• 제목/요약/키워드: Engine test

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한국형발사체 75톤급 엔진 개발 시험 현황 (Current Status of Development Test of 75 tonf Engine System for KSLV-II)

  • 김승한;김성룡;김성혁;김채형;서대반;우성필;유병일;소윤석;이광진;이승재;이정호;임지혁;전준수;조남경;황창환;박재영;한영민
    • 한국추진공학회:학술대회논문집
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    • 한국추진공학회 2017년도 제48회 춘계학술대회논문집
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    • pp.99-103
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    • 2017
  • 한국형발사체 1단 엔진 개발을 위한 엔진시스템 시험으로 액체산소-케로신을 추진제로 하는 75 톤급 액체로켓엔진의 연소 시험이 수행되었다. 한국형발사체 1단용 75 톤급 엔진시스템을 이용한 개발 연소시험 현황을 연소기, 터보펌프, 가스발생기, 파이로 구성품 및 공급계 부품을 포함하는 엔진시스템 연소 시험 결과를 포함하여 소개한다. 액체산소-케로신 추진제 엔진시스템의 시동 및 점화, 정상 구간 작동, 종료가 안정적으로 수행되었으며, 엔진 연소 시험 중 엔진 추력 제어 시스템의 검증 시험도 성공적으로 수행되었다. 75 톤급 엔진 연소시험 결과는 한국형발사체 1단용 엔진시스템 설계 검증 및 성능 평가에 활용될 예정이다.

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다단연소사이클 엔진 기술검증시제 개발 현황 (Development Status of Technology Demonstration Model for Staged Combustion Cycle Engine)

  • 김채형;이정호;우성필;소윤석;이승재;이광진;조남경;한영민;김진한
    • 한국추진공학회지
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    • 제23권4호
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    • pp.104-111
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    • 2019
  • 다단연소사이클 엔진은 가스발생기 기반의 개방형 엔진에 비해 성능이 좋기 때문에 현재 한국형발사체사업(KSLV-II)의 후속사업의 일환으로 선행연구가 진행 중이다. 기술검증시제 명칭의 TDM0A, TDM0B를 통해 다단연소사이클 엔진의 시동 조건과 연소 특성을 이해하고, 산화제 과잉 예연소기와 연소기 개발을 위한 연소 성능 시험이 수행되었다. 시험 데이터를 토대로 엔진 형상 모델 TDM1A를 제작하여 연소 시험을 수행했으며, 주연소기 연소압 91 bar, 터보펌프 회전수 28,000 rpm의 안정적인 결과로 개발요구조건을 만족하였다. 본 논문에서는 TDM0A부터 TDM1A까지의 개발과정과 특징에 대해 논하고자 한다.

항공기 왕복엔진 냉각설계 및 인증시험 (Cooling Design and Flight Test for Airplane Reciprocating Engine)

  • 이강이;박종혁;박성환
    • 항공우주시스템공학회지
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    • 제6권2호
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    • pp.35-41
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    • 2012
  • A reciprocating engine installed on a normal category airplane shall be effectively cooled by air flown through the engine compartment. A airplane powerplant designer has to design cooling air inlets, baffles, seals, and outlets to maintain cylinder head temperatures and oil temperature under the limits, and show compliance with appropriate airworthiness standard. In this study, cooling designs of the installed engine and compliance requirements applicable to the cooling designs were reviewed, and engine cooling flight test results were evaluated for design changes. Engine cooling certification test will be conducted in a next step.

자동차용 가솔린의 경비행기 엔진 적합성에 관한 실험적 연구 (Experimental Study of Automotive Gasolines in a Light Aircraft Engine)

  • 성낙원
    • 한국자동차공학회논문집
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    • 제3권1호
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    • pp.108-117
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    • 1995
  • The primary purpose of this extensive test effort was to observe real-time operational performance characteristics associated with automotive grade fuel utilized by piston engine powered light aviation aircraft. In fulfillment of this effort, baseline engine operations were established with 100LL aviation grade fuel followed by four blends of automotive grade fuel. A comprehensive sea-level-static test cell/flight test data collection and evaluation effort were conducted to review operational characteristics of a carbureted light aircraft piston engine as related to fuel volatility, fuel temperature, and fuel system pressure. Presented herein are results, data, and conclusions drawn from test cell engine operation as well as flight test operation on 100LL aviation grade and four blends of automotive grade fuel.

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Test System Design for Turbofan Engine Exhaust Infrared Signature Reduction Study

  • Jo, Hana;Kim, Jaewon;Jin, Juneyub
    • 항공우주시스템공학회지
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    • 제14권6호
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    • pp.85-90
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    • 2020
  • The infrared signature that is associated with an aircraft is mainly caused by heat released from the engine and the exhaust plume. In this study, a test-system was designed to observe the overall infrared signature characteristics of a turbofan engine during operation under ground running conditions and the infrared reduction features that result from different exhaust nozzle configurations. A test stand was designed for the 1400 lbf class turbofan engine that included a bell-mouth type intake, fuel supply system, a measurement system, and a data acquisition/control system. The design and verification of the test system were conducted so that the basic nozzle and various 2D nozzles could be applied to study the infrared signature produced by a turbofan engine exhaust.

