• Title/Summary/Keyword: Gear Pump

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Numerical Simulation of External Gear Pump Using Immersed Solid Method (Immersed Solid Method 를 이용한 외접형 기어 펌프의 수치해석)

  • Yoon, Yong Han;Park, Byung Ho;Han, Yong Oun;Hong, Byeong Joo;Shim, Jaesool
    • Transactions of the Korean Society of Mechanical Engineers B
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    • v.38 no.1
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    • pp.95-101
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    • 2014
  • In this study, an ISM (immersed solid method) was used for investigating the mass flow rate and efficiency of an involute-gear pump featuring very high rotational speed. For considering circulation flow at the gear pump and housing, fluid flow was assumed as turbulent, and the rotational speed of the gear pump increased under the condition of constant pressure at both the inlet and outlet. The efficiency and mass flow rate of the gear pump were studied by varying its rotational speed and the clearance between the gear tip and the housing. In the simulation results, as the rotational speed were increased, the average mass flow rate and efficiency increased. Furthermore, as the clearance between the gear tip and the housing was increased, the average mass flow rate and efficiency decreased. The efficiency was 85.11, 90.94, and 93.62 at rotational speeds of 6,000 rpm, 8,000 rpm, and 10,000 rpm, respectively, under the condition that there was no clearance. In addition, the efficiency was 93.62, 93.29, and 92.74 at clearances of 0 m, 0.00001 m, and 0.00003 m respectively.

A Study of the Life Test of Hydraulic Pump Driving Gear Box for the Large Excavator (초대형 굴삭기용 유압펌프 구동 기어박스의 수명시험에 관한 연구)

  • Lee, Yong Bum
    • Journal of Advanced Marine Engineering and Technology
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    • v.39 no.3
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    • pp.211-216
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    • 2015
  • Large hydraulic excavator weighted 90 tons used the several pumps installed in parallel to use the hydraulic pump driving gearbox to improve fuel consumption by improving the energy efficiency of the hydraulic system. Gearbox connected to hydraulic pump supply the mechanical output to the high pressure and low pressure pump to be supplied by torque and rotation, which are the mechanical power, through a input shaft connected to large size engine of the excavator. So, gearbox connected to hydraulic pump is same as main artery in the human body and is required long life because it operates the hydraulic pump continuously during operating the engine. This study had used oil contamination analysis method to check the wear characteristics of the gearbox and frequency response characteristic analysis method to check the failure of the teeth failures of gearbox, while the test equipment adopted by the electrical feedback method to reduce the energy consumption was operating for the life assessment, in which the required power was 600 kW input power.

보일러 급수 펌프의 과도진동 연구 사례 - 실험 및 신호처리를 중심으로 -

  • Kim, Jeung T.;Lim, Byung-Duk;Lee, Hyun
    • Journal of KSNVE
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    • v.1 no.2
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    • pp.129-140
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    • 1991
  • The boiler feed pump located at a power plant has been experienced a severe vibration since the plant began to service in early 1980. The research is focused on the field measurement and implementation of simple signal processing techniques in order to provide realistic and effective solution which could be implemented into the plant. Based on the root cause analysis for the trouble-making pump system, the driving part gear in the fluid coupling system is identified as a potential source. The followed verification test confirms the analytical result. The test result shows that vibration reduction obtained after the gear replacement reaches up 15.8 dB, which is 1/6 times of the vibration level compared to that of the troble-making pump. The measured vibration level of the pump satisfies the manufacture criteria and guarantees the smoothed operation.

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A Study for Numerical Analysis of Flow Variation on Low Pressure Fuel Pump Fluid using Excavator Engine (굴삭기 엔진용 저압연료펌프 유체의 유동변화에 대한 수치해석적 연구)

  • Lee, IL Kwon;Kim, Seung Chul
    • Journal of the Korean Institute of Gas
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    • v.19 no.6
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    • pp.47-53
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    • 2015
  • This paper is to study applying for numerical analysis method for flow field, velocity and pressure of fuel on the low pressure pump using excavator. The pressure distribution of fuel pump certified the linear variation according to rotation angle of rotor. Especially, it knew the fact that the pressure in rotation angle $40^{\circ}$ appeared high outlet and low inlet of fuel pump. Also, this range angle can seek the fact that the leakage flow and velocity are the most increasing. And the more rotor rotation of fuel pump, the more mean outlet flow rate increased in linear. Whenever the gap size decrease with rotor and housing, the discharge flow rate could seek the approaching 0.0712kg/s that consider with theory discharge flow rate calculated from displacement between rotor gear and idle gear.

A Research for the Noise Development of the FF 8th Speed Automatic Transmission (전륜 8속 자동변속기 소음 개발에 대한 연구)

  • Lee, Hyun Ku;Hong, Sa Man;Kim, Moo Suk;Hur, Jin Wook;Yoo, Dong Kyu
    • Transactions of the Korean Society for Noise and Vibration Engineering
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    • v.26 no.5
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    • pp.559-566
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    • 2016
  • This study shows a development procedure and results of noise reduction for a new developed FF 8th speed automatic transmission. Based on planetary gear operating frequency analysis using PTA(planetary transmission analysis) program developed in 2012, It is expected that gear noise of the rear planetary gear set could be recognized easily in the concept design stage. Therefore, pRMC (planetary run many cases) analysis program that is developed in 2012 was applied to minimize the planetary gear noise level and noise distributions versus torque. To minimize noises coming from oil pump and final gears of a new transmission, several changes were applied, such as changing the clearance of double angular ball bearing, the oil pump rotor tooth number from 9 to 11 and the oil pump type from parachoid to megafloid and so on. Besides, stiffness values of the transmission case and the mount bracket were measured and reinforced properly. Finally, The total noise of the new FF 8th speed automatic transmission was developed successfully. Furthermore, E.O.L. testers also have been adapted to control the noise quality of automatic transmission assembly in the manufacturing factory. This paper could provide practical solutions to the automatic transmission NVH problems.

A Study on the Three-dimensional Gear Modeling for CAD/CAM (CAD/CAM을 위한 3차원 기어 모델링에 관한 연구)

  • 주만식;김민주;이승수;전언찬
    • Proceedings of the Korean Society of Precision Engineering Conference
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    • 1997.10a
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    • pp.1008-1012
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    • 1997
  • This study is on a mathematical model of profile shifted involute gear, and this model is based on Camus's theory. Gear is general mechanical elements that used for power transmission between two shafts that interval is comparatively short. and it delivers bit power as accurate ratio of speed. The profile of Spur gear which is the most basic factor is divided into Trochoidal fillet curve and Involute curve. Involute curve is used a lot of a shape curve of machine parts such as a gear, a scroll compressor and a collar of centrifugal pump. However, It is poor to study the modeling of Trochoidal fillet curve and the three dimensions model shaped mathematical curve. So we draw three dimensions gear have accurate mathematical function using ADS(Automatic Drawing system), VisualLISP. To check accuracy and perfection, we make a program of checking Interference. and use for this study.

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