• Title/Summary/Keyword: 500MW Thermal Power Plant

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Performance Analysis of Upgrading Process with Amine-Based CO2 Capture Pilot Plant

  • Kwak, No-Sang;Lee, Junghyun;Lee, Dong Woog;Lee, Ji Hyun;Shim, Jae-Goo
    • KEPCO Journal on Electric Power and Energy
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    • v.4 no.1
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    • pp.33-38
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    • 2018
  • This study applied upgrades to the processes of a 10 MW wet amine $CO_2$ capture pilot plant and conducted performance evaluation. The 10 MW $CO_2$ Capture Pilot Plant is a facility that applies 1/50 of the combustion flue gas produced from a 500 MW coal-fired power plant, and is capable of capturing up to 200 tons of $CO_2$. This study aimed to quantitatively measure efficiency improvements of post-combustion $CO_2$ capture facilities resulting from process upgrades to propose reliable data for the first time in Korea. The key components of the process upgrades involve absorber intercooling, lean/rich amine exchanger efficiency improvements, reboiler steam TVR (Thermal Vapor Recompression), and lean amine MVR (Mechanical Vapor Recompression). The components were sequentially applied to test the energy reduction effect of each component. In addition, the performance evaluation was conducted with the absorber $CO_2$ removal efficiency maintained at the performance evaluation standard value proposed by the IEA-GHG ($CO_2$ removal rate: 90%). The absorbent used in the study was the highly efficient KoSol-5 that was developed by KEPCO (Korea Electric Power Corporation). From the performance evaluation results, it was found that the steam consumption (regeneration energy) for the regeneration of the absorbent decreased by $0.38GJ/tonCO_2$ after applying the process upgrades: from $2.93GJ/ton\;CO_2$ to $2.55GJ/tonCO_2$. This study confirmed the excellent performance of the post-combustion wet $CO_2$ capture process developed by KEPCO Research Institute (KEPRI) within KEPCO, and the process upgrades validated in this study are expected to substantially reduce $CO_2$ capture costs when applied in demonstration $CO_2$ capture plants.

Feed Water Flow Control of Super Critical Once Through Boiler in Korea Standard Power Plant (한국표준형 초 임계압 관류형 보일러의 급수제어)

  • 김은기;장용창;조수현
    • 제어로봇시스템학회:학술대회논문집
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    • 2000.10a
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    • pp.251-251
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    • 2000
  • Tangjin Power Plant is modern Korean standard plant which is made up Once Through Super Critical Boiler, Turbin, Generator and Flue Gas Desulfarization System. INFI-90 system fur control of the 500 MW Korean standard super critical once through boiler Mark-V for Turbine, EX-2000 fer Generator, WDPF for FGD were installed in Tangiin thermal power plant. There were two BFPTs, BFPM, 25% control valve, 35% control valve to control boiler feed water flow. It is very difficult to tune the Separator Tank level control system and change the mode from Wet to Dry. This paper focuses on test results and modification control logic for feed water control system in Tangjin power plant.

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A Study on the safety measures for hydrogen cooling system of 500MW class thermal power plant (500MW급 화력발전소 수소냉각시스템의 안전대책)

  • Kim, Soon-Gi;Yuk, Hyun-Dai;Ka, Chool-Hyun
    • Proceedings of the Korean Institute of IIIuminating and Electrical Installation Engineers Conference
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    • 2005.05a
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    • pp.385-390
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    • 2005
  • This paper provided a counter measures against the troubles and accidents that are likely to take place in the power plant using hydrogen gas as a coolant for the cooling system of the generator. Because of the extremely wide flammability limits of hydrogen in comparison to the other flammable gases, the safety measures against the hydrogen accidents is very important to ensure the normal operation of electric-power facility. This study's purpose was a presentation of standard model of safety management of hydrogen equipments in the coal firing power plant such as following items: 1) providing the technical prevention manual of the hydrogen explosions and hydrogen fires occurring in the cooling system of power generator; 2) the selection of explosion-proof equipments in terms of the risk level of operating environment; 3) the establishment of regulations and counter measures, such as the incorporation of gas leakage alarm device, for preventing the accidents from arising; 4) the establishment of safety management system to ensure the normal operation of the power plant.

