engine considering humidity effects (습도 영향을 고려한 초소형 터보제트 엔진 성능시험 소개)

  • Lee, Bo-Hwa;Lee, Kyung-Jae;Yang, Soo-Seok;Kim, Yu-Il
    • Proceedings of the Korean Society of Propulsion Engineers Conference
    • /
    • 2010.11a
    • /
    • pp.335-338
    • /
    • 2010
  • The moisture in the atmosphere exerts a lot of influence upon Gas turbine engine performances. There is a noticeable influence of wet air at the summer sea level, high flight mach number and low engine rpm increasingly. An altitude Engine Test Facility is used to accomplish the engine performance tests at dry air condition and wet air condition, through which engine performance results is revealed. In the result, net thrust and specific fuel consumption measured -2.826% and 1.325%, respectively at wet air condition compared to dry air condition.

  • PDF

A Design for Water Cooling of a Marine Diesel Engine with Verification of Improvement (선박용 수냉식 디젤엔진의 개발 및 성능평가)

  • Sim, Hansub;Jun, Jongoh
    • Journal of the Korean Society of Manufacturing Process Engineers
    • /
    • v.15 no.6
    • /
    • pp.58-63
    • /
    • 2016
  • This paper presents a study of heat dissipation away from the fuel combustion of a marine diesel engine. These engines are operated for long periods under high load conditions: so cooling systems are necessary for radiation and control of the high temperature levels. In the study, each component of the water cooling system was developed to achieve improvements in cooling and safety. Heat transfer considerations and arrangement design for the components were important and an intercooler and exhaust manifold incorporated. An optimization of the cooling water's flow path was achieved subject to the need for convenient maintenance. The 750Ps marine diesel engine was used for performance testing of the cooling system. The test results showed adequate cooling performance improvement.

Study of Mechanism of Counter-rotating Turbine Increasing Two-Stage Turbine System Efficiency

  • Liu, Yanbin;Zhuge, Weilin;Zheng, Xinqian;Zhang, Yangjun;Zhang, Shuyong;Zhang, Junyue
    • International Journal of Fluid Machinery and Systems
    • /
    • v.6 no.3
    • /
    • pp.160-169
    • /
    • 2013
  • Two-stage turbocharging is an important way to raise engine power density, to realize energy saving and emission reducing. At present, turbine matching of two-stage turbocharger is based on MAP of turbine. The matching method does not take the effect of turbines' interaction into consideration, assuming that flow at high pressure turbine outlet and low pressure turbine inlet is uniform. Actually, there is swirl flow at outlet of high pressure turbine, and the swirl flow will influence performance of low pressure turbine which influencing performance of engine further. Three-dimension models of turbines with two-stage turbocharger were built in this paper. Based on the turbine models, mechanism of swirl flow at high pressure turbine outlet influencing low pressure turbine performance was studied and a two-stage radial counter-rotation turbine system was raised. Mechanisms of the influence of counter-rotation turbine system acting on low-pressure turbine were studied using simulation method. The research result proved that in condition of small turbine flow rate corresponding to engine low-speed working condition, counter-rotation turbine system can effectively decrease the influence of swirl flow at high pressure turbine outlet imposing on low pressure turbine and increases efficiency of the low-pressure turbine, furthermore increases the low-speed performance of the engine.