• Title/Summary/Keyword: Bed temperature

Search Result 1,039, Processing Time 0.033 seconds

Seasonal Variation in Species Composition of Fishes in the Eelgrass Beds in Angel Bay of the Southern Coast of Korea (남해 안골만 잘피밭 어류 종조성의 계절변동)

  • LEE Tae Won;MOON Hyung Tae;HWANG Hak Bin;HUH Sung-Hoi;KIM Dae Ji
    • Korean Journal of Fisheries and Aquatic Sciences
    • /
    • v.33 no.5
    • /
    • pp.439-477
    • /
    • 2000
  • Seasonal variation in species composition of fishes in the eelgrass bed in Angel Bay of the southern coast of Korea was determined using monthly samples by a beam trawl from April 1998 to March 1999, A total of 39 species, 2,065 individuals and 8,930 g of fishes were collected during the study period. The fish were composed of the small-sized resident species and the juveniles of Leiognathus nuchalis, Pholis nebulosa, Spgnathus schlegeli and Sebastes ineinis predominated in abundance, accounting for $60{\%}$ of total number of individuals. The number of species and biomass were low from December to March when the water temperature was low, The biomass increased by the catch of a large number of L. nuchalis and S. inemis in April and May when the eelgrass grew fast. The fish numbers decreased in June and July when the adults of the resident species declined after the spawning. A large number of juveniles which had released in spring occurred in August. The biomass of fish decreased from September, and a few number of fish were collected in winter. Species were grouped into four by cluster analysis: the warm season group including P. nebulosa, S. schlegeli and L. nuchalis, the cold season group including Chaenogobius heptaoanthus and Platycephalus indieus, the group of fish species occurred during the growing season of eelgrass such as P. couoides, S. inermis and P. perooides, and the group of fish species occurred during decaying season of eelgrass such as S. cirrhifer and H. coronatus. Principal component analysis indicated that seasonal variation in species composition was determined by the water temperature and standing crops of eelgrass.

  • PDF

COATED PARTICLE FUEL FOR HIGH TEMPERATURE GAS COOLED REACTORS

  • Verfondern, Karl;Nabielek, Heinz;Kendall, James M.
    • Nuclear Engineering and Technology
    • /
    • v.39 no.5
    • /
    • pp.603-616
    • /
    • 2007
  • Roy Huddle, having invented the coated particle in Harwell 1957, stated in the early 1970s that we know now everything about particles and coatings and should be going over to deal with other problems. This was on the occasion of the Dragon fuel performance information meeting London 1973: How wrong a genius be! It took until 1978 that really good particles were made in Germany, then during the Japanese HTTR production in the 1990s and finally the Chinese 2000-2001 campaign for HTR-10. Here, we present a review of history and present status. Today, good fuel is measured by different standards from the seventies: where $9*10^{-4}$ initial free heavy metal fraction was typical for early AVR carbide fuel and $3*10^{-4}$ initial free heavy metal fraction was acceptable for oxide fuel in THTR, we insist on values more than an order of magnitude below this value today. Half a percent of particle failure at the end-of-irradiation, another ancient standard, is not even acceptable today, even for the most severe accidents. While legislation and licensing has not changed, one of the reasons we insist on these improvements is the preference for passive systems rather than active controls of earlier times. After renewed HTGR interest, we are reporting about the start of new or reactivated coated particle work in several parts of the world, considering the aspects of designs/ traditional and new materials, manufacturing technologies/ quality control quality assurance, irradiation and accident performance, modeling and performance predictions, and fuel cycle aspects and spent fuel treatment. In very general terms, the coated particle should be strong, reliable, retentive, and affordable. These properties have to be quantified and will be eventually optimized for a specific application system. Results obtained so far indicate that the same particle can be used for steam cycle applications with $700-750^{\circ}C$ helium coolant gas exit, for gas turbine applications at $850-900^{\circ}C$ and for process heat/hydrogen generation applications with $950^{\circ}C$ outlet temperatures. There is a clear set of standards for modem high quality fuel in terms of low levels of heavy metal contamination, manufacture-induced particle defects during fuel body and fuel element making, irradiation/accident induced particle failures and limits on fission product release from intact particles. While gas-cooled reactor design is still open-ended with blocks for the prismatic and spherical fuel elements for the pebble-bed design, there is near worldwide agreement on high quality fuel: a $500{\mu}m$ diameter $UO_2$ kernel of 10% enrichment is surrounded by a $100{\mu}m$ thick sacrificial buffer layer to be followed by a dense inner pyrocarbon layer, a high quality silicon carbide layer of $35{\mu}m$ thickness and theoretical density and another outer pyrocarbon layer. Good performance has been demonstrated both under operational and under accident conditions, i.e. to 10% FIMA and maximum $1600^{\circ}C$ afterwards. And it is the wide-ranging demonstration experience that makes this particle superior. Recommendations are made for further work: 1. Generation of data for presently manufactured materials, e.g. SiC strength and strength distribution, PyC creep and shrinkage and many more material data sets. 2. Renewed start of irradiation and accident testing of modem coated particle fuel. 3. Analysis of existing and newly created data with a view to demonstrate satisfactory performance at burnups beyond 10% FIMA and complete fission product retention even in accidents that go beyond $1600^{\circ}C$ for a short period of time. This work should proceed at both national and international level.

