• 제목/요약/키워드: Friction Flow Loss

검색결과 187건 처리시간 0.034초

신발형 리브의 형상변화가 열전달 및 압력 강하에 미치는 영향 (Effects of Geometry of a Boot-Shaped Rib on Heat Transfer and Pressure Drop)

  • 서재원;김준희;김광용
    • 한국유체기계학회 논문집
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    • 제18권3호
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    • pp.66-73
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    • 2015
  • This paper deals with a parametric study on boot-shaped ribs in a rectangular cooling channel. Numerical analysis of the flow and heat transfer was performed using three-dimensional Reynolds averaged Navier-Stokes equations with the Speziale, Sarkar and Gatski turbulence model. The parametric study was performed for the parameters, tip width-to rib width, tip height-to-rib height, rib height-to-channel height, and rib height-to-width ratios. To assess the cooling performance and friction loss, Numsselt number and friction factor were defined as the performance parameter, respectively. The results showed that the cooling performance and friction loss were seriously affected by the four geometric parameters.

Development and validation of wall and interfacial friction models in LOCUST for reactor downcomer with direct vessel injection

  • Rongshuan Xu;Xinan Wang;Caihong Xu;Dongyu He;Ting Wang;Jinggang Li
    • Nuclear Engineering and Technology
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    • 제56권10호
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    • pp.4397-4403
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    • 2024
  • The multi-dimensional thermal-hydraulic phenomena in the downcomer of advanced pressurized water reactor with direct vessel injection system are the key points for the safety analysis during a loss of coolant accident. In order to improve the accuracy of LOCUST code for the predictions of thermal-hydraulic phenomena in downcomer region, some newly correlations have been implemented into LOCUST code. The wall friction model of LOCUST code was modified based on the correlations which developed by Yang. The interfacial friction models in LOCUST code have been modified as Hibiki-Ishii correlations. In addition, in order to simulate the upward flow of recirculation flow in downcomer region, the Kinoshita-Hibiki correlations have been also implemented into LOCUST code for better simulating the recirculation flow in downcomer region. The modified code was validated with experimental data of DOBO facility. Five tests of DOBO facility have been calculated by LOCUST, and the calculated axial void fraction distributions have been compared with the measurements. The results show that the modified LOCUST with new correlations of distribution parameter and drift velocity shows better accuracy than the original code. The deviations of the modified LOCUST code are less than the original code and are almost within ±20 %.

박용엔진 피스톤 스커트 프로파일 변경에 의한 마찰손실(FMEP) 저감 연구 (Friction Power Loss Reduction for a Marine Diesel Engine Piston)

  • 안성찬;이상돈;손정호;조용주
    • Tribology and Lubricants
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    • 제32권4호
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    • pp.132-139
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    • 2016
  • The piston of a marine diesel engine works under severe conditions, including a combustion pressure of over 180 bar, high thermal load, and high speed. Therefore, the analyses of the fatigue strength, thermal load, clamping (bolting) system and lubrication performance are important in achieving a robust piston design. Designing the surface profile and the skirt ovality carefully is important to prevent severe wear and reduce frictional loss for engine efficiency. This study performs flexible multi-body dynamic and elasto-hydrodynamic (EHD) analyses using AVL/EXCITE/PU are performed to evaluate tribological characteristics. The numerical techniques employed to perform the EHD analysis are as follows: (1) averaged Reynolds equation considering the surface roughness; (2) Greenwood_Tripp model considering the solid_to_solid contact using the statistical values of the summit roughness; and (3) flow factor considering the surface topology. This study also compares two cases of skirt shapes with minimum oil film thickness, peak oil film pressure, asperity contact pressure, wear rate using the Archard model and friction power loss (i.e., frictional loss mean effective pressure (FMEP)). Accordingly, the study compares the calculated wear pattern with the field test result of the piston operating for 12,000h to verify the quantitative integrity of the numerical analysis. The results show that the selected profile and the piston skirt ovality reduce friction power loss and peak oil film pressure by 7% and 57%, respectively. They also increase the minimum oil film thickness by 34%.

