• 제목/요약/키워드: Assembly torque

검색결과 99건 처리시간 0.026초

카메라 모듈 부품 및 금형 코어 측정 시스템 개발 (Development of the inspection system for injection molding core and mobile camera module parts)

  • 신봉철;김건희;김재철;조명우
    • 한국산학기술학회논문지
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    • 제10권1호
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    • pp.12-18
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    • 2009
  • 본 논문에서는 고품질 고기능성이 요구되는 카메라폰용 카메라 모들의 주요 부품인 초소형 플라스틱 barrel, base의 조립 토크 편차 저감을 위하여 금형 코어, 전극 및 사출성형품의 나사 형상의 주요 기하를 정밀하게 측정할 수 있는 시스템을 개발하였다. 해당 공정을 실현하기 위하여 품질 평가의 주요 측정 파라메터를 선정하고 측정 방법을 개발하였으며, 최종적으로 현장 적용이 가능한 전용 측정 시스템을 개발하였다.

The effect of bolt tightening methods and sequence on the performance of gasketed bolted flange joint assembly

  • Abid, Muhammad;Khan, Yasir Mehmood
    • Structural Engineering and Mechanics
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    • 제46권6호
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    • pp.843-852
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    • 2013
  • This paper presents results of the effect of different bolt tightening sequences and methods on the performance of gasketed bolted flange joint using nonlinear finite element analysis. Bolt preload scatter due to elastic interactions, flange stress variation and bolt bending due to flange rotation and gasket contact stress variation is difficult to eliminate in torque control method i.e. tightening one bolt at a time. Although stretch control method (tightening more than one bolt at time) eradicates the bolt preload scatter, flange stress variation is relatively high. Flange joint's performance is compared to establish relative merits and demerits of both the methods and different bolt tightening sequences.

회전 라이너를 이용한 엔진 마찰저감 (Engine Friction Reduction Through Liner Rotation)

  • 주신혁;김명진;;전광민
    • 한국자동차공학회논문집
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    • 제14권1호
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    • pp.31-38
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    • 2006
  • Cylinder liner rotation is a new concept for reducing piston assembly friction in the internal combustion engine. The purpose of cylinder liner rotation is to reduce the occurrence of boundary and mixed lubrication friction in the piston assembly. This paper reports the results of experiments to quantify the potential of the rotating liner engine. A GM Quad-4 SI engine was converted to single cylinder operation and modified for cylinder liner rotation. The hot motoring method was used to compare the friction loss between the baseline engine and the rotating liner engine. Additionally, tear-down tests were used to measure the contribution of each engine component to the total friction torque. The cycle-averaged motoring torque of the RLE represents a $23\~31\%$ friction reduction compared to the baseline engine for hot motoring tests. Through tear down tests, it was found that the piston assembly friction of the baseline engine is reduced from $90\%$ at 1200 rpm to $71\%$ at 2000 rpm through liner rotation.

접촉센서의 형상과 힘/토크 정보를 이용한 로봇조립 (Robotic Assembly Using Configuration and Force/Torque Information of Tactile Sensor System)

  • 강이석;김근묵;윤지섭;조형석
    • 대한기계학회논문집
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    • 제16권12호
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    • pp.2315-2327
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    • 1992
  • 본 연구에서는 조립될 부품사이의 위치 오차를 극복하여, 로봇에 의한 정밀부 품의 자동조립을 가능하게 하는 조립알고리즘을 제시하였다. 제안된 조립알고리즘은 임의로 파지된 자세를 인식하여 조립될 축과 구멍의 중심선을 일치시키는 알고리즘과 복합위치 및 힘제어(hybrid position/force control)를 적용하여 위치오차를 극복하여 주는 구멍검색 알고리즘으로 구성하였으며, 로봇을 이용한 자동조립에 제안된 알고리 즘을 적용한 실험 결과를 보였다.

진공청소기용 팬-모터 어셈블리의 시스템-레벨 분석 (System-level Analysis of a Fan-motor Assembly for Vacuum Cleaner)

  • 박창환;박경현;장경식
    • 한국유체기계학회 논문집
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    • 제20권1호
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    • pp.5-14
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    • 2017
  • A fan-motor assembly in a vacuum cleaner is analyzed through system-level analysis method. This system consisted of three components, a fan, motor, and the flow resistance of the motor, or of the vacuum cleaner. System-level analysis method is characterized by the combination of torque matching at a constant throttling condition between the fan and the motor and the pressure drop at a constant flow rate due to the flow resistance of the motor, or of the vacuum cleaner. The performance characteristics of the fan-motor assembly and the vacuum cleaner system could be predicted over the whole range of operation, based on the characteristics of each component. The predicted performance of the vacuum cleaner system through system-level analysis agreed well with the experimental results within 4.5% difference of pressure and 6% difference of the efficiency. The effect of flow resistance of a motor is investigated and it is found that the efficiency decrease of fan-motor assembly at the constant flow rate due to the flow resistance of a motor is determined by the flow resistance ratio(FRR), which is defined as a ratio of flow resistance of motor and the flow resistance of a constant throttling condition of a given point. The fan-motor assembly(S2 model) was modified to reduce the FRR from 9.0% to 2.4% and the experimental result shows that the efficiency of S2 model was improved by about 3% at best efficiency point.

