• Title/Summary/Keyword: 허가배출기준

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NOx Emission Characteristics with Operating Conditions of SNCR in SRF Usage Facilities (고형연료제품 사용시설에서의 SNCR의 운전조건에 따른 NOx 배출특성)

  • Seo, Je-Woo;Kim, Younghee
    • Clean Technology
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    • v.27 no.4
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    • pp.350-358
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    • 2021
  • The results of this study shows that the combustor temperature ranged from 848.27 to 1,026.80 ℃, averaging about 976.61 ℃, and the NOx concentration increased as the temperature increased. The urea usage ranged from 291.00 to 693.00 kg d-1, averaging about 542.34 kg d-1, and the NOx concentration decreased as the urea usage increased. Residence time was about 3.38 to 9.17 s, averaging about 5.22 s, about 2.61 times larger than the 2 s of the design details. This is 1,086 kg h-1, averaging about 55.71%, compared to the 1,950 kg h-1 SRF input permission standard. The combustion chamber area is constant, but the residence time is shown to increase with the decrease of exhaust gas. The O2/CO ratio was 847.05 to 14,877.34, averaging about 3,111.30, and the NOx concentration slightly increased as the O2/CO ratio increased. As the combustor temperature and O2/CO ratio increased, the combustion reaction with nitrogen in the air increased and the NOx concentration slightly increased. As the urea usage and residence time increased, the NOx concentration decreased slightly with an increase in reactivity with NOx. The NOx concentration at the stack ranged from 7.88 to 34.02 ppm with an average of 19.92 ppm, and was discharged within the 60 ppm emission limit value. The NOhx emission factor was 1.058 to 1.795 kg ton-1, averaging about 1.450 kg ton-1. This value was about 24.87% of the maximum emission factor of 5.830 kg ton-1 of other solid fuels. Other synthetic resins and industrial wastes were 79.80% and 43.65% compared to 1.817 kg ton-1 and 3.322 kg ton-1, respectively. This value was similar to 1.400 kg ton-1 of RDF in the NIER notice (2005-9), 10.98% compared to the maximum SRF of 13.210 kg ton-1. Therefore, the NOx emission factor had a large deviation.

Eligibility Analysis of Land on a Reforestation CDM Project in Goseong District, South Korea (청정개발체제하 재 조림 사업의 토지적격성에 대한 사례 분석 -고성군 재조림 사업을 중심으로-)

  • Guishan, Cui;Kwon, Tae-Hyub;Lee, Woo-Kyun;Kwak, Hanbin;Nam, Kijun;Song, Yongho;Hangnan, Yu
    • Journal of Korean Society of Forest Science
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    • v.102 no.2
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    • pp.216-222
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    • 2013
  • For reducing greenhouse gases, many countries carried out a series of activities not only at home but abroad. Particularly, after the release of the Kyoto Protocol, either nation or companies' participation was intensified, due to endow to responsibility of emission limits. This study focused on reforestation CDM work in Goseong Gun based on clean development system. Obstacle factors of land eligibility could be distinguished to three periods: before December 31th 1989, present and future. The obstacle before December 31th 1989 was that land cover of study area hardly illustrated by Landsat image, due to the low resolution, which were confirmed by a document of Grassland Composition Permission instead. The problem of current land eligibility is that the area of trees presence are difficult to be determined as forest or not. The boundary of forest in strata was identified, using 3-Dimensional Cartography Machine and aerial photograph. Land eligibility would still have obstacle whether the study area with trees presence has potentiality to be forest in the future at situation in absence of reforestation project. This was resolved by prediction of tree growth using stem analysis during execution of the project at study area.

Development of the Safety Cabinet for Respiratory High-Pressure cylinder according to Consequence Analysis of Physical Explosion Damage (호흡용 고압용기 파열 피해영향 분석에 따른 안전충전함 개발)

  • Jang, Kap Man;Kim, Jeong Hwan;Jang, Yu Ri;Lee, Jin Han;Jo, Young Do
    • Journal of the Korean Institute of Gas
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    • v.20 no.6
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    • pp.80-88
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    • 2016
  • A fire station and scuba have operated filling facilities for respiratory high-pressure cylinder without getting authority or reporting according to High-Pressure Gas Safety Control Act. They need facility improvement and special management to make provision for the time of accident during filling process. The Government have strived to correct illegal operations and suggested an alternative, establishing and operating the safety cabinet. It insures a safety being distance from danger caused by overpressure and a safety provoked by the protective wall equals or superiors. The safety cabinet is required to have an internal structure that smoothly distribute overpressure at the time of rupture. Plus, it needs to minimize fragments. It is also equipped with the performance of protective wall that makes overpressure to outside vent on the place where there is no person (top or bottom). This study calculated the consequence of physical explosion damage and built a prototype of safety cabinet. In addition, through the gas burst test, it derives for the ways to mitigate the physical explosion damage.