• Title/Summary/Keyword: 연소가스 탈황설비

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Flow Analysis and Pressure Loss Calculation in the Ducts of FGD System (탈황설비 배관내 유동장 해석 및 압력손실 계산)

  • 고성모;이진욱;황금호
    • Proceedings of the Korea Society for Energy Engineering kosee Conference
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    • 1998.05a
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    • pp.21-25
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    • 1998
  • 탈황설비 배관내 연소가스의 삼차원 유동장에 대한 전산해석을 수행하였다. 복잡한 형상으로 주어진 배관내의 유동장 특성을 관찰하고 압력손실을 계산하였다. 특히 안개깃의 설치유무에 따른 유동장 특성 변화 및 압력손실 감소효과를 집중적으로 고찰하였다. 안내깃의 설치에 따라 유량배분이 적절하게 되고 압력손실이 현저하게 줄어듬을 알 수 있었다. 배관에서의 압력손실을 계산하여 배관설계 및 송풍기 용량 산정의 적절성을 확인할 수 있었다.

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CFD를 이용한 흡수탑 내 유동 균일효과 연구

  • 이춘만;이호경
    • Proceedings of the Korean Society of Precision Engineering Conference
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    • 2004.05a
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    • pp.106-106
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    • 2004
  • 보일러에서 연소된 후 배출된 가스는 탈황목적으로 설치된 흡수탑 내에 유입되어 Slurry Spray Nozzle에서 분사된 Limestone Slurry에 의해 배기가스중의 SO$_2$를 흡수한 다음 반응조로 떨어지게 되지만 분사된 액적의 일부는 배기가스의 압력에 의하여 같은 유동 방향으로 미세한 Mist의 형태로 배기가스와 함께 흡수탑의 Outlet Duct를 통해 빠져나간다. 이 Mist(액적크기 40 $\mu\textrm{m}$이하)에는 고형 성분이 함유되어 있는데 보통 Chloride농도가 높아 탈황설비 후단 (duct, GGH, Stack)에 plugging, 부식 등의 문제를 유발하므로 Spray Header상부에서 Mist Eliminator를 설치하여 Mist를 제거하도록 한다.(중략)

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Prediction of Cleaning Time of Desulfurization Absorber in a Oil-Fired Power Plant through the Operation Data (중유화력발전소의 운전자료를 이용한 탈황 흡수탑의 세정시기 예측)

  • Jang, Yeong-Gi;Lee, Jae-Heon
    • Plant Journal
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    • v.11 no.4
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    • pp.38-46
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    • 2015
  • 중유를 연소하는 D 발전소 탈황설비는 운전시간의 경과에 따라 흡수탑 중간층에 석고가 쌓이고 가스분사 파이프 내에 경질석고 스케일이 부착됨으로써 발전설비 및 탈황설비의 정상적인 운전이 어렵게 된다. 흡수탑 내부에 발생된 스케일을 제거하지 않을 경우에는 탈황효율의 저하에 따른 SO2 배출농도의 증가로 발전가능 최대출력의 하향조정이 발생되고 나아가 발전정지를 초래한다. 스케일 제거를 위한 탈황설비 세정은 발전가능 최대출력의 하향조정이 발생하는 시점으로 결정할 수 있다. 본 연구에서는 탈황설비의 운전 자료를 분석하여 발전가능 최대출력의 하향조정이 발생되기 6주 전은 탈황설비 출구 SO2 농도값이 130ppm을 초과하고 동시에 흡수탑 차압은 380mmH2O을 초과하며, 직전 흡수탑 세정 이후 44주가 경과된 시점이 됨을 확인하였다. 그리고 흡수탑의 세정시기는 세정준비기간 6주와 발전가능 최대출력 하향이 발생되기 6주 전까지의 운전경과일수 44주를 더하여 직전 세정시점으로부터 50주가 경과된 시점임을 예측하였다.

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Variation of Liquid to Gas Ratio and Sulfur Oxide Emission Concentrations in Desulfurization Absorber with Coal-fired Thermal Power Plant Outputs (석탄화력 발전설비의 출력에 따른 탈황 흡수탑 액기비와 황산화물 배출농도 변화에 대한 연구)

  • Kim, Kee-Yeong;Moon, Seung-Jae
    • Plant Journal
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    • v.14 no.4
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    • pp.39-47
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    • 2018
  • In this research, when the output of the standard coal-fired thermal power plant operating continuously at the rated output of 500 MW is changed to operate at 300 to 500 MW, the amount of sulfur oxide produced and the amount of sulfur oxide in the absorption tower of desulfurization equipment and proposed an extra liquid to gas ratio improvement inversely proportional to the output. In order to calibrate the combustion efficiency at low power, the ratio of sulfur oxides relative to the amount of combustion gas is increased as the excess air ratio is increased. When the concentration of sulfur oxide at the inlet of the desulfurization absorber was changed from 300 to 500 ppm along with the output fluctuation. The liquid to gas ratio of limestone slurry and combustion gas was changed from 10.99 to 16.27. Therefore, if the concentration of sulfur oxides with output of 300 MW is x, The following correlation equation is recommended for the minimum required flow rate of slurry for the reduction of surplus energy due to the increase of the liquid weight at low load. $y1[m^3/sec]=0.11x+3.74$

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Flue Gas Desulfurization System For Reducing SOx Emission In Thermal Power Plant (황산화물 저감을 위한 배연탈황설비 설치 사례)