High Density Tilapia Culture in a Recirculating Water System without Filter Bed (무여과순환수 탱크 이용 Tilapia의 고밀도 사육실험)

  • KIM In-Bae
    • Korean Journal of Fisheries and Aquatic Sciences
    • /
    • v.16 no.2
    • /
    • pp.59-67
    • /
    • 1983
  • An experiment on the rearing of tilapia stocked in closed recirculating tanks eliminating biological filter beds was carried out at the Fish Culture Experiment Station of the National Fisheries University of Pusan, from May 18 through October 21, 1982, and the growth rates, feed conversion, water quality, spawning prevention and space utilization efficiency were discussed. Finally discussed is the feasibility on the establishment of commercial production units. On the water quality, the water temperature ranged from $22.8^{\circ}C\;to\;29.1^{\circ}C$, and total ammonia arround 10 ppm or slightly up. Maintaining phytoplankton bloom was not successful probably because of the active consumption by the heavily stocked tilapia. Several attempts were made by changing the culture water with green water from a nearby earthen pond with results of fading-away in a couple of days. Feed conversions were relatively high ranging from 0.9 to 1.2 except for experiment 1 when the fish were not fully recovered from weakened wintering state. The feed used was partly laboratory prepared $25\%$ protein diet and mostly commercially available $39\%$ protein carp feed. Spawning was completely controlled during the experiment, resulting from density effect, which ranged from 10kg to 40.7kg per square meter with water depth of 0.5 to 0.6m. Space utilization efficiency was very high. Daily net production from the experiment division 3, which showed the highest result, was 6.206 kg per tank, which is calculated 3,235 metric tons per hectare per year, This time, water temperature ranged from 27.8 to $29.1^{circ}C$, average being $28.4^{circ}C$, and total ammonia arround 10 ppm. An estimation for the commercial set-up of the production system based on the results of experiment divisions which had initial stocking rate $15\;kg/m^2$ or up, is made. If the total facility, 8 tanks comprising $56\;m^2$ in surface area, is used for the present study, the yield would become 5,639 kg from 200 day rearing, which would be possible under double sheets vinyl house without additional heating, and it is thought feasible in the economic view point, when 10 or more units are operated.

  • PDF

Phosphorus Modified Co/Al2O3 Fischer-Tropsch Catalyst for a Slurry Phase CSTR with Enhanced Hydrothermal and Mechanical Stability (수열특성 및 기계적 안정성의 개선으로 슬러리상 CSTR에 적합한 P 첨가 알루미나 기반의 Fischer-Tropsch 합성용 코발트 촉매)

