• Title/Summary/Keyword: As-welded

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Eruption Styles and Processes of the Dongmakgol Tuff, Cheolwon Basin, Korea (철원분지 동막골응회암의 분출유형과 분출과정)

  • Hwang, Sang Koo;Son, Yeong Woo;Choi, Jang O;Kim, Jae Ho
    • The Journal of the Petrological Society of Korea
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    • v.22 no.1
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    • pp.49-62
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    • 2013
  • The Dongmakgol Tuff is divided into 8 lithofacies based on their grain size and depositional structures: massive tuff breccia(TBm), welded tuff and lapilli tuff(LTw), rheomorphic tuff and lapilli tuff(LTr), massive lapilli tuff(LTm), stratified lapilli tuff(LTs), gradedly bedded lapilli tuff(LTg), crudely bedded lapilli tuff(LTb) and massive fine tuff(Tm). They can be divided into 3 pyroclastic rock group based on their constituents of the lithofacies. The lower group(LI) is composed of LTm, LTw and LTr, which are interpreted to have resulted from emplacement of voluminous pyroclastic flows due to ignimbrite-form eruption to boiling-over eruption. The middle group(LT+MI) consists of LTs, LTg and LTm associated with Tm in the lower part, and of LTm, LTw and LTr in the middle and upper parts; these suggest that started with deposition of pyroclastic surges from phreatoplinian eruption by poor eternal water, passed through emplacement of pyroclastic flows from ignimbrite-form eruption and ended with deposition of voluminous pyroclastic flows from boiling-over eruption. The upper group(lUT+uUT+UI) is composed of LTs, LTg and Tm in the lowermost, TBm, LTb, LTb and Tm in the lower part, and LTm and LTw in the middle and upper part, suggesting that began with deposition of surges from phreatoplinian eruption, passed through deposition of pumice- and ash-fallouts from plinian eruption and transformed into emplacement of pyroclastic flows due to boiling-over eruption. As result, eruptive processes in the Dongmakgol Tuff approximately began with phreatoplinian or/and plinian eruption, transformed into ignimbrite-forming eruption and proceeded into boiling-over eruption in each volcanism, but proceeded presumably without phreatoplinian or plinian eruption in the earlier stage of 1st volcanism.

Development of heat exchanger for underground water heat. II - Design and manufacture for heat exchanger of underground water - (지하수 이용을 위한 열교환기 개발. II - 지하수이용 냉·난방기 설계제작 -)

  • Lee, W.Y.;Ahn, D.H.;Kim, S.C.;Park, W.P.;Kang, Y.G.;Kim, S.B.
    • Journal of Practical Agriculture & Fisheries Research
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    • v.4 no.1
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    • pp.128-137
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    • 2002
  • This study was conducted to develop the heat exchanger by utilizing the heat energy of underground water(15℃), which might be used for cooling and heating system of the agricultural facilities. We developed the heat exchanger by using the parallel type plat fin tube made of Aluminum(Al 6063), which was named Aloo-Heat(No. 0247164, offered by Korean Intellectual property Office). The trial manufactures were made from Aloo-heat which was 600mm, 700mm length respectively, and It were welded to the end "U" type in order to direct flow of the underground water. The performance test was carried out under the condition of open space and room temperature with the change of flow rate of the underground water and air. The results are as follows. 1. The trial manufactures had convection heat value from 33 to 156 W/m2℃, and It was coincided with design assumption. 2. The amount of energy transfer was increased with the increment of the area of heat transfer, the air flow, the gap of temperature inlet & outlet the underground water and the air. 3. The heat value was 6,825W when the air flow was 6,000m3/h and the gap of temperature between inlet and outlet of the underground water was 6℃, and It dropped from 25.8℃ to 23.2℃(-2.6℃ difference). The convection heat value was 88.5W/m2℃. 4. The heat value was 2.625W when the air flow was 4,000m3/h and the gap of temperature between inlet and outlet the underground water was 2℃, and It dropped from 27℃ to 22.5℃(-4.5℃ difference). The convection heat value was 33.6W/m2℃. 5. Correlation values(R2) of the testing heat values of the trial manufacture type I, II, and III were 0.9141, 0.8935, and 0.9323 respectively, and correlation values(R2) of the amount of the air flow 6,000m3/h, 5,000m3/h, 4,000m3/h were 0.9513, 0.9414, and 0.9003 respectively.