• Title/Summary/Keyword: Fixed Mandrel

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Die Design for Shape Drawing to Improve the Dimensional Accuracy of a Hollow LM-Guide Rail (중공형 LM-Guide Rail의 치수정밀도 향상을 위한 형상인발 금형 설계)

  • Park, J.H.;Lee, K.H.;Kim, S.M.;Kim, H.J.;Kim, S.J.;Kim, B.M.
    • Transactions of Materials Processing
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    • v.24 no.5
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    • pp.340-347
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    • 2015
  • Multi-pass shape drawing is used to manufacture long products of arbitrary cross-sectional shapes. This process allows smooth surface finishes and closely controlled dimensions of the cross-sectional shape. Tube shape drawing for hollow type products provides material savings and weight reduction. The intermediate die shapes are very important in multi-pass tube shape drawing. In the current paper, the design method for the intermediate dies in a tube shape drawing process is developed using a die offset for corner filling (DOCF) method. Underfill defects are related to the radial velocity distribution of each divided section in the deformation zone. The developed intermediate die shape design was applied to the two-pass tube shape drawing with fixed mandrel for manufacturing a hollow linear motion (LM) guide rail. The proposed design method led to uniform and steady metal flow at each divided section. FE-simulations and experiments were conducted to validate the effectiveness of the proposed method in multi-pass tube shape drawing process.

Analysis of Deformation of Brass Tube Drawn By Various Methods (인발 방법에 따른 황동관의 변형 해석)

  • ;Oh Kyu Hwan;Lee Dong Nyung
    • Proceedings of the Korean Society for Technology of Plasticity Conference
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    • 1995.10a
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    • pp.76-85
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    • 1995
  • The general equation of homogeneous strin for tube drawing has been derived. This can be applied to the general tube drawing method for non-zero plug angle. Also, the derived equation can represent Blazynski's equations for the sinking and tube drawing with a constant plug diameter. The general tube drawing was divided into two steps, sinking and contact drawing zones. The derived equation can calculate the homogeneous strains of the two steps. The various tube drawing methods such as fixed tapered plug, fixed mandrel, fixed back tapered plug, and floating plug have been analysed by the equation and finite element analysis. From the FEM calculations, the total strains and drawing stresses are obtained and consequently the redundancy factor of various drawing methods was analysed. The fixed back tapered plug method showed the largest redundancy factor and the floating plug method had the largest drawing stress.

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A Study on the Manufacturing Processability of Automatic Winding Device for Manufacturing Strand Specimens (스트랜드 시편 제작 장치의 제작 공정성 연구)

  • Cha, Jae Ho;Jang, Jeong Keun;Lee, Bo Mi;Yoon, Sung Ho
    • Composites Research
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    • v.33 no.5
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    • pp.315-320
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    • 2020
  • In this study, when strand specimens were manufactured using an automatic winding device to obtain uniform strand specimens, analysis and test were conducted to investigate the effect of thermal expansion of the mandrel on strand specimens. Also, necessity of changing materials and mandrel configuration was checked. According to the results, strand specimen received unintended tension that was created by thermal expansion of the mandrel and this unintended tension depended on the curing temperature and position of specimens. Tensile test was conducted to check that initial tension affected on the performance of carbon fiber tow prepreg. All other conditions were fixed and only the initial tension was controlled at 40 N, 60 N, and 80 N. From the results of analysis and test, neither additional tension and tension deviation due to the thermal expansion of the mandrel and the initial tension difference had a significant effect on tensile test results, because carbon fiber had sufficiently high strength compared with tension. Therefore, it was confirmed that the change of the mandrel material and configuration of the automatic winding device was unnecessary.