• Title/Summary/Keyword: Car Body and Parts

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Crush Analysis of a TTX M-Car Design (TTX 구동차 설계안의 충돌압괴특성 분석)

  • Jung Hyun-Seung;Kwon Tae-Soo;Koo Jeong-Seo;Cho Tae-Min
    • Proceedings of the KSR Conference
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    • 2004.10a
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    • pp.616-621
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    • 2004
  • In this paper, the crush characteristics of a tilting train express (TTX) M-car design are evaluated with a head-on collision scenario. Its body shell is divided into three parts - front end, middle section, and rear end. For each part, crush-force relation is evaluated numerically through 3-dimensional shell element analysis with LS-DYNA. TTX's embody structure is a hybrid type structure made of steel and composite materials. Composite sandwich panels are modeled as layered shells whose layers have different material properties. And a damage material model is used to consider the effect of stiffness degradation during deformation. The crush characteristics obtained from these calculations will be used as material modeling data of full-rake collision analyses.

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Study of Examples for Air Bag Non-deployment Including Rear Collision and Failure Phenomenon by Damage of Control Parts in Vehicle Air Bag (자동차 에어백의 제어부품 불량에 의한 고장현상 및 후방 추돌에 관련된 에어백 미전개에 대한 사례 연구)

  • Lee, Il Kwon;Kim, Young Gyu;Moon, Hak Hook
    • Journal of the Korean Institute of Gas
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    • v.16 no.6
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    • pp.102-106
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    • 2012
  • The purpose of this paper is to study the failure cases in relation to system of Air Bag in vehicle happened in the field. In the first example, it was separated the soldering parts connected the wire pin between air bag module and clock spring of air bag. Whenever the pin shake by the car's vibration, the driver verified the malfunction phenomenon appeared air bag warning lamp on instrument panel in front of driver's seat. in car inside room. The second example, it verified the warning lamp lighting phenomenon of air bag by produced the circuit plate non-contacting of single an element in air bag electronic control unit. The third example, it verified the light of air bag warning indicator lamp by separated with soldering parts connecting inner pin and resistance terminal of seat belt pretensioner using passenger seat. The fourth example, when the passenger car crash a back of truck, the former bumper get jammed under the latter as the roof height of car low less than that. Therefore, the impact of Car's collision verified that don't transfer with body frame of vehicle because of no attachment impact sensor in it.

A study on measurement and compensation of automobile door gap using optical triangulation algorithm (광 삼각법 측정 알고리즘을 이용한 자동차 도어 간격 측정 및 보정에 관한 연구)

  • Kang, Dong-Sung;Lee, Jeong-woo;Ko, Kang-Ho;Kim, Tae-Min;Park, Kyu-Bag;Park, Jung Rae;Kim, Ji-Hun;Choi, Doo-Sun;Lim, Dong-Wook
    • Design & Manufacturing
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    • v.14 no.1
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    • pp.8-14
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    • 2020
  • In general, auto parts production assembly line is assembled and produced by automatic mounting by an automated robot. In such a production site, quality problems such as misalignment of parts (doors, trunks, roofs, etc.) to be assembled with the vehicle body or collision between assembly robots and components are often caused. In order to solve such a problem, the quality of parts is manually inspected by using mechanical jig devices outside the automated production line. Automotive inspection technology is the most commonly used field of vision, which includes surface inspection such as mounting hole spacing and defect detection, body panel dents and bends. It is used for guiding, providing location information to the robot controller to adjust the robot's path to improve process productivity and manufacturing flexibility. The most difficult weighing and measuring technology is to calibrate the surface analysis and position and characteristics between parts by storing images of the part to be measured that enters the camera's field of view mounted on the side or top of the part. The problem of the machine vision device applied to the automobile production line is that the lighting conditions inside the factory are severely changed due to various weather changes such as morning-evening, rainy days and sunny days through the exterior window of the assembly production plant. In addition, since the material of the vehicle body parts is a steel sheet, the reflection of light is very severe, which causes a problem in that the quality of the captured image is greatly changed even with a small light change. In this study, the distance between the car body and the door part and the door are acquired by the measuring device combining the laser slit light source and the LED pattern light source. The result is transferred to the joint robot for assembling parts at the optimum position between parts, and the assembly is done at the optimal position by changing the angle and step.