무고정조립작업을 위한 협조 로봇 매니퓰레이터의 제어 (control of Two-Coopearationg Robot Manipulators for Fixtureless Assembly)

  • 최형식
    • 한국정밀공학회:학술대회논문집
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    • 한국정밀공학회 1996년도 춘계학술대회 논문집
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    • pp.427-431
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    • 1996
  • A modeling of the dynamics of two cooperating robot manipulators doing assembly job such as peg-in-hole while coordinating the payload along the desired path is proposed. The system is uncertain due to the unknown mass and moment of inertia of the manipulators and the payload. To control the system, a robust control algorithm is proposed. The control algorithm includes fuzzylogic. By the fuzzy logic, the magnitude of the input torque of the manipulators is controlled not to go over the hardware saturation with keeping path tracking errors bounded.

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수정된 RLS 기반으로 관절 토크 센서를 이용한 로봇에 가해진 외부 힘 예측 및 펙인홀 작업 구현 (External Force Estimation by Modifying RLS using Joint Torque Sensor for Peg-in-Hole Assembly Operation)

  • 정유석;이철수
    • 로봇학회논문지
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    • 제13권1호
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    • pp.55-62
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    • 2018
  • In this paper, a method for estimation of external force on an end-effector using joint torque sensor is proposed. The method is based on portion of measure torque caused by external force. Due to noise in the torque measurement data from the torque sensor, a recursive least-square estimation algorithm is used to ensure a smoother estimation of the external force data. However it is inevitable to create a delay for the sensor to detect the external force. In order to reduce the delay, modified recursive least-square is proposed. The performance of the proposed estimation method is evaluated in an experiment on a developed six-degree-of-freedom robot. By using NI DAQ device and Labview, the robot control, data acquisition and The experimental results output are processed in real time. By using proposed modified RLS, the delay to estimate the external force with the RLS is reduced by 54.9%. As an experimental result, the difference of the actual external force and the estimated external force is 4.11% with an included angle of $5.04^{\circ}$ while in dynamic state. This result shows that this method allows joint torque sensors to be used instead of commonly used external sensory system such as F/T sensors.

캠코더용 Iris Assembly의 국산화 및 생산 기술 개발 사례 (A Study of Development and Product ion Technology for Camcoder Iris Assembly)

  • 고종선
    • 대한전기학회:학술대회논문집
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    • 대한전기학회 1996년도 하계학술대회 논문집 A
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    • pp.250-252
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    • 1996
  • In this paper, the principle of operation. the part characteristic, characteristic of component movement, analysis are carried out for camcoder iris assembly which is one of the important element component in Video large projection TV instrument, and some Know-how for development of element component is also included. The magnetic field circuit for the small and simple structure with low power consumption is introduced and new materials of yoke for small motor system is suggested. Especially, the relation with remained magnetic field and operation duration time is analyzed by experimental results. Some problems of nonlinear torque characteristics include to obtain the simple and low cost structure in domestic production of element component is analyzed. Furthermore, development procedure is suggested for iris assembly and some methods to reduce the burr with some check points for small precise accessories are explained.

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모바일 폰 카메라 모듈 금형기술 개발 (Development of Die Technology of Mobile Phone Camera Module)

  • 박준홍;전언찬;김태호;문순균
    • 한국기계가공학회지
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    • 제7권4호
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    • pp.17-23
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    • 2008
  • Development of die technology for holder and barrel dies is necessary according to minimization of lens assembly, image sensor, and connectors. In these cases, there are two technical problems arising from die design. One is determination of knock-out pin location in die set. Minimization of lens assembly size make it difficult to obtain ejecting space. The other is whether or not high-precision die technology is possible to reduce torque variation when holer and barrel products is assembled. In this study, multi-cavity die set was developed taking advantage of gear-driven ejecting method. In the developed technology, die manufacturing technology was guaranteed with a high-precision level.

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센서퓨젼 기술을 이용한 정밀조립작업 (Precise assembly task using sensor fusion technology)

  • 이종길;이범희
    • 제어로봇시스템학회:학술대회논문집
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    • 제어로봇시스템학회 1993년도 한국자동제어학술회의논문집(국내학술편); Seoul National University, Seoul; 20-22 Oct. 1993
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    • pp.287-292
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    • 1993
  • We use three sensors such as a vision sensor, a proximity sensor, and a force/torque sensor fused by fuzzy logic in a peg-in-hole task. The vision and proximity sensors are usually used for gross motion control and the information is used here to position the peg around the hole. The force/torque sensor is used for fine motion control and the information is used to insert the peg into the hole precisely. Throughout the task, the information of all the three sensors is fused by a fuzzy logic controller. Some simulation results are also presented for verification.

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