  • Jung, Gyu-In;Ha, Kyoung-Su;Park, Seon-Ju;Kim, Du-Eil;Woo, Min-Hee;Jun, Ki-Won;Bae, Jong-Wook;Kang, Yong
    • Korean Chemical Engineering Research
    • /
    • v.50 no.2
    • /
    • pp.229-237
    • /
    • 2012
  • Phosphorus was incorporated into Co/$Al_2O_3$ catalyst for FTS by impregnating an acidic precursor, phosphoric acid, in ${\gamma}-Al_2O_3$ support to improve the mechanical strength, the hydrothermal stability of the catalyst particle, and the catalytic performance as well. Surface characterization techniques such as FT-IR revealed that $AlPO_4$ phase was generated on the surface of the P-modified catalyst. The addition of phosphorus was found to alleviate the interaction between cobalt and alumina surface, and to increase reducibility of catalyst. The catalytic activity such as $C_{5+}$ productivity and turnover frequency (TOF) was calculated to evaluate catalytic performance. The influence of calcination temperature of the $Al_2O_3$ containing 2 wt.% P on the catalytic performance was also investigated. Through hydrothermal stability test and XRD analysis, the P-modified catalyst had strong resistant to the pressurized and hot $H_2O$. The mechanical strength of the P-modified catalyst was also examined through an in-house fluidized-bed vessel, and it was found that the catalyst fragmentation could be successfully suppressed with P. Taken as a whole, the best performance was shown to be at 1~2 wt.% P in alumina and at the calcination temperature of $500^{\circ}C$.

Strategies about Optimal Measurement Matrix of Environment Factors Inside Plastic Greenhouse (플라스틱온실 내부 환경 인자 다중센서 설치 위치 최적화 전략)

  • Lee, JungKyu;Kang, DongHyun;Oh, SangHoon;Lee, DongHoon
    • Journal of Bio-Environment Control
    • /
    • v.29 no.2
    • /
    • pp.161-170
    • /
    • 2020
  • There is systematic spatial variations in environmental properties due to sensitive reaction to external conditions at plastic greenhouse occupied 99.2% of domestic agricultural facilities. In order to construct 3 dimensional distribution of temperature, relative humidity, CO2 and illuminance, measurement matrix as 3 by 3 by 5 in direction of width, height and length, respectively, dividing indoor space of greenhouse was designed and tested at experimental site. Linear regression analysis was conducted to evaluate optimal estimation method in terms with horizontal and vertical variations. Even though sole measurement point for temperature and relative humidity could be feasible to assess indoor condition, multiple measurement matrix is inevitably required to improve spatial precision at certain time domain such as period of sunrise and sunset. In case with CO2, multiple measurement matrix could not successfully improve the spatial predictability during a whole experimental period. In case with illuminance, prediction performance was getting smaller after a time period of sunrise due to systematic interference such as indoor structure. Thus, multiple sensing methodology was proposed in direction of length at higher height than growing bed, which could compensate estimation error in spatial domain. Appropriate measurement matrix could be constructed considering the transition of stability in indoor environmental properties due to external variations. As a result, optimal measurement matrix should be carefully designed considering flexibility of construction relevant with the type of property, indoor structure, the purpose of crop and the period of growth. For an instance, partial cooling and heating system to save a consumption of energy supplement could be successfully accomplished by the deployment of multiple measurement matrix.

Simultaneous Removal of $NO_x$ and $SO_2$ through the Combination of Sodium Chlorite Powder and Carbon-based Catalyst at Low Temperature ($NaClO_2(s)$와 탄소 분산형 촉매를 이용한 저온에서의 $NO_x$$SO_2$ 동시 제거)

