• Title/Summary/Keyword: Automotive Seat Assembly Line

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RFID-based Verification System and Method for Improving Quality of a Automotive Seat Assembly Line (자동차 시트 조립공정에서의 품질 향상을 위한 RFID기반 검증시스템 및 방법)

  • Kim, Heejin;Choi, Byoungju;Park, Chanmok
    • Journal of Information Technology Services
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    • v.12 no.4
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    • pp.175-186
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    • 2013
  • Among many automotive manufacturing processes, an assembly process has the smallest automatization percentage. As the correct assembly of the supplied components according to its specification is directly related with the quality of the final product, it is of the utmost importance to reduce the possible human errors in the assembly line. However, due to the lack of an effective verification system for an assembly line, currently, there is huge cost loss caused by the errors in seat assembly every year. Therefore, in this paper, to overcome the limit of the current verification method and to prevent the occurrence of assembly errors caused by mismatching assembling components or its specifications, a verification system and its method is proposed employing the RFID technology. The system is for automatic detection of the assembly errors, so that it can reduce the time and effort needed for verification and maximize the work efficiency. Also, by preventing the assembly errors in advance, the productivity can be increased through a quality innovation.

A Study on Development of Pre-heat Treated Steel Head Bolt for Swashplate Type Compressor of Car Air-conditioner (차량용 에어컨 압축기의 선조질강 헤드 볼트 개발에 대한 연구)

  • Kim, Youngshin;Kim, Hokyoum;Hwang, Seungyong;Kim, Youngman
    • Transactions of the Korean Society of Automotive Engineers
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    • v.24 no.5
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    • pp.588-595
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    • 2016
  • This paper is a study on head bolts that are used in A/C compressors to reduce production cost and solve leak problems on the head bolt seat area that causes massive intermittent malfunctioning during production. In this study, the pre-heat treated steel, which was used as a material in the head bolt, eliminated the heat treatment process after forging. The pre-heat treated steel head bolts, which have 10 % lower tensile strength than the conventional SCM 435 head bolts, were selected after considering the results of creeping rupture properties, axial force, and stress concentration per tensile strength variation. Then, the performance test and the durability test with the A/C compressor that was assembled with the pre-heat treated steel head bolts were performed and verified. Based on the results, the pre-heat treated steel head bolts developed in this study saved 7.3 % in production cost by eliminating the heat treatment process and the logistics process. Furthermore, the leak problem on the head bolt seat area in the A/C compressor was addressed significantly on the mass production assembly line.