• Title/Summary/Keyword: EOH(Equivalent Operation Hour)

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Analysis of Damage Trend for Gas Turbine 1st Bucket Related to the Change of Models (모델 변천에 따른 가스터빈 1단 버켓의 손상경향 분석)

  • Kim, Moon-Young;Park, Sang-Yeol;Yang, Sung-Ho;Choi, Hee-Sook;Ko, Won;Song, Kuk-Hyun
    • Transactions of the Korean Society of Mechanical Engineers A
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    • v.31 no.6 s.261
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    • pp.718-724
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    • 2007
  • Some of gas turbine model of 7F-Class has constructed and is operating with units domestically. Non-destructive testing (NDT) is one of the methods being used to inspect damage $1^{st}$ stage bucket and review damage trends. We also analyze damage configuration and microstructure according to material and compare with pape of electric power research institute (EPRI). The damaged mode could be determined by leveraging failure analysis. Especially, configuration uprate of bucket is not only to prevent damage during operation but also avoid domestic manufacturing by the competitors. Modifications were mainly concentrated on surfaces such as cooling hole and bucket tips. Analyzing of bucket damage, the earlier model of 7F-Class used with one cycle with equivalent operation hour (EOH), has various cracking of the bucket surface. Bucket damage of new model is centered on tip area (54%) as analyzed by EPRI research. We conclude that improving bucket configuration would increase repair rate on the bucket tip.

Crack Initiation and Propagation at the Gas Turbine Blade with Antioxidation and Thermal Barrier Coating (내산화 및 열차폐 코팅처리 가스터빈 블레이드의 균열거동)

  • Kang, Myung-Soo;Kim, Jun-Sung
    • Journal of the Korean Society for Precision Engineering
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    • v.27 no.12
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    • pp.99-106
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    • 2010
  • Gas turbines operation for power generation increased rapidly since 1990 due to the high efficiency in combined cycle, relatively low construction cost and low emission. But the operation and maintenance cost for gas turbine is high because the expensive superalloy hot gas path parts should be repaired and replaced periodically This study analyzed the initiation and propagation of the crack at the gas turbine blades which are coated with MCrAIY as a bond coat and TBC as a top coat. The sample blades had been serviced at the actual gas turbines for power generation. Total 7 sets of blades were analyzed and they have different EOH(equivalent operation hour). Blades were sectioned and the cracking distribution were measured and analyzed utilizing SEM(scanning electron microscope) and optical microscope. The blades which had 52,000 EOH of operation had cracks at the substrate and the maximum depth was 0.2 mm. Most of the cracks initiated at the boundary layer between TBC and bond coat and propagated down to the bond coat. Once bond coat is cracked, the base metal is exposed to the oxidation condition and undergoes notch effect. Under this environment, the crack branched at the inter-diffusion layer and propagated to the substrate. Critical cracks affecting the blade life were analyzed as those on suction side and platform.

Mechanical Properties for Welding Part on Ni Base Superalloy Material According to Heat Treatment Parameters (열처리조건에 따른 Ni기지 초합금 용접부의 기계적 특성)

  • Yang, Sung-Ho;Park, Sang-Yeol;Choi, Hee-Sook;Ko, Won;Chae, Na-Hyun;Kim, Moon-Young
    • Transactions of the Korean Society of Mechanical Engineers A
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    • v.31 no.4
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    • pp.525-531
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    • 2007
  • The operating temperature has been increased to improve the efficiency of gas turbine. The most advanced Gas turbine is operated at above $1,500^{\circ}C$. Improvement in material and cooling method permit hot gas path component to run at increased temperature. But, the repair of blades which are developed with advanced manufacture technique is difficult to use normal welding. Most of gas turbine blades are made of precipitation harden nickel base superalloy, which is very hard to weld. Therefore, the employment of welding filler on blade is solid solution nickel base superalloy(Hastelloy X, Inconel 617). In this study, Tensile test in high temperature was conducted on welded GTD111DS with GTD111 to evaluate effect of variation of pre, post treatment. The result of this study showed that the specimen was treated with optimum pre and post treatment(preweld HT($1200^{\circ}C$), Post treatment($1100^{\circ}C$ HIP, $1200^{\circ}C$ + $1100^{\circ}C$ + $800^{\circ}C$ HT) is mush superior.