• Title/Summary/Keyword: Drill bit

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Standardization of Cautious blasting (정밀발파의 표준화(下))

  • Huh, Ginn
    • Journal of the Korean Professional Engineers Association
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    • v.23 no.6
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    • pp.41-46
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    • 1990
  • First of all, Under given condition such as bit gage of 36mm Drill bit with right class of jack-logs experimental test carried out from two face of Bench, firing of each hole brought 90 degree Angle face and them measured length of Burden and charged ammount of powder as following. (equation omitted) A=Activated Area A=ndi=m S=Peripheral length of Charged. room Ca=Rock Coeffiecency d : di=Hole diameter When constructed subway of Seoul in 1980 the blasting works increased complaint of ground vibration. in order to prevent the damage to structures. Some empirical equations were made as follows on condition with Jackleg Drill (Bit Gage ø 36mm) and within 30 meter distance between blasting site and structures. V=K(D / W)$\^$-n/ N=1.60-1.78 K=48-138 Project one of contineous works to above a determination of empirical equation on the cautious blasting vibration with Crawler Drill(ø 70-75mm) in long distance. V=41(equation omitted) V=124(equation omitted).

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Standardization of Cautious blasting (정밀발파의 표준화)

  • Huh Ginn
    • Explosives and Blasting
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    • v.8 no.3
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    • pp.3-13
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    • 1990
  • First ot of all, under given condition such as bit gage of 36mm Drill bit with right class of jack-leg-experimental test carried out from two face of Bench, firing of each hole brought 90 degree Angle face and them measured length of Burden and charged ammount of powder as following. $ca=\frac{A}{SW}$ A=Activated Area A=nd i=m S=Peripheral length of charged, room Ca=Rock Coeffiecency d: di=Hole diameter When constructed subway of Seoul in 1980 the blasting works increased complaint of ground vibration, in order to prevent the damage to structures. Some empirical equations were made as follows on condition with Jackleg Drill (Bit Gage 36mm) and within 30 meter distance between blasting site and structures. $V=K(D/W)^{-n}$ N=1.60 - 1.78 K= 48 - 138 Project is one of contineous works to above a determination of empirical equation on the cautious blasting vibration with Crawler Drill (70-75mm) in long distance. $V=41(D/\sqrt[3]{W})^{-1.41}$ $30m\le{D}\le{100m}$ $V=124(D/\sqrt[3]{W})^{-1.66}$ $100m\le{D}\le{285m}$.

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Evaluation of Pull-out Performance of Torsion Control Expansion Anchor According to Drill Bit Diameter (드릴비트 직경에 따른 비틀림 제어 확장 앵커의 인발성능 평가)

  • Kyoung-Hun Chae;Tae-Wo Park;Moo-Won Hur;Yeong-Seung An;Ju-Yeon Han
    • Journal of the Korea institute for structural maintenance and inspection
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    • v.27 no.1
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    • pp.64-70
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    • 2023
  • In this study, reliability tests of torsion control expansion anchors according to drill bit diameters were performed. The standard deviation and coefficient of variation of the anchor were reviewed through the tests for each variable, and the results were compared and evaluated with the standard test results. As a result of the reliability test of the M12 and M16 anchors with 1.04 times the drill bit diameter, they were within 20% of the ultimate tensile load permissible standard coefficient of variation. It was found that the pulling-out performance of the anchor installed in the large hole was sufficiently secured. However, it was found to be about 253% and 210% of the design strength, indicating that the pulling performance of the anchor installed in 1.04 times the drill bit diameter was sufficiently secured. As a result of the reliability test of the M12 and M16 anchors with 1.02 times the drill bit diameter, the value of the coefficient of variation of the ultimate tensile load limit was within 20%, which satisfies the test standard. It was shown to be about 136% and 168% of the design strength, indicating that the pulling-out performance of the anchor installed in 1.02 times the drill bit diameter is sufficiently secured.

Pseudoaneurysm Formation due to Popliteal Artery Injury Caused by Drilling during Medial Opening Wedge High Tibial Osteotomy

  • Chun, Keun Churl;So, Byung Jun;Kang, Hyun Tak;Chun, Churl-Hong
    • Knee surgery & related research
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    • v.30 no.4
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    • pp.364-368
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    • 2018
  • We report a case of 53-year-old woman with an injured popliteal artery due to excessive drilling with a drill bit during medial opening wedge high tibial osteotomy (MOWHTO). Pseudoaneurysm was diagnosed three days after surgery and confirmed by urgent computed tomography (CT) angiography. Open vascular surgery with resection of the perivascular hematoma and end-to-end anastomosis using ipsilateral saphenous vein interposition graft was performed. CT angiography at 8 months postoperatively showed that blood flow was maintained without obstruction of the graft site and active dorsiflexion of the foot was possible. To reduce neurovascular injury during MOWHTO, it is important not to drill the far cortex at the proximal part of the osteotomy site when using a drill bit, and the metal should be positioned posteromedially as much as possible.

Correlation Between Drilling Parameter and Tunnel Support Pattern Using Jumbo Drill (도로터널에서 지보패턴별 굴착지수 상관관계 고찰)

  • Kim, Nag-Young;Kim, Sung-Hwan;Chung, Hyung-Sik
    • Journal of Korean Tunnelling and Underground Space Association
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    • v.3 no.4
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    • pp.17-24
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    • 2001
  • Four road tunnels of which the construction conditions were similar were selected in the paper, and laboratory tests and rockmass classification for the tunnels were carried out. And the analysis was performed to find out the correlation between ratio of bit abrasion or drilling parameter and support pattern of tunnel using jumbo drill machine. It was analyzed that there was average abrasion of bit from 11.85% to 3.25% per support patterns of tunnel in four tunnels. Drilling parameter happens to fluctuate according to extent of fracture zone.

