• 제목/요약/키워드: Gas-turbine

Search Result 1,630, Processing Time 0.029 seconds

Performance Analysis of a Gas Turbine for Power Generation Using Syngas as a Fuel (Syngas를 연료로 사용하는 발전용 가스터빈의 성능해석)

  • Lee, Jong-Jun;Cha, Kyu-Sang;Sohn, Jeong-Lak;Joo, Yong-Jin;Kim, Tong-Seop
    • Transactions of the Korean Society of Mechanical Engineers B
    • /
    • v.32 no.1
    • /
    • pp.54-61
    • /
    • 2008
  • Integrated Gasification Combined Cycle (IGCC) power plant converts coal to syngas, which is mainly composed of hydrogen and carbon monoxide, by the gasification process and produces electric power by the gas and steam turbine combined cycle power plant. The purpose of this study is to investigate the influence of using syngas in a gas turbine, originally designed for natural gas fuel, on its performance. A commercial gas turbine is selected and variations of its performance characteristics due to adopting syngas is analyzed by simulating off-design gas turbine operation. Since the heating value of the syngas is lower, compared to natural gas, IGCC plants require much larger fuel flow rate. This increases the gas flow rate to the turbine and the pressure ratio, leading to far larger power output and higher thermal efficiency. Examination of using two different syngases reveals that the gas turbine performance varies much with the fuel composition.

Introduction For Gas Turbine Electric Propulsion LNGC (GAS TURBINE ELECTRIC PROPULSION LNG선 소개)

  • Yeo, Dong-Il
    • Proceedings of the Korean Society of Marine Engineers Conference
    • /
    • 2006.06a
    • /
    • pp.27-28
    • /
    • 2006
  • 최근 LNG 연료 시장의 호황에 힘입어 LNG선들이 점차 대형화 추세에 있고, LNG선의 추진 기관 또한 경제성, 환경 영향 등의 주어진 요구 환경에 따라 다양화 되고 있다. 기존의 Steam Turbine Propulsion 외에 Conventional 2-stroke Diesel Engine 및 Dual-fuel 4-stroke Diesel Engine of LNG선의 주 기관으로서 이미 상용화 되었고, 기술적/경제적인 이유로 일반 상선의 주기관으로서는 논외에 있었던 Gas Turbine 또한 일부 Oil Major와 Gas Turbine Maker에 의해 그 적용 가능성이 논의되고 있다. 이에 따라 LNG 선에 Gas Turbine 적용 타당성, 고려 사항 및 적용에 따른 이점과 단점 등을 고찰하였다.

  • PDF

ANALYSIS OF FLUID CHARACTERISTICS OF THRUST BEARING ON MILLIMETER-SCALE MICRO GAS TURBINE (초소형 가스 터빈용 스러스트 베어링 내의 유동특성 해석)

  • Seo, J.H.;Baek, J.H.
    • 한국전산유체공학회:학술대회논문집
    • /
    • 2010.05a
    • /
    • pp.258-262
    • /
    • 2010
  • Since MEMS based micro actuators or generating devices showed high efficiency per volume, plenty of research are ongoing. Among them, MEMS based millimeter-scale micro gas turbine is one of the most powerful item for replacing chemical batteries. However, due to MEMS manufacturing technique, it is very difficult that makes wide turbine bearing area. It causes low DN number, so sufficient bearing force is hard to achieve. Thus, the most important issue on micro gas turbine is to design the proper bearing which can keep rotor stable during operation. In order to that, micro-scale gas-lubricated bearing is generally used. In this paper, basic feasibility study of thrust bearing of 10mm diameter turbine is described. Thrust bearing is hydrostatic gas-lubricated type. Numerical simulation is performed with ANSYS CFX 11.0 which is commercial numerical tool. Relationship between bearing inlet pressure and mass flow rate and bearing force is figured while changing bearing gap and number of capillaries. The simulation results will be used for further design of micro gas turbine.

  • PDF

A Study on Repair Case of Journal and Bearing Damage for 25MW Industrial Gas Turbine (25MW급 산업용 가스터빈의 저널과 베어링 손상 보수사례에 관한 연구)

  • Kim, Byung Ok;Sun, Kyung Ho;Lee, An Sung
    • The KSFM Journal of Fluid Machinery
    • /
    • v.15 no.6
    • /
    • pp.64-69
    • /
    • 2012
  • This paper deals with the study on repair case of journal shaft and bearing damage in 25MW industrial gas turbine caused by sudden blackout, operation mistake, and logic abnormal, etc. When a serious accident such as journal and bearing damage in a gas turbine occurs, the domestic local companies having the gas turbine are dependent on manufacturer for all maintenance and repair schedule until now. This case study shows that the damaged gas turbine is normally re-operated itself in domestic by establishing repair schedule in a short period of time, repairing damage journal shaft and tilting pad bearings, and performing rotating test for a reliability check. This paper can be regarded as the important case study of emergency test run experience of the refurbished 25MW gas turbine rotor.

