• 제목/요약/키워드: Gas-gas heater

검색결과 304건 처리시간 0.026초

단층 탄소나노튜브의 일산화질소 가스에 대한 감응특성과 열처리 효과 (NO Gas Sensing Characteristics of Single-Walled Carbon Nanotubes and Heating Effect)

  • 김민주;윤광현;허증수
    • 센서학회지
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    • 제13권4호
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    • pp.292-297
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    • 2004
  • Carbon nanotubes (CNT) were synthesized by arc-discharge method. To fabricate CNT sensor, CNT powder was dispersed in ${\alpha}$-Terpinol($C_{10}H_{17}OH$) solution. The CNT tilms were fabricated by screen printing method on the interdigitated Pt/Pd alloy electrode. The microstructure of CNT film was observed by scanning electron microscopy (SEM) and transmission electron microscopy (TEM). In order to investigate the gas sensing characteristics of the film, the CNT film was experimented to measure NO response and recovery time. The CNT sensor with a heater was compared to that without a heater. And this sensor shows better reproductibility and faster recovery time than another CNT sensors. We suggest the possibility to utilize a CNT as new sensing materials for environmental monitoring.

히트파이프를 이용한 온풍난방기 배기열회수 시스템의 열회수 특성 (Heat Recovery Characteristics of the Exhaust Heat Recovery System with Heat Pipe Unit Attached to the Hot Air Heater in the Greenhouse)

  • 강금춘;김영중;유영선;백이;이건중
    • Journal of Biosystems Engineering
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    • 제26권5호
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    • pp.441-448
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    • 2001
  • Hot air heater with light oil combustion is used as the most common heater for greenhouse heating in the winter season. However, exhaust gas heat discharged to atmosphere through chimney reaches up to 10~20% of total heat capacity of the oil burred. In order to recover the heat of this exhaust gas and to use for greenhouse heating, the heat pipe type exhaust heat recovery system was manufactured and tested in this experiment. The system consisted of a heat exchanger made of heat pipes, ø15.88${\times}$600mm located in the rectangular box of 675(L)${\times}$425(W)${\times}$370(H)mm, an air suction fan and air ducts. The number of heat pipe was 60, calculated considering the heat exchange amount between exhaust gas and air and heat transfer capacity of a heat pipe. The working fluid of heat pipe was acetone because acetone is known for its excellent heat transfer capacity. The system was attached to the exhaust gas path. According to the performance test it could recover 53,809 to 74,613kJ/h depending on the inlet air temperature of 12 to -12˚at air flow rate of 1.100㎥/h. The temperature of the exhaust gas left the heat exchanger dropped to 100$^{\circ}C$ from 270$^{\circ}C$ after the heat exchange between the suction air and the exhaust gas.

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가속시험을 이용한 가스 센서 신뢰성 (Reliability Analysis of Gas Sensor Based on ALT)

  • 김종걸;채수근;강규섭
    • 한국신뢰성학회:학술대회논문집
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    • 한국신뢰성학회 2000년도 추계학술대회
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    • pp.235-241
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    • 2000
  • 가스기기 안전장치 및 조리기구에 중요한 안전장치인 Gas Sensor를 가속시험을 이용하여 신뢰성을 분석하였다. 시험을 실시한 결과 GAS SENSOR의 Heater는 인가전압에 따른 특성 변화가 아레니우스 모델과 어링모델이 잘 일치함을 보여주었다. 즉, Heater선의 전압은 발열온도에 비례하고 있음을 알 수 있었다. 이번 실험을 통하여 STRESS에 비례적으로 특성이 변하는 제품은 설계단계에서 수명에 영향을 주는 잠재적 취약부를 단시간에 효과적으로 끌어내어 개선할 수 있는 기술임을 입증하였으나 다양한 STRESS의 복합적인 인자에 의하여 변화되는 특성을 분석하여 실질적으로 현장실무에 활용을 위해서는 많은 기술적 보안이 필요할 것으로 판단된다.

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다이아프램 구조를 이용한 탄소나노튜브 가스 센서의 가스 감응 특성 (Gas sensing characteristics of carbon nanotube gas sensor using a diaphragm structure)

  • 조우성;문승일;김영조;박정호;주병권
    • 센서학회지
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    • 제15권1호
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    • pp.13-19
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    • 2006
  • The micro-gas sensor based on carbon nanotubes (CNTs) was fabricated and its gas sensing characteristics on nitrogen dioxide ($NO_{2}$) have been investigated. The sensor consists of a heater, an insulating layer, a pair of contact electrodes, and CNT-sensing film on a micromachined diaphragm. The heater plays a role in the temperature change to modify sensor operation. Gas sensor responses of CNT-film to $NO_{2}$ at room temperature are reported. The sensor exhibits a reversible response with a time constant of a few minutes at thermal treatment temperature of $130^{\circ}C$.