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Modelling of Power Plant Fan Pitch Blade Control Actuator (전력설비 대용량 보일러 통풍기 날개각 제어 작동기 모델링)

  • Huh, J.Y.;Son, T.H.
    • Transactions of The Korea Fluid Power Systems Society
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    • v.4 no.2
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    • pp.28-33
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    • 2007
  • In the power plant facility which use soft coal as a power source the fan pitch blade control hydraulic actuator is used to control the inlet and outlet gas to regulate the internal pressure of the furnace and control the frequence. Sometimes malfunctions of this equipment lead to the decline of boiler thermal efficiency and unexpected power plant trip. In order to localize the fan pitch blade control hydraulic actuator specially for the 500MW large scale boiler, Analysis and modelling of the system is carried out mathematically. The responses of the system are examined by using matlab simulation fur the variation of the major parameters in view of reverse engineering. Consequently the validity of the established parameters are examined.

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A Study of Reheater Temperature Control on an Once through boiler in 500MW Thermal Power Plant (500MW 화력발전소 관류보일러 재열기 온도제어에 관한 연구)

  • Lee, Joo-Hyun;Lim, Ick-Hun;Park, Doo-Yong;Yu, Kwang-Myung;Byun, Seung-Hyun
    • Proceedings of the KIEE Conference
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    • 2011.07a
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    • pp.1838-1839
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    • 2011
  • 최근 국내 표준 화력발전소는 대부분 초 임계압의 관류형 보일러가 설치되어 운전되고 있다. 보일러 출구 증기온도를 정격치 이내로 운전하는 것은 보일러 운전에 중요한 요소이다. 보일러 효율 상승 등을 고려하여 재열기 Tube 재질의 온도 허용 한계치 이내에서 운전이 되어야 한다. 본 논문은 화력발전소에서 부하변동 범위가 넓고, 고효율 운전이 가능한 초 임계압 관류보일러의 온도제어 계통 구성과 재열기 온도제어로직에 대하여 기술하고자 한다.

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Economic Analysis of Dry Bottom Ash Handling System in a Pulverized Coal Thermal Power Plant in Korea (Ⅱ) -Case Study for Retrofitting the Existing Facility (國內 微分炭 化力發電所에서 바닥재 再活用을 위한 乾式 바닥재 處理시스템 導入의 經濟性 分析 (Ⅱ) -旣存設備 改善事業에 대하여)

  • Oh, Se-Won
    • Resources Recycling
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    • v.14 no.2
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    • pp.56-61
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    • 2005
  • Economic feasibility for retrofitting the wet bottom ash handling system to the dry system in a existing 500MW${\times}$2 units pulverized coal thermal power plant in Korea was studied. Replacing to the dry system requires the initial capital costs of 13,415,127,000\, and saves the operating costs of 935,345,000\ per year. Economic analyses based on these results showed that the initial capital cost would not be recovered within the service life of the facilities at the interest rate of 10%, and the internal rate of return of 5.6% were obtained. Thus, the retrofitting to the dry system was not economically favorable in the current condition. However, the retrofitting would be profitable when the ash disposal cost and ash selling price were increased over 15,000\/MT or 17,000\/MT, respectively.

A Study of Function Verification of Digital Excitation System with Real Time Simulator (시뮬레이터 탑재형 디지털 여자시스템 기능검증 시험에 관한 연구)

  • Ryu, Ho-Seon;Shin, Man-Su;Lee, Joo-Hyun;Lim, Ick-Hun
    • Proceedings of the KIEE Conference
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    • 2011.07a
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    • pp.1191-1192
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    • 2011
  • We released new triple redundant digital excitation system with real time generator-turbine simulator. One of its great merits is the real time generator-turbine simulator when it was compared with the other products. If excitation system is tripped by unexpected faults, Maintenance man can do easily performance test of digital excitation control board, sequence relay and thyristor switching device of phase controlled rectifier without manufacturer's support. For the verification of this system, It was tested with an actual excitation system implemented on 5kVA M-G Set. After finishing the tests, the trial product will be installed and operated at a 500MW thermal power plant.