Design of a New 2-DOF PID Controller for Gun-san Gas Turbine Generation Plant

  • Kim, Dong-Hwa
    • Journal of KIEE
    • /
    • v.10 no.1
    • /
    • pp.16-22
    • /
    • 2000
  • The Main role of the gas turbine lies in the utilization of waste heat which may be found in exhaust gases from the gas turbine or at some other points of the process to produce additional electricity. Up to date, the PID controller has been used to operate under such difficult conditions, but since the gain of PID controller manually experience. In this paper parameter separation type 2-DOF PID controllers are proposed based on the gas turbine control system. Gas turbine transfer function is achieved from operation data of Gun-san gas turbine and Tuning algorithms of parameter separation type 2-DOF PID controller is ANFIS. Results represents satisfactory response.

  • PDF

Performance Evaluation of the Gas Turbine for Integrated Ossification Combined Cycle (석탄가스화 복합발전용 가스터빈의 성능 평가)

  • Lee, Chan;Lee, Jin-Wook;Yun, Yong-Seung
    • The KSFM Journal of Fluid Machinery
    • /
    • v.2 no.1 s.2
    • /
    • pp.7-14
    • /
    • 1999
  • This simulation method is developed by using GateCycle code for the performance evaluation of the gas turbine in IGCC(Integrated Gasification Combined Cycle) power plant that uses clean coal gas fuel derived from coal gasification and gas clean-up processes and it is integrated with ASU(Air Separation Unit). In the present simulation method, thermodynamic calculation procedure is incorporated with compressor performance map and expander choking models for considering the off-design effects due to coal gas firing and ASU integration. With the clean coal gases produced through commercially available chemical processes, their compatibility as IGCC gas turbine fuel is investigated in the aspects the overall performance of the gas turbine system. The predictions by the present method show that the reduction of the air extraction from gas turbine to ASU results in a remarkable increase in the efficiency and net power of gas turbines, but it is accompanied with a shift of compressor operation point toward to surge limit. In addition, the present analysis results reveal the influence of compressor performance characteristics of gas turbine have to be carefully examined in designing the ASU integration process and evaluating the overall performance parameters of the gas turbine in IGCC Power plant.

  • PDF

Study on the Closed-die Forging Process for Turbine Disk of Small Gas Turbine Engine (소형 가스터빈용 터빈 디스크의 형단조 공정 연구)

  • Kim, D.K.;Kim, Y.D.;Kim, D.Y.
    • Proceedings of the Korean Society for Technology of Plasticity Conference
    • /
    • 2007.05a
    • /
    • pp.427-430
    • /
    • 2007
  • Gas turbine disk components have been used by Ni-base superalloys which have high temperature strength for enduring stress induced by high speed rotation. This study introduced the overview of development strategy of precision forging of turbine disk and closed-die forging process for manufacturing good quality gas turbine disk. To make superior quality turbine disk, it is important to select optimal forging process conditions like preform shape, die shape and forging temperature etc. In this paper, closed-die forging process has been studied through the rigid-plastic finite element simulation. Proposed forging process can be used for the successful manufacturing of small-size gas turbine disk.

  • PDF

Effect of Boundary Conditions on Internal Coolant Flow in Gas Turbine Blades (경계 조건이 가스터빈 블레이드 냉각공기 유량에 미치는 영향)

  • Shin, Jee-Young;Park, Byung-Kyu
    • Proceedings of the KSME Conference
    • /
    • 2001.06d
    • /
    • pp.559-564
    • /
    • 2001
  • Advanced gas turbine engines employ turbine entry temperatures so high that cooling of the turbine blades is essential. The coolant flow introduces losses which need to be minimized, and therefore it is important that the minimum amount of coolant is used. This work presents the result of the one-dimensional analysis and the effect of the boundary conditions on coolant flow rate in gas turbine blades.

  • PDF

Effect of Boundary Condition on the Flow Rate of the Internal Coolant in Gas Turbine Blades (경계조건에 따른 가스터빈 블레이드 냉각공기 유량변화)

  • 신지영;박병규
    • Korean Journal of Air-Conditioning and Refrigeration Engineering
    • /
    • v.13 no.9
    • /
    • pp.888-894
    • /
    • 2001
  • Advanced gas turbine engines employ turbine entry temperatures so high that cooling of the turbine blades is essential. The coolant flow introduces losses which need to be minimized, and therefore it is important that the minimum amount of coolant should be used. This work presents the result of the one-dimensional analysis and the effect of the boundary conditions on coolant flow rate in gas turbine blades.

  • PDF