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Development of Precision Drilling Machine for the Instrumentation of Nuclear Fuels (핵연료계장을 위한 정밀 드릴링장치 개발)

  • Hong, Jintae;Jeong, Hwang-Young;Ahn, Sung-Ho;Joung, Chang-Young
    • Journal of the Korean Society for Precision Engineering
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    • v.30 no.2
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    • pp.223-230
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    • 2013
  • When a new nuclear fuel is developed, an irradiation test needs to be carried out in the research reactor to analyze the performance of the new nuclear fuel. In order to check the performance of a nuclear fuel during the irradiation test in the test loop of a research reactor, sensors need to be attached in and out of the fuel rod and connect them with instrumentation cables to the measuring device located outside of the reactor pool. In particular, to check the temporary temperature change at the center of a nuclear fuel during the irradiation test, a thermocouple should be instrumented at the center of the fuel rod. Therefore, a hole needs to be made at the center of fuel pellet to put in the thermocouple. However, because the hardness and the density of a sintered $UO_2$ pellet are very high, it is difficult to make a small fine hole on a sintered $UO_2$ pellet using a simple drilling machine even though we use a diamond drill bit made by electro deposition. In this study, an automated drilling machine using a CVD diamond drill has been developed to make a fine hole in a fuel pellet without changing tools or breakage of workpiece. A sintered alumina ($Al_2O_3$) block which has a higher hardness than a sintered $UO_2$ pellet is used as a test specimen. Then, it is verified that a precise hole can be drilled off without breakage of the drill bit in a short time.

An Experimental Study on Drilling Conditions for the Instrumentation of Nuclear Fuel (핵연료 계장을 위한 천공조건에 대한 실험적 연구)

  • Hong, Jintae;Kim, Ka-Hye;Jeong, Hwang-Young;Ahn, Sung-Ho;Joung, Chang-Young
    • Journal of the Korean Society for Precision Engineering
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    • v.30 no.1
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    • pp.113-119
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    • 2013
  • To develop a new nuclear fuel, it needs to make a test fuel rod and carry out burn-up test in the test loop of a research reactor to check the irradiation characteristics of the nuclear fuel. At that time, several sensors such as thermocouples, LVDTs and SPNDs are needed to be attached in and out of the fuel rod and connect them with instrumentation cables. Then, the instrumentation cables deliver the signals measured by the sensors to the measuring device located outside of the reactor pool. In particular, to install a thermocouple in a fuel rod, it needs to drill off holes on the alumina blocks and sintered $UO_2$ pellets. However, because the hardness of a sintered $UO_2$ pellet is 700 Hv (or HRC 61) and that of an alumina block is 1480 Hv, a special drilling machine which adapts a diamond coated drill bit had developed. In this study, several case experiments have been carried out to find an optimal drilling condition of the drilling machine. And, using the optimal drilling condition, minimum numbers of the holes that a drill bit can drill off are verified.

A Study on Improving the Impact Force of Impact Hammer Drill (충격햄머드릴의 타격력 향상을 위한 연구)

  • 김재환;정재천;박병규;백복현
    • Journal of KSNVE
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    • v.7 no.4
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    • pp.669-679
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    • 1997
  • This paper deals with a study of striker type impact hammer drill for improving the drilling performance. The study was performed through a numerical simulation of the impact hammer mechanism and an experimental comparison of the numerical simulation results was followed. Optimization of the impact mechanism was also performed. The numerical model of the impact hammer drill takes into account the striker motion and the effects of the pressure in the cylinder as well as the friction acting on the striker. The equation of motion is solved with the pressure equation in the cylinder including the friction force. The friction is considered as a combination of Coulomb friction and viscous damping friction. At the moment of impact, an ideal impact model that uses restitution coefficient is used to calculate the sudden change of the striker motion. The numerically simulated impact force shows a good agreement with the experimental result and thus, the validity of the numerical model is proven. Based upon the proposed model, an optimization was performed to improve the impact force of the hammer drill. The objective function is to maximize the impact force and the used design variables are striker mass, frequency of piston, bit guide mass, cylindrical diameter and dimensions of the mechanism components. Each design variable and some other conditions that are essential to manitain normal operation of the hammer drill are considered as constraints. The optimized result show a remarkable improvement in impact force and an experimental proof was investigated.

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Agitation Performance Study of 2-shafts Agitator Rotate Directio in the Mud Tank Based on CFD (CFD를 이용한 머드 탱크 2축 교반기의 회전방향에 따른 교반성능 연구)

  • Im, Hyo-Nam;Lee, Hee-Woong;Lee, In-Su;Choi, Jae-Woong
    • Journal of Ocean Engineering and Technology
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    • v.28 no.2
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    • pp.111-118
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    • 2014
  • In drilling process of oil wells, the drilling fluid such as mud keeps the drill bit cool and clean during drilling, with suspending drill cuttings and lubricating a drill bit. In this paper, a commercial CFD package(ANSYS Fluent 15.0) was used to solve the hydrodynamic force and evaluate mud mixing time in the mud mixing tank on offshore drilling platforms. Prediction of power consumption in co-rotating and counter-rotating models has been compared with results of Nagata's correlation equation. This research shows the hydrodynamic effect inside the two phase mud mixing tank according to rotating directions(co-rotating and counter-rotating). These results, we can conclude that the co-rotating direction of the two shafts with mixing blade in the mud mixing tank can be a preferable in power consumption and mixing time reduction.