비공비 혼합냉매 R-410A를 적용한 납작한 알루미늄 마이크로 멀티 튜브에서의 마찰손실에 관한 연구 (A study on the friction head loss in flat aluminum micro multi tubes with nonazeotropic refrigerant mixtures R-410A)

  • 이정근;민경호
    • Design & Manufacturing
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    • 제13권2호
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    • pp.37-43
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    • 2019
  • This study conducted a research as to condensation heat transfer friction loss headby using three types of flat micro multi-channel tubes with different processing of micro-fin and number of channels inside the pipes and different sizes of appearances. In addition, identical studies were conducted by using smoothing circular tubes with 5mm external diameter to study heat enhancement factor and pressure drop penalty factor. 1) The friction head loss showed an increase as the vapor quality and mass flux increased. In case of saturation temperature, it shows an increase as it gets lower. These factors are the reason occurring as the lower the saturation temperature is, the higher the density of refrigerant vapor gets. The influence of heat flux is similar as the dryness is low, but as it gets higher, it lowers in heat flux, and as the high temperature of high heat flux, it is a factor that occurs as the density gets lower. 2) RMS error of the in case of friction head loss, it showed to be predicted as 0.45~0.67 by Chisholm, Friedel, Lockhart and Martinelli. 3) As forfriction head loss penalty factor, the smaller the aspect ratio is, the larger the penalty factor gets, and as for the effect of micro-fin, the penalty factor increased because it decreases to the gas fluid the way groove for the refrigerant's flow.

콜부르크-화이트 방정식의 수치해와 이의 적용 (Numerical Solution of Colebrook-White Equation and It's Application)

  • 김민환;송창수
    • 상하수도학회지
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    • 제19권5호
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    • pp.613-618
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    • 2005
  • In analysis of pipelines or pipe network we calculated the friction loss using Hazen-Williams or Manning formula approximately, or found one by friction coefficient from Moody diagram graphically. The friction coefficient is determined as a function of relative roughness and Reynolds number. But the calculated friction coefficient by Hazen-Williams or Manning formula considered roughness of pipe or velocity of flow. The friction coefficient in Darcy-Weisbach equation was obtained from the Moody diagram. This method is manual and is not exact from reading. This paper is presented numerical solution of Colebrook-White formula including variables of relative roughness and Reynolds number. The suggested subroutine program by an efficient linear iteration scheme can be applied to any pipe network system.

채널의 분기 및 병합이 있는 액체로켓 연소기 재생냉각 유로에서의 수력학적 특성 (Hydraulic Characteristics of Branching and Merging of Channels in Regenerative Cooling Passage in Liquid Rocket Combustors)

  • 김홍집;김성구;최환석
    • 한국항공우주학회지
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    • 제36권11호
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    • pp.1087-1093
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    • 2008
  • 고성능 로켓엔진용 연소기에서 열적 건전성을 확보하기 위해 적용되는 재생냉각 채널은 채널의 분기/병합, 방향 전환과 같이 복잡한 유동구조를 포함한다. 냉각유로에서 발생하는 압력 손실을 마찰과 국소유동저항으로 나눠, 각각의 유동조건에 따라 경험적으로 제시된 문헌상의 계수를 적용함으로써, 재생냉각유로 설계에 효과적으로 적용할 수 있도록 수력학적 자료를 구하였다. 해석의 타당성을 검증하기 위하여 실물형 연소기의 냉각유로 설계안에 적용하였다. 먼저, 물을 사용하였을 때 모사시제를 사용한 수류시험 결과와 비교하였다. 정량적으로 타당한 결과를 얻은 것으로 확인되어, 실유체인 케로신을 사용한 수력해석을 수행하여 CFD 결과와 비교하여 수력해석 방법의 타당성을 확인할 수 있었다.