A Study on Determination of Complex Stiffness of Frame Bush for Ride-comfort Improvement of Body-on-frame Vehicle (프레임 차량의 주행 진동 저감을 위한 프레임 부시 복소동강성계수 크기 결정에 관한 연구)

  • Jeong, Myeon-Gyu;Kim, Ki-Sun;Kim, Kwang-Joon
    • Transactions of the Korean Society for Noise and Vibration Engineering
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    • v.16 no.6 s.111
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    • pp.619-626
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    • 2006
  • Body-on-frame type vehicle has a set of frame bushes between body and frame for vibration isolation. Such frame bushes are important vibration transmission paths to passenger space for excitations during driving. In order to reduce the vibration level of passenger space, therefore, change of complex stiffness of the frame bushes is more efficient than modification of other parts of the vehicle such as body, frame and suspension. The purpose of this study is to reduce the vibration level for ride comfort by optimization of complex stiffness of frame bushes. In order to do this, a simple finite element vehicle model was constructed and complex stiffness of the frame bushes was set to be design variables. The objective function was defined to reflect frequency dependence of passenger ride comfort. Genetic algorithm and sub-structure synthesis were applied for minimization of the objective function. After optimization level at a position of interest on the car body was reduced by about 43.7 % in RMS value. Causes for optimization results are discussed.

Vibration Signal Analysis of Running Electric Train using Adaptive Signal Processing (적응신호처리에 의한 주행전기동차의 진동신호해석)

  • 최연선
    • Journal of the Korean Society for Railway
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    • v.2 no.2
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    • pp.13-20
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    • 1999
  • The vibration signals of driving parts of electric train are distorted its signal patterns due to the impact components, which occurs when wheel passes rail joints. An elimination method of the impact components is investigated using adaptive signal processing technique in this study The result shows that adaptive interference canceling method seems to be more effective than line enhancement technique. The application of adaptive interference canceling method to the signal measured at bogie shows that the extractions of the signals of driving parts of traction motor, reduction gear, and axle bearing are successful. Therefore, only the signals of bogie, which is the place to attach an accelerometer easily, is sufficient for the fault diagnosis and the safety evaluation of electric train. Also, adaptive interference canceling method can be applicable to evaluate the performance of vibration isolation between bogie and car body and to investigate the characteristics of indoor sound.

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Vibration Signal Analysis of Running Electric Train using Adaptive Signal Processing (적응신호처리에 의한 주행전기동차의 진동신호해석)

  • 최연선;이봉현
    • Proceedings of the KSR Conference
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    • 1999.05a
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    • pp.143-150
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    • 1999
  • The vibration signals of driving parts of electric train are distorted its signal patterns due to the impact components, which occurs when wheel passes rail joints. An elimination method of the impact components is investigated using adaptive signal processing technique in this study. The result shows that adaptive interference canceling method seems to be more effective than line enhancement technique. The application of adaptive interference canceling method to the signal measured at bogie shows that the extractions of the signals of driving parts of traction motor, reduction gear, and axle bearing are successful. Therefore, only the signals of bogie, which is the place to attach an accelerometer easily, is sufficient for the fault diagnosis and the safety evaluation of electric train. Also, adaptive interference canceling method can be applicable to evaluate the performance of vibration isolation between bogie and car body and to investigate the characteristics of indoor sound.