초음속 유도무기 지상 시험용 가열기 개념 설계 (Concept Design on Heating System for Supersonic Air-Breathing Engine Test Facility)

  • 한풍규;남궁혁준;이경훈;김영수
    • 한국추진공학회:학술대회논문집
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    • 한국추진공학회 2006년도 제26회 춘계학술대회논문집
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    • pp.321-326
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    • 2006
  • 초음속 유도무기에 사용되고 있는 공기흡입 추진기관의 지상 연소시험에서 요구되는 700K-6바의 공기를 공급하기 위한 Vitiated형 공기 가열기에 대한 개념설계를 수행하였다. 본 가열기는 여분의 기체 산소와 공기를 혼합하는 예혼합기, 예혼합 기체와 연료를 혼합시키는 혼합기, 점화기를 포함하는 연소실과 수축팽창 노즐, 그리고 디퓨저로 구성하였다. 가열기에 사용된 연료는 천연가스이며, 유동해석을 통해 가열기의 각 구성요소의 성능을 파악하였으며, 점화 후 화염유지가 이루지는 것을 해석적으로 확인하였다.

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온풍난방기의 배기열을 이용한 지중 난방용 온수공급시스템의 열회수특성 (Heat Recovery Characteristics of the Hot Water Supply System with Exhaust Heat Recovery Unit Attached to the Hot Air Heater for Plant Bed Heating in the Greenhouse)

  • 김영중;유영선;장진택;강금춘;이건중;신정웅
    • Journal of Biosystems Engineering
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    • 제25권3호
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    • pp.221-226
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    • 2000
  • Hot air heater with light oil burner is the most common heater for greenhouse heating in the winter season in Korea. However, since the thermal efficiency of the heater is about 80∼85%, considerable unused heat amount in the form of exhaust gas heat discharges to atmosphere. In order to capture this exhaust heat a heat recovery system for plant bed heating in the greenhouse was built and tested in the hot air heating system of greenhouse. The heat recovery system is made for plant bed or soil heating in the greenhouse. The system consisted of a heat exchanger made of copper pipes, ${\Phi}12.7{\times}0.7t$ located in the rectangular column of $330{\times}330{\times}900mm$, a water circulation pump, circulation plastic pipe and a water tank. The total heat exchanger area is 1.5$m^2$, calculated considering the heat exchange amount between flue gas and water circulated in the copper pipes. The system was attached to the exhaust gas path. The heat recovery system was designed as to even recapture the latent heat of flue gas when exposing to low temperature water in the heat exchanger. According to the performance test it could recover 45,200 to 51,000kJ/hr depending on the water circulation rates of 330 to $690\ell$/hr from the waste heat discharged. The exhaust gas temperature left the heat exchanger dropped to $100^{\circ}C$ from $270^{\circ}C$ by the heat exchange between the water and the flue gas, while water gained the difference and temperature increased to $38^{\circ}C$ from $21^{\circ}C$ at the water flow rate of $690\ell$/hr. By the feasibility test conducted in the greenhouse, the system did not encounter any difficulty in operations. And, the system could recover 220,235kJ of exhaust gas heat in a day, which is equivalent of 34% of the fuel consumption by the water boiler for plant bed heating of 0.2ha in the greenhouse.

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수소가스 감지용 가연성 가스센서 제작을 위한 요소기술 개발 (Development of Core Technologies for Integrating Combustible Hydrogen Gas Sensor)

  • 윤의중;박형식;이석태;박노경
    • 한국전기전자재료학회논문지
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    • 제20권3호
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    • pp.228-233
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    • 2007
  • Core technologies for integrating hydrogen gas sensor were investigated. In this study, the thermally isolated micro-hot-plate with areas of $100{\times}100-260{\times}260{\mu}m^2$ was fabricated by utilizing surface micromachining technique that provides better manufacturing yield than bulk micromachining counterpart. The optimum design of the sensor was peformed by analyzing the thermal profile of the structure obtained from a ANSYS simulator. The 400-nm-thick polysilicon films doped with phosphorus, the 300-nm-thick aluminum films, and the 200-nm-thick $SnO_2$(or ZnO)films were used as the micro-heater material, the temperature sensor material, and the gas sensitive material, respectively. The experimental results show that the developed gas sensors can detect $H_2$ concentration as low as 1 ppm.

석탄화력 탈황설비 Non-leakage Type Gas-Gas Heater(GGH) 운영 및 개선사례 (Operation and Improvement Cases of FGD Non-leakage Type Gas-Gas Heater(GGH) for Coal Fired Power Plants)

  • 성기종;이창식
    • 한국연소학회지
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    • 제22권4호
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    • pp.35-42
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    • 2017
  • This case covers the issues related to the operation problem, cause analysis and improvement cases of the FGD that employed the non-leakage type GGH in coal-fired power plant for the first time in Korea. In the Cooler, there was a main problem that the tube is damaged by the ash cutting due to the high velocity of flue gas in the duct and by the weak wear resistance of material. In the Reheater, there was a main problem that the tube was corroded due to chlorine and sulfur in the circumstance of the low temperature. In order to solve those problems, we have improved the Reheater tube and tube fins by coating enamel to reduce corrosion rate.