자동차의 엔진 토오크 산출에 대한 연구 (A Study on Calculation of Engine Torque for Automotive)

  • 나완용
    • 한국자동차공학회논문집
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    • 제11권4호
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    • pp.211-219
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    • 2003
  • The main study experiments to obtain engine torque of the vehicle during performance test of the recent automobile. Torque was measured through the engine dynamometer to produces engine torque of the vehicle but the research method calculated engine torque of the vehicle without the engine dynamometer. The performance of the vehicle receive various running resistance. The study certificates performance of certification before a certification of used vehicle didn't carry out and certificate. This way evaluated on road test and chassis dynamometer The result of the study shows that it is much possible to apply the test. After comparing the engine torque of road driving with that of chassis dynamometer, the results are approximately the same. When rapidly speeded up, the road-load vehicle can pitch in some degrees, which may result in the fluctuations of acceleration, and then affect on the engine torque. Therefore it is confirmed that this method is easier way to measure the performance of vehicles.

초음파 연료공급장치용 디젤자동차의 성능 향상에 관한 연구(III) (과급 디젤기관에 대하여) (A Study on the Performance of Diesel Automobile Engine with Ultrasonic Fule Supply System(III) (On the case of Turbo-charging Diesel Engine))

  • 최두석;이흥영;류정인
    • 한국자동차공학회논문집
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    • 제3권4호
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    • pp.12-18
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    • 1995
  • To improve the performance of diesel automobile engine, we designed new fuel supply system named ultrasonic fuel supply system. The performance test of diesel automobile engine carried out to examine possibility of practical use of ultrasonic fuel supply system to test engine. This paper deals with the comparative results of performance test of diesel automobile engine in terms of smoke, HC, SFC, PS, thermal, efficiency, torque. Following are obtained result. 1) In naturally aspirated diesel engine, when we use ultrasonic fuel supply system output, fuel consumptions are improved and exhaust gas reduced significantly. 2) In turbo-charging diesel engine both using of ultrasonic fuel supply system and using of conventional injector, engine performance and exhaust gas temperature are almost constant. 3) In turbo-charging diesel engine, when we use ultrasonic fuel supply system, NOx are emitted approximately 3.5% higher than total average. 4) In turbo-charging diesel engine, when we use ultrasonic fuel supply system, smoke and CO are 17% and 11.8% improved respectively.

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Present Status and Further Development of Performances of Industrial Gas Turbine Engine Turbogreen 1200

  • 민대기
    • 유체기계공업학회:학술대회논문집
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    • 유체기계공업학회 1998년도 유체기계 연구개발 발표회 논문집
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    • pp.191-197
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    • 1998
  • The recent results of the engine development performed in this you on Turbogreen 1200, the first industrial gas turbine engine developed in Korea, are presented. In order to improve the engine performance and structural stability from the first prototype engine, several variants of the engine and major components such as combustor and rotor assembly have been developed and tested. This paper shows these results especially focused on the engine test and performance analysis, in which test system, instrumentation and data processing are discussed as well. The engine performance and its trend give relatively good coincidence with the design ones. At design power of 1.2MW, the thermal efficiency of the engine is estimated over $25\%$ which is below the design target of $27.2\%$. This gap of efficiency is caused mainly by large tip clearance between turbine blades and casing. Considering high design efficiency superior to those of other competitive engines in this power class, Turbogreen 1200 would have a strong competition in its performance if the design efficiency is achieved by further developments such as tip clearance control, which are very possible and natural in final mass production of the developed gas turbine engine.

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한국형발사체 7톤 파워팩 시스템 고주파 신호 분석 (The Analysis of High Frequency Signal for 7tonf-class Power Pack System of KSLV-II)

  • 소윤석;이승재;이광진;김승한;한영민
    • 한국추진공학회지
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    • 제20권3호
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    • pp.96-102
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    • 2016
  • 7톤 엔진 시험 전에 엔진 시동/정격구동/종료 특성을 확인하고자 나로우주센터 터보펌프 실매질 시험설비에서 파워팩 시험을 수행하였다. 가스발생기 연소실의 동압은 0.2 bar이하로 측정되어 연소 불안정을 발생하지 않았고, 터보펌프에 장착된 RPM 및 가속도 센서 신호 분석 결과, 예측 RPM 범위 안에서 파워팩 시험이 안정하게 수행되었다는 것을 확인하였다.

부력엔진 독립시험 모듈 해양공학수조 시험 (Buoyancy Engine Independent Test Module Test in the Ocean Engineering Basin)

  • 이종무;김형우;정태환
    • 한국산업융합학회 논문집
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    • 제26권6_2호
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    • pp.1155-1162
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    • 2023
  • The Korea Research Institute of Ships and Ocean Engineering (KRISO), which is developing the core technology for the buoyancy engine of underwater gliders, has developed a test module that can vertically ascend and descend with a buoyancy engine to verify the performance of the developed buoyancy engine. The independent test module was tested in a 15 metre deep pit in the Ocean Engineering Basin to verify its ability to ascend and descend. In order to test at a shallower depth than the real sea, it was necessary to know the negative buoyancy value during descent and the time at which the buoyancy engine would be activated. To do this, we solved the equation of motion in the vertical direction to obtain these values and applied them to the tank test. To validate the usefulness of solving the equation, we also compared the depth of descent over time measured in the test with the results calculated from the solution.