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A Study of Musculoskeletal Disorders at Automobile Industries in Korea (국내 자동차산업의 근골격계질환 실태에 관한 연구)

  • 김철홍
    • Journal of Korean Society of Industrial and Systems Engineering
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    • v.24 no.67
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    • pp.1-10
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    • 2001
  • A series of studies with collaboration of university, research institute, and labor union were conducted to examine the situation and severity of work-related musculoskeletal disorders (MSDs) at an automobile company which is one of the three major car companies in Korea. As the first part of the study, a questionnaire survey was conducted on 4,000 employees at 2 different assembly sites and A/S centers over the country. The questionnaire was consisted of three parts; symptom survey, work environment information, and labor intensity survey. Among 4,000 questionnaires, 2,643 responses were considered for analysis. The result showed that 68.5% of the respondents complained pains on at least one part of the body and 48.8% on at least two parts of the body. After cross-sectional analysis of various information and risk factors such as severity of symptom, duration and frequency of pain, 31.5% of respondents were considered as at high risk of having MSDs. This high-risk rate showed similar result when compared with previous studies conducted at various manufacturing industries in Korea. Also the analysis of the work environment and job intensity survey supported the high-risk rate of MSDs.

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The Development of Seat Track Parts Using Shape Freeze in UHSS (초고강도 소재 성형시 형상 동결을 이용한 Seat Track 부품 개발)

  • Park, Dong Hwan;Yun, Jae Jung;Moon, Hyun Duk;Lee, Tae Gil
    • Journal of the Korean Society of Manufacturing Technology Engineers
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    • v.26 no.1
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    • pp.59-65
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    • 2017
  • A seat track product is a car seat part that provides a base for vehicle seats. An ultra-high strength steel sheet is used to reduce the weight of vehicle body parts. However, the formability of an ultra-high strength steel sheet is poor because of its very low elongation and very high elastic deformation. For this reason, a new forming technology of an ultra-high strength steel sheet is required. The influence of spring-back of seat track parts on the shape freeze in forming processes was investigated to be solved by adjusting the appropriate tool design such as minus clearance between punch and die, and punch angle. This paper describes how to apply the spring-back prevention technique for improving shape freeze by using the ultra-high strength steel sheet with 980MPa to develop lightweight seat tract parts.

Durability Improvement due to the Change of Lower Arm by the Class of Automotive Body (차체의 종류별 로어암 형상의 변화에 따른 내구성 향상에 관한 연구)

  • Han, Moonsik;Cho, Jaeung
    • Journal of the Korean Society of Manufacturing Process Engineers
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    • v.16 no.6
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    • pp.29-34
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    • 2017
  • This study analyzed automobile lower arm assembly structure and fatigue to identify configuration changes to enhance structural safety. Parts connected to the car body were fixed and 500 N load was applied at the lower arm head. Maximum equivalent stress and maximum total deformation were minimized for model 1 ( MPa and 0.10315 mm, respectively). Fatigue analysis using extreme SAE bracket history fatigue loads showed model 1 also improved fatigue life ($3.3693{\times}10^5cycles$). This study provides important inputs to improve lower arm durability by modifying the arm configuration.

A Study on Laser Welding Application of the Cowl Cross Member for Ultra-High Strength Steel (초고장력 강판을 적용한 Cowl Cross Member의 레이저 용접 적용에 관한 연구)

  • Park, Dong Hwan;Yun, Jae Jung;Kim, Kun Young
    • Journal of the Korean Society of Manufacturing Technology Engineers
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    • v.23 no.5
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    • pp.525-531
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    • 2014
  • A cowl cross is a part of the car's instrument panel used to maintain the rigidity of the vehicle body side. The application of laser welding has the benefits of speed and thermal deformation compared to arc welding. An ultra-high strength steel sheet is used to reduce the weight of the vehicle body parts. Generally, formability of such a steel sheet is poor because its elongation is very low. For this reason, a method for cold forming of an ultra-high strength steel sheet is required. This paper describes how to improve the formability and weldability of the ultra-high strength steel sheet. Mechanical tests of this material were also performed to evaluate the welding properties of $CO_2$ (GMAW) and those of laser welding.