지지격자가 있는 봉다발과 축방향으로 평행한 유동의 압력손실에 관한 실험적 연구 (Experimental Study on Pressure Loss of Flow Parallel to Rod Bundle with Spacer Grid)

  • 이치영;신창환;박주용;인왕기
    • 대한기계학회논문집B
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    • 제36권7호
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    • pp.689-695
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    • 2012
  • 지지격자가 있는 봉다발과 축방향으로 평행한 유동에서, 봉다발 마찰계수와 지지격자 손실계수를 평가하였다. 시험부는 외경 9.5 mm, 길이 2000 mm 인 봉 25 개를 $5{\times}5$ 정사각 구조로 배열하여 제작하였으며, 봉 중심간 거리와 봉 외경의 비는 1.35 였다. 지지격자로는 plain 지지격자, split-vane 지지격자, hybrid-vane 지지격자를 이용하였다. 지지격자가 없는 봉다발의 마찰계수는 기존 상관식과 비교적 잘 일치하였다. 지지격자가 있는 봉다발 실험의 경우, hybrid-vane 지지격자에서 봉다발 마찰계수 및 지지격자 손실계수가 가장 크게 측정되었으며, 이는 지지격자의 유동단면 막음비 증가와 혼합날개 형상에 의한 유동 교란이 증가되기 때문인 것으로 판단된다. Re=$5{\times}10^5$ 조건에서 plain 지지격자, split-vane 지지격자, hybrid-vane 지지격자의 손실계수는 약 0.79, 0.80, 0.88 로 예측되었다.

극저비속도 원심펌프의 불안정성능개선 및 소형화에 관한 연구 (Improvement of Performance Instability and Miniaturization of Very Low Specific Speed Centrifugal Pump)

  • 최영도;쿠로카와준이치
    • 한국유체기계학회 논문집
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    • 제10권4호
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    • pp.21-28
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    • 2007
  • The ratio of disk friction loss in a centrifugal pump is very large for the total pump loss in the range of very low specific speed. Therefore, impeller radius should be shortened to increase the pump efficiency because the disk friction loss is proportional to the fifth power of impeller radius. In order to compensate the decreased head by the shortened impeller radius, vane angle at impeller outlet should be increased. However, as the vane angle at impeller outlet becomes larger, performance instability occurs at low flow rate regions. In this study, J-Groove is adopted to suppress the performance instability and detailed examination is performed for the influence of the J-Groove on the pump performance. The results show that J-Groove gives good effect on the suppression of performance instability. Moreover, as J-Groove increases pump head considerably, the pump size can be smaller for head requirements.

등압법과 T-method를 이용한 공조시스템 배관 설계에 관한 연구 (A Study on the Duct Design of HVAC System Using the Equal Friction Method and the T-method)

  • 박준석;최길환;조대승
    • 대한조선학회논문집
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    • 제46권4호
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    • pp.435-443
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    • 2009
  • Optimal duct design of a HVAC system requires analysis technology to accurately evaluate its pressure losses, flow rate and velocity for making a compromised design among fan capacity and duct size affecting initial manufacturing and operation costs, and noise induced by the HVAC system. In this paper, we carry out initial duct design using the equal friction method. Using the result, the T-method is applied for accurate analysis of flow rate. Then, the duct size is modified using the difference between the required and the calculated flow rate, which can guarantee required flow rate, reduce the pressure unbalance among duct paths and lead to select optimal fan performance. To verify the validity and effectiveness of the proposed design method, an example for HVAC system design including noise analysis is demonstrated.

컴퓨터를 이용한 회주철의 탕구방안 설계에 관한 연구 (A study on the computed aided gating design in gray cast iron)

  • 최정길;김동옥
    • 한국주조공학회지
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    • 제6권1호
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    • pp.27-35
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    • 1986
  • The gating design of gray cast iron was programmed in a Personal computer. By this program, casting test was done. The results obtained are as follows. 1. Gating design that can calculate the velocity of metal flow and size in each gate section by knowing the loss coefficient caused by friction loss and bend loss was programmed. 2. In the test casting, the gating ratio was changed into 1.1:1.3:1, 1:2:2, 1:4:4. And sound casting, free of sand washing defect, was obtained at the velocity of 35.5cm/sec in ingate.

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