  • Byun, Young-Chul;Lee, Ki-Man;Koh, Dong-Jun;Shin, Dong-Nam
    • Journal of Korean Society of Environmental Engineers
    • /
    • v.33 no.1
    • /
    • pp.39-46
    • /
    • 2011
  • NO oxidation is an important prerequisite step to assist the selective catalytic reduction (SCR) at low temperatures ($<200^{\circ}C$). Therefore, we conducted the lab- and bench-scales experiments appling the sodium chlorite powder ($NaClO_2(s)$) for the oxidation of NO to $NO_2$ and the carbon-based catalyst for the reduction of $NO_x$ and $SO_2$; the lab- and bench-scales experiments were conducted in laboratory and iron-ore sintering plant, respectively. In the lab-scale experiment, known concentrations of $NO_x$ (200 ppm), $SO_2$ (75 ppm), $H_2O$ (10%) and $NH_3$ (400 ppm) in 2.6 L/min were introduced into a packed-bed reactor containing $NaClO_2(s)$, then gases produced by the reaction with $NaClO_2(s)$ were fed into the carbon-based catalyst (space velocity = $2,000hr^{-1}$) at $130^{\circ}C$. In the bench-scale experiment, flue gases of $50Nm^3/hr$ containing 120 ppm NO and 150 ppm $SO_2$ were taken out from the duct of iron-ore sintering plant, then introduced into the flow reactor; $NaClO_2(s)$ were injected into the flow reactor using a screw feeder. Gases produced by the reaction with $NaClO_2(s)$ were introduced into the carbon-based catalyst (space velocity = $1,000hr^{-1}$). Results have shown that, in both lab- and bench-scales experiments, NO was oxidized to $NO_2$ by $NaClO_2(s)$. In addition, above 90% of $NO_x$ and $SO_2$ removal were obtained at the carbon-based catalyst. These results lead us to suggest that the combination of $NaClO_2(s)$ with the carbon-based catalyst has the potential to achieve the simultaneous removal of $NO_x$ and $SO_2$ at low temperature ($<200^{\circ}C$).

Studies on the Improvement of Nursery for Better Ripening Percentage and Prevention of Red Discoloration of Rice Variety "Tongil" (통일벼의 등숙(登熟) 향상(向上)과 적고방지(赤枯防止)를 위(爲)한 묘대개선(苗垈改善)에 관(關)한 연구(硏究))

  • Choi, Boum Rawl
    • Korean Journal of Agricultural Science
    • /
    • v.1 no.1
    • /
    • pp.9-26
    • /
    • 1974
  • 1. Results in Nursery This experiment was carried out on the effect of the seed treament, soil preparations, kinds of covering soil and inside covering methods in two rice varieties, 'Tongil' and 'Akibare' to find out the most reasonable model of the flat nursery bed, with which lower cost is required comparing with the tunnel nursery. The results obtained are as follows: (1) The seedling of all plots of the ordinary seed were very poor compared to the plots of sprouted seed. (2) In case that the variety 'Tongil' was cultivated on the dry nursery bed, the good seedling percentage and the plant height rat io were significantly increased but the other characteristics of the seedling were not noticeable. (3) The kinds of the covering soil had not an effect on the seedling growth significantly. (4) Inside straw mulching was seemed effective for the protection in the case of the extreme high temperature and heavy rain fall, even though there was not significant differences between inside straw mulching and no treatments at the flat type nursery. (5) Difference of seedling growth between the flat type nursery and the tunnel type nursery was not significant. And it's reason was thought that the covering period of polyethylene film was short in semi hot nursery for the common early transplanting cultivation of rice. (6) The percentage of good seedling was higher at 'Akibare' than 'Tongil', variety but the number of seedling leaf and the seedling growth ratio in height were significantly increased in the variety 'Tongil'. The other seedling characters between there two varieties were not significantly different. 2. Results after transplanting This experiment was conducted to study on the ripening percentage, rice yield and disease, appearance of the seedling from sprouted seed plots including common irrigated nursery as check plot after transplantnig. The results obtained are summarized as follows: (1) The rice yield, the yield components and the appearance of leaf discoloration of both varieties, 'Tongil' and 'Akibare' were slightly betterat the plot of the standard tunnel nursery than that of the flat nursery with inside mulching or the among these three plots. (2) For 'Tongil' variety, the ripening percentage and the rice yield were significantly decreased at the common irrigated nursery compared with semi hot nursery. (3) The ripening percentage and the rice yield of 'Akibare' contrasted with 'Tongil' were significantly decreased at thesemi 'hot-nursery compared with common irrigated nursery. The main reason was thought to be the injury of the rice stripe disease (Rice stripe disease virus). Considering above mentioned experimental result, the seedling of 'Tongil' must be cultivated on the semi bot nursery for better ripening percentage as well as rice yield and for prevention of red discoloration. And as a model of semi hot nursery, the polyethylene covering nursery of standard tunnel type is most desirable but that of flat type with inside straw mulching is thought to be desirable too.

