• 제목/요약/키워드: Combustor performance test

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5MW 발전용 가스터빈 엔진 연소기 성능시험 (Performance Test of 5MW Gas Turbine Engine Combustor)

  • 박부민;김형모;최영호;양수석;천무환
    • 한국연소학회지
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    • 제13권4호
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    • pp.37-46
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    • 2008
  • Performance test of 5MW class gasturbine combustor was carried out at combustor test facility of KARI(Korea Aerospace Research Institute). The combustor is dry low NOx type premixed combustor and fuel is natural gas. The characteristics of combustor were measured including emission, pressure pulsation and exit temperature distribution. Optimum operation point of combustor was found by changing parameters like fuel ratio between pilot and main burner. The test result showed that the combustor performance is sufficient to satisfy the gasturbine system requirement.

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가스터빈 연소기 기본형상 결정에 관한 연구 (A Study on the Preliminary Design of Gas Turbine Combustor)

  • 안국영;김한석;김관태;배진호
    • 한국연소학회:학술대회논문집
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    • 한국연소학회 1997년도 제15회 KOSCO SYMPOSIUM 논문집
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    • pp.135-151
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    • 1997
  • The preliminary design and performance test for determining dimensions of gas turbine combustor were investigated. The combustor design program was developed and applied to design our combustor. and detailed design for determining of swirler. dome and liner holes were performed experimentally. The swirler. which govern the combustion characteristics of combustor, was determined $40^{\circ}$ as swirl angle at first performance test. After second performance test the swirler was re-determined by 24 mm i.d.. 34 mm o.d., and swirl angle of $45^{\circ}$. The geometry of liner holes were determined by considering the flame stability and recirculation zone size. It was found that flame can be more easily stabilized by adjusting the swirier dimensions rather than liner holes. The geometry of swirler and liner holes were re-determined by final performance test with dilution holes. Also. the performance of combustor was evaluated by analysis of exhaust gases.

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보조동력장치용 환형 역류형 연소기 (TS2) 성능 시험 (Performance Test of A Reverse-Annular Type Combustor (TS2) for APU)

  • 고영성;한영민;양수석;이대성;윤상식;최성만
    • 대한기계학회:학술대회논문집
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    • 대한기계학회 2001년도 춘계학술대회논문집D
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    • pp.840-845
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    • 2001
  • Development of a small gas-turbine combustor for 100kW class APU(Auxiliary Power Unit) has been performed. This combustor is a reverse-annular type and has a tangential swirler in the liner head to improve the fuel/air mixing and flame stability. Three main and three pilot fuel injectors of the simplex pressure-swirl type are used. The performance target at the design condition includes a turbine inlet temperature of 1170K, a combustion efficiency of 99%, a pattern factor of 30%, and an engine durability of 3000 hours. Under developing the combustor, we conducted performance test of our first prototype(TS1) with some variants. As a result of the test, the performance targets of the combustor are satisfied except that the pattern factor is about 4% higher than target value. So, we redesigned the second prototype(TS2) and conduct performance test with the critical focus on pattern factor and exit mean temperature. We adopted TS2 four variant to check the improvement of pattern factor. As the result, the pattern factors of several variants were satisfied with the performance target. Finally, We chose the TS2A variant as a final combustor for our APU model.

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액체로켓엔진 연소기용 단일 분사기 연소기와 축소형 연수고 수류/연소시험 결과 비교 (Comparison of Combustion Performance between Single Injector Combustor and Sub-scale Combustor)

  • 김승한;한영민;서성현;문일윤;이광진
    • 유체기계공업학회:학술대회논문집
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    • 유체기계공업학회 2006년 제4회 한국유체공학학술대회 논문집
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    • pp.451-454
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    • 2006
  • This paper describes the results of cold flow test and hot firing tests of an uni-element coaxial swirl injector and hot firing tests of a subscale combustor, as to the development effort of coaxial swirl injector for high performance liquid rocket engine combustor. A major design parameter for coaxial swirl injector is the recess number of a bi-swirl injector. The results of hot firing tests of the uni-element injector combustor and the sub-scale combustor are analyzed to investigate the effect of the recess number influencing on the combustion performance and pressure fluctuation. The test results of a cold flow test of the unielement combustor shows that it was shown that the change in recess number has significant effect on mixing characteristics and efficiency, while the effect of recess number on atomization characteristic is not The results of a series of firing tests using unielement and subscale combustor show that the recess length significantly affects the hydraulic characteristics, the combustion efficiency, and the dynamics of the liquid oxygen/kerosene bi-swirl injector. As a point of combustion performance, combustion efficiencies are 90% for unielement combustor and 95% for subscale combustor. The difference in the characteristic velocities between the unielement combustor and the subscale combustor may be caused by the difference in thermal loss to the combustor wall and the relative lengths of the combustion chamber. For a mixed type coaxial swirl combustor, the pressure drop across the injector increases as recess number becomes larger. The low frequency pressure fluctuation observed in unielement combustor can be related to the propellant mixing characteristics of the coaxial bi-swirl injector. The effect of the recess number on the pressure fluctuation inside the combustion chamber is more significant in un i-element combustor than the subscale combustor, of which the phenomena are also observed in time domain and frequency domain.