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Characteristics of Unburned Material Derived from Coal-fired Power Plant Burning Low Grade Coal (저급탄 연소 석탄회의 미연물질 특성 분석)

  • Park, Ho-Young;Kim, Young-Ju;Kim, Tae-Hyung;Baek, Se-Hyun;Kim, Kyung-Soo;Jeoung, Kwon-Dal
    • Journal of Energy Engineering
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    • v.21 no.1
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    • pp.68-74
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    • 2012
  • Sub-bituminous coals have been used increasingly in coal-fired power plants with a proportion of over 50% in the blend with bituminous coals. As a result, the unburned material in fly ash has increased and is causing problems in utilizing the fly ash as an additive for concrete production. In this study, analysis of fly ash obtained from a 500 MWe power plant was carried out and unburned material in the fly ash found to be soot. The coals used in the plant were analyzed with CPD model to investigate the sooting potential depending on the coal type and blending ratio.

Noise influence Coming to Existing Neighborhood Area by Extension of Power Site and Noise Reduction Service (발전소 증절이 부지경계의 가존 지역에 미지는 소음영향과 저감 대책)

  • Kim, Yeon-Whan;Goo, Jae-Rayng;Bae, Chun-Hee;Kim, Kye-Yean;Yang, Dong-Cheol
    • Proceedings of the Korean Society for Noise and Vibration Engineering Conference
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    • 2009.10a
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    • pp.716-722
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    • 2009
  • 4000MW급 유연탄발전소는 기존 500MW급 4기의 발전설비 운영조건에서 지역공동체는 긍정적이었으나, 500MW급의 증설 호기가 늘어나면서 지역 공동체는 발전소 증설과 관련하여 기존 동쪽 부지 경계지역의 소음환경에 대하여 부정적인 문제를 제기하였다. 2000MW급 증설이 진행되어온 4000MW급 발전소의 다양한 소음원에 의한 소음파워 증대와 증가방출 과도소음 에 대하여 고저가 다양한 주변지역에 미치는 영향음 평가하고자 3차원 모델링기법을 적용한다. 기존호기를 비롯한 전체의 발전소 전면부 소음원응 비교 시험결과 증가방출 소음 파워가 기존 설계의 변경 제작되어 기존호기에 비해 20~30dBA 높아져 동시 방출사 주변지역에 과도하게 영향을 미치는 상태였으며 500MW급 4기를 추가 증설에 따라 일상소음원에 의한 소음 영향도 증설전 대비 2~3dBA 증가된 것으로 평가되었다. 따라서 증설호기의 과도 소음원 제거 방안으로 대가 방출증가가 회수되도록 증설호기의 증가방출설비를 개선하였고, 증설에 의하여 증가된 소음 영향음 저감하고자 기존 경계지역에 미치는 소음원음 고려하여 방음벽음 설치한 결과 47 ~ 49dBA를 나타내고 인근 주거건물의 전면부 소음은 43dBA이었다.

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Suggestion of Logic to Control Power Plant Equipped ESS in case of Full Open Turbine Control Valve (ESS를 이용한 발전소 터빈제어밸브 전개 운전 제어로직 제안)

  • In Young Chung;Jae-Heon Lee
    • Plant Journal
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    • v.18 no.4
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    • pp.66-72
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    • 2023
  • In order to respond to the demand for flexible operation of thermal power generation, development of natural sliding pressure operation that minimizes throttle loss by opening the turbine control valve 100% and maximize power generation efficiency in conjunction with ESS in order to quickly respond to fluctuations in the system frequency is required. The logic development of natural sliding pressure operation with ESS was developed to modify the existing logic at the power plant's top-level control logic such as the unit master, the boiler master and the turbine master. Cooperative control algorithms that complement the advantages and disadvantages of ESS operation (quick response, limited capacity) and power plant operation (slow response, continuous operation) not only improve efficiency when applied to actual power plants, but also respond quickly and flexibly to load demands to ensure system stability.

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