  • PDF

TECHNICAL STUDY ON THE CONTROLLING MECHANIQUES OF THE ENVIRONMENTAL FACTORS IN THE MUSHROOM GROWING HOUSE IN CHONNAM PROVINCE (전남지방(全南地方)에 있어서의 양송이 재배(栽培)에 최적(最適)한 환경조건(環境條件) 조절법분석(調節法分析)에 관(關)한 연구(硏究))

  • Lee, Eun Chol
    • Journal of Korean Society of Forest Science
    • /
    • v.9 no.1
    • /
    • pp.1-44
    • /
    • 1969
  • The important results which have been obtained in the investigation can be recapitulated as follows. 1. As demostrated by the experimental results and analyses concerning their effects in the on-ground type mushroom house, the constructions in relation to the side wall and ceiling of the experimental houses showed a sufficient heat insulation on effect to protect insides of the houses from outside climatic conditions. 2. As the effect on the solar type experimental mushroom house which was constructed in a half basement has been shown by the experimental results and analyses, it has been proved to be effective for making use of solar heat. However there were found two problems to be improved for putting solar houses to practical use in the farm mushroom growing: (1) the construction of the roof and ceiling should be the same as for the on-ground type house, and (2) the solar heat generating system should be reconstructed properly. A trial solar heat generating system is shown in Fig. 40. 3. Among several ventilation systems which have been studied in the experiments, the underground earthen pipe and ceiling ventilation, and vertical side wall and ceiling ventilation systems have been proved to be most effective for natural ventilation. 4. The experimental results have shown that ventilation systems such as the vertical side wall and underground ventilation systems are suitable to put to practical use as natural ventilation systems for farm mushroom houses. These ventilation systems can remarkably improve the temperature of fresh air which is introduced into the house by heat transfers within the ventilation passages, so as to approach to the desired temperature of the house without any cooling or heating operation. For example, if it is assuming that x is the outside temperature and y is the amount of temperature adjustment made by the influence of the ventilation system, the relationships that exist between x and y can be expressed by the following regression lines. Underground iron pipe ventilation system ${\cdots}{\cdots}$ y=0.9x-12.8 Underground earthen pipe ventilation system ${\cdots}{\cdots}$y=0.96x-15.11 Vertical side wall ventilation system${\cdots}{\cdots}$ y=0.94x-17.57 5. The experimental results have shown that the relationships existing between the admitted and expelled air and the $Co_2$ concentration can be described with experimental regression lines or an exponent equation as follows: 1) If it is assumed that x is an air speed cm/sec. and y is an expelled air speed in cm/sec. in a natural ventilation system, since the y is a function of the x, the relationships that exist between x and y can be expressed by the regression lines shown below: 2) If it is assumed that x is an admitted volume of air in $m^3/hr$ and y is an expelled volume of air in $m^3/hr$ in a natural ventilation system, since the y is a function of the x, the relationships that exist between x and y can be expressed by the regression lines shown below. 3) If it is assumed that the expelled air speed in cm/sec and replacement air speed in cm/sec. at the bed surface in a natural ventilation system are shown as x and y, respectively, since the y is a function of the x, the relationships that exist between x and y can be expressed by the following regression line: G.E. (100%)- C.V. (50%) ventilation system${\cdots}$ y=0.54X+0.84 4) If it is assumed that the replacement air speed in cm/sec. at the bed surface is shown as x, and $CO_2$ concentration which is expressed by multiplying 1000 times the actual value of $CO_2$ % is shown as y, in a natural ventilation system, since the y is a function of the x the relationships that exist between x and y can be expressed by the following regression line: G.E. (100%)- C.V. (50%) ventilation system${\cdots}{\cdots}$ y=114.53-6.42x 5) If it is assumed that the expelled volume of air is shown as x and the $CO_2$ concentration which is expressed by multiplying 1000 times the actual of $CO_2$ % is shown as y in a natural ventilation system, since the y is a function of of the x, the relationships that exist between x and y can be expressed by the following exponent equation: G.E. (100%)-C.V. (50%) ventilation system${\cdots}{\cdots}$ $$y=127.18{\times}1.0093^{-X}$$ 6. The experimental results have shown that the ratios of the crass sectional area of the G.E. and C.V. vent to the total cubic capacity of the house, required for providing an adequate amount of air in a natural ventilation system, can be estimated as follows: G.E. (admitting vent of the underground ventilation)${\cdots}{\cdots}$ 0.30-0.5% (controllable) C.V. (expelling vent of the ceiling ventilation)${\cdots}{\cdots}$ 0.8-1.0% (controllable) 7. Among several heating devices which were studied in the experiments, the hot-water boilor which was modified to be fitted both as hot-water toiler and as a pressureless steam-water was found most suitable for farm mushroom growing.