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가스터빈 연소기 기본형상 결정을 위한 성능실험 (An experimental study for preliminary design of gas turbine combustor)

  • 안국영;김한석;조은성;배진호
    • 대한기계학회논문집B
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    • 제22권6호
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    • pp.840-848
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    • 1998
  • The preliminary design and performance test were carried out for determining dimensions of gas turbine combustor. The combustor design program was developed and applied to design our combustor, and the specific dimensions for swirler, dome and liner holes were determined by the semiempirical manner. Based on the first performance test data, the swirl angle governing the combustion characteristics of primary combustor zone was determined as 40 deg.. Using the second performance test data, the swirler dimensions were readjusted by 24 mm i.d., 34 mm o.d., and swirl angle of 45 deg.. The geometry of liner holes were determined by considering the flame stability and recirculation zone size. It was found that flame can be more easily stabilized by adjusting the swirler dimensions rather than liner holes. The geometry of swirler and liner holes were readjusted by using the final performance test data with dilution holes. Also, the combustor performance and emission characteristics were evaluated by analysis of exhaust gases.

항공추진용 가스터빈엔진 연소기 성능시험 (Performance Test of Combustor for Aeropropulsion Gasturbine Engine)

  • 박부민;김형모;최영호;전병호;양수석
    • 한국추진공학회:학술대회논문집
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    • 한국추진공학회 2008년도 제31회 추계학술대회논문집
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    • pp.405-406
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    • 2008
  • 연소기는 가스터빈 엔진의 주요 구성품 중의 하나이며, 다른 구성품과 달리 거의 시험을 통해서 개발된다. 항우연은 항공용 및 발전용 가스터빈의 연소기 성능시험을 성공적으로 수행해왔다. 연소기 성능시험을 위해서는 대량의 공기를 고온/고압 조건으로 공급해야 하므로, 시험은 대형 시험설비에서 이루어진다.

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저공해 연소기 시험기술 (Test Methods on Development of Low Emission Gas Turbine Combustor)

  • 김형모;최영호;김동식;박부민
    • 항공우주기술
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    • 제6권1호
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    • pp.29-34
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    • 2007
  • On the stage of combustor development process, many aerodynamic and combustion characteristics are found out not by only ideal design concept but by only useful tests which are top confidentiality of technically advanced engine development companies, RR and GE, etc. In this study, test techniques of one of that company are analysed and described about some unique tests for test low emission combustors.

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한국의 가스터빈엔진 연소기 연구개발 동향 (Research and Development Trend of Gas Turbine Combustor in Korea)

  • 최성만
    • 한국연소학회:학술대회논문집
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    • 한국연소학회 2012년도 제45회 KOSCO SYMPOSIUM 초록집
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    • pp.287-289
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    • 2012
  • The research and development history of the gas turbine combustor in Korea is introduced briefly. It is very important to understand the fuel spray, mixing phenomena in achieving combustion performance. In this paper, two kinds of fuel injection system such as duplex fuel injector and rotary spray system are introduced in developing gas turbine combustor in Korea. The extensive experimental research of fuel spray, ignition, performance and endurance rig test makes gas turbine combustor successfully in Korea.

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보조동력장치용 환형 역류형 연소기 (TS2) 성능 시험 (Performance Test of A Reverse-Annular Type Combustor (TS2) for APU)

  • 고영성;한영민;이강엽;양수석;이대성
    • 대한기계학회논문집B
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    • 제26권6호
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    • pp.805-810
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    • 2002
  • Development of a small gas-turbine combustor for 100㎾ class APU(Auxiliary Power Unit) has been performed. This combustor is a reverse-annular type and has a tangential swiller in the liner head to improve the fuel/air mixing and flame stability. Three main and three pilot fuel injectors of the simplex pressure-swirl type are used. The performance target at the design condition includes a turbine inlet temperature of l170k, a combustion efficiency of 99%, a pattern factor of 30%, and an engine durability of 3000 hours. Under developing the combustor, we conducted the performance test of our first prototype(TS1) with some variants. As a result of the test, the performance targets of the combustor are satisfied except that the pattern factor is about 4% higher than the target value. Therefore, the second prototype(TS2) was redesigned and the performance test was conducted with the critical focus on the pattern factor and the exit mean temperature. We adopted TS2 four variants to check the improvement of the pattern factor. As a result, the pattern factors of several variants were satisfied with the performance target. Finally, the TS2A variant was chosen as a final combustor fur our APU model.

초소형 가스터빈 엔진용 금속 3D 프린팅 연소기 성능 시험 (Performance Test of Metal 3D Printed Micro Gas Turbine Engine Combustor)

  • 김재호;김형모;박부민;이동호
    • 한국추진공학회지
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    • 제23권6호
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    • pp.51-58
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    • 2019
  • 본 연구에서는 소형 무인기에 사용되는 초소형 가스터빈 엔진의 연소기를 3D 프린팅으로 제작하고, 시험 설비와 리그를 제작하여 연소기 단품 성능시험을 수행하였다. 연소기 성능시험은 두 가지 부하조건에서 당량비를 조절하여 각 부하조건 별 4가지 시험조건에서 수행하였다. 성능시험 결과 연소기의 압력손실과 출구온도분포는 우수하였지만, 연소가스에서 다량의 UHC와 CO가 검출되어 연소효율은 일반적인 가스터빈 연소기에 비해 아주 낮음을 확인하였다. 성능시험을 통해 획득한 정량적 성능데이터는 향후 3D 프린팅 기술로 성능이 개선된 연소기의 설계와 제작에 활용 할 예정이다.