  • PDF

Characteristics of Coal Slurry Gasification under Partial Slagging Operating Condition (부분 용융 운전 조건에서 석탄슬러리 가스화 운전 특성)

  • Lee, Jin Wook;Chung, Seok Woo;Lee, Seung Jong;Jung, Woohyun;Byun, Yong Soo;Hwang, Sang Yeon;Jeon, Dong Hwan;Ryu, Sang Oh;Lee, Ji Eun;Jeong, Ki Jin;Kim, Jin Ho;Yun, Yongseung
    • Korean Chemical Engineering Research
    • /
    • v.52 no.5
    • /
    • pp.657-666
    • /
    • 2014
  • Coal gasification technology is considered as next generation clean coal technology even though it uses coal as fuel which releases huge amount of greenhouse gas because it has many advantages for carbon capture. Coal or pet-coke slurry gasification is very attractive technology at present and in the future because of its low construction cost and flexibility of slurry feeding system in spite of lower efficiency compared to dry feeding technology. In this study, we carried out gasification experiment using bituminous coal slurry sample by integrating coal slurry feeding facility and slurry burner into existing dry feeding compact gasifier. Especially, our experiment was conducted under fairly lower operation temperature than that of existing entrained-bed gasifier, resulting in partial slagging operation mode in which only part of ash was converted to slag and the rest of ash was released as fly ash. Carbon conversion rate was calculated from data analysis of collected slag and ash, and then cold gas efficiency, which is the most important indicator of gasifier performance, was estimated by carbon mass balance method. Fairly high performance considering pilot-scale experiment, 98.5% of carbon conversion and 60.4% of cold gas efficiency, was achieved. In addition, soundness of experimental result was verified from the comparison with chemical equilibrium composition and energy balance calculations.

Early Life History and Spawning Behavior of the Gobiid Fish, Mugilogobius abei (Jordan et Snyder) Reared in the Laboratory (모치망둑, Mugilogobius abei(Jordan et Snyder)의 산란행동(産卵行動)및 초기생활사(初期生活史))

  • Kim, Yong-Uk;Han, Kyeong-Ho
    • Korean Journal of Ichthyology
    • /
    • v.3 no.1
    • /
    • pp.1-10
    • /
    • 1991
  • Spawning behavior and development of eggs and larvae of Mugilogobius abei were observed in the laboratory at Pusan, Korea. The adult male of Mugilogobius abei was observed making nest-like spawning-bed to lay eggs and showing territorial and courtship behaviors. The eggs were transparent and spherical in shape, measuring 0.40~0.50 mm in diameter. They have a bundle of adhesive filaments at their basal end and a cluster of small oil globules. The eggs became ellipsoid shape after the insemination and measured about 0.93~0.96 mm on the long axis. Hatching began about 110 hours after fertilization at water temperature of $24.5{\sim}25.5^{\circ}C$. The newly hatched larvae were 2.04~2.10 mm in total length, with 24~25(8~9+16) myomeres. Many melanophore and guanophore are distributed on eye cups, gas bladder, optic vesicle and the caudal region. Four days after hatching the yolk and oil-globule were completely absorbed and the larvae attained a total length 2.20~2.35 mm. The larvae swam actively in the aquarium and start to practice feeding on the rotifer. Twelve days after hatching, the larvae averaged 3.20 mm in TL and the caudal notochord flex at $45^{\circ}$. Rudimental second dorsal, anal, caudal and ventral fins are also formed. The larvae attained 10.40~10.80 mm in TL, 35 days after hatching, are found to start the bottom-life after having completely formed first dorsal and ventral fins. The larvae reached the juvenile stage at 50~60 days after hatching and attained 15.37~20.25 mm in TL. At this period all scales appeared on the body.

  • PDF