  • 조승원;황영호;전상기
    • Proceedings of the Korea Air Pollution Research Association Conference
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    • 1999.10a
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    • pp.451-452
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    • 1999
  • 석탄이나 석유와 같은 화석연료의 연소 시 대기 중에 발생되는 황산화물의 배출저감 방법으로서 사용연료의 황 함유량을 감소시키는 연소 전 처리방법과 연소과정 중 제거방법, 연소 후 제거하는 방법으로 구분할 수 있다. 본 논문에서는 전기 생산능력 40만 kW 급 중유화력 발전소의 연료 연소 후 배기가스 중 황 성분을 제거하는 방법으로 석회석 슬러리와 배기가스를 효과적으로 접촉시켜 SOx 와 먼지 등의 환경오염물질을 제거하고 부산물로 재활용 가능한 고순도의 석고를 생산하게 되는 JBR (Jet Bubbling Reactor) 형식의 습식 석회석-석고법 배연탈황 시스템을 소개하고자 한다.(중략)

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Computational Fluid Dynamic Analysis for Improving the Efficiency of Desulfurization System for the Wet Flue Gas (습식 배연탈황 시스템의 효율 향상을 위한 전산해석)

  • Hwang, Woo-Hyeon;Lee, Kyung-Ok
    • Journal of the Korea Society of Computer and Information
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    • v.19 no.2
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    • pp.161-171
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    • 2014
  • In this paper the flow dynamics of the flue gas equipment in the desulfurization system was numerically analyzed by simulating the problems for the turbulent and combustion flow from Induced Draft Fan(I.D.Fan) outlet to Booster Up Fan(B.U.Fan) inlet using the commercial CFD software of CFD-ACE+ in CFDRC company for Computational Fluid Dynamic Analysis. The guide vane of this section was examined for the minimum pressure loss and the uniform flow dynamic to B.U.Fan with the proper velocity from I.D,Fan exit to B,U,Fan inlet section at the boiler both the maximum continuous rating and the design base. The guide vanes at I,D.Fan outlet and B.U.Fan inlet were removed and modified by numerical simulation of the CFD analysis. The flue gas at the system had the less pressure loss and the uniform flow dynamics of the flow velocity and flow line by comparing with the old design equipment.

Desirable pH of Slurry in the Desulfurization Absorber for a 200 MW Anthracite Power Plant (200 MW급 무연탄 발전용 탈황 흡수탑에서 적정 슬러리pH)

  • Choi, Hyun-Ho;Yoo, Hoseon
    • Plant Journal
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    • v.16 no.1
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    • pp.38-43
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    • 2020
  • In this study, Seochon Thermal Power Plant No.1 for anthracite coal was tested to find the proper operation range of limestone slurry pH in the absorber tower which can be operated continuously in compliance with the Air Quality Preservation Act and Seocheon Thermal Power Division's internal regulation, sulfur dioxide average emission regulation. When operating the sulfur dioxide concentration [ppm] in the combustion gas flowing into the desulfurization absorption tower at 370, 400, 460 and 550 ppm while the main operating elements such as the flow rate of the combustion gas were fixed, the proper slurry pH Were 4.4, 4.5, 4.8 and 5.1, respectively. Therefore, it is recommended to operate with the correlation equation, RpH=0.004×Cin+2.93 derived using sulfur dioxide and the appropriate slurry pH.

Analysis of cause of engine failure during power generation using biogas in sewage treatment plant (하수처리장 바이오가스를 이용한 발전시 가스엔진의 고장원인 분석)

  • Kim, Gill Jung;Kim, Lae Hyun
    • Journal of Energy Engineering
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    • v.25 no.4
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    • pp.13-29
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    • 2016
  • In this study, we analyzed the causes of major faults in the biogas plant through the case of gas engine failure when cogenerating electricity and heat using biogas as a fuel in the actual sewage treatment plant and suggested countermeasures. Hydrogen sulfide in the biogas entering the biogas engine and water caused by intermittent malfunction of the water removal system caused intercooler corrosion in the biogas engine. In addition, the siloxane in the biogas forms a silicate compound with silicon dioxide, which causes scratches and wear of the piston surface and the inner wall of the cylinder liner. The substances attached to the combustion chamber and the exhaust system were analyzed to be combined with hydrogen sulfide and other impurities. It is believed that hydrogen sulfide was supplied to the desulfurization plant for a long period of time because of the high content of hydrogen sulfide (more than 50ppm) in the biogas and the hydrogen sulfide was introduced into the engine due to the decrease of the removal efficiency due to the breakthrough point of the activated carbon in the desulfurization plant. In addition, the hydrogen sulfide degrades the function of the activated carbon for siloxane removal of the adsorption column, which is considered to be caused by the introduction of unremoved siloxane waste into the engine, resulting in various types of engine failure. Therefore, hydrogen sulfide, siloxane, and water can be regarded as the main causes of the failure of the biogas engine. Among them, hydrogen sulfide reacts with other materials causing failure and can be regarded as a substance having a great influence on the pretreatment process. As a result, optimization of $H_2S$ removal method seems to be an essential measure for stable operation of the biogas engine.

Practical Study of the Thermal Efficiency Improvement and the White Plume Removal from Flue Gas by Fuel Additive Injection (연료첨가제를 이용한 열효율향상 및 가시백연 제거에 관한 연구)

  • 전상기;조승원;황영호
    • Proceedings of the Korea Air Pollution Research Association Conference
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    • 2003.11a
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    • pp.487-488
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    • 2003
  • 우리나라 대기환경기준이 점차 강화되고 있고, 국민의 욕구수준 또한 선진국 수준으로 강화될 계획으로 있어 이에 따른 대기오염 방지시설의 설치 또는 보완이 요구되고 있다 특히, 배기가스 중 황산화물 및 질소산화물 배출농도 강화로 울산화력발전소에서는 최신의 배연탈황ㆍ탈질설비를 가동중에 있으나 황산 Mist가 주요원인으로 추정되는 Plume Opacity가 발생되어 오염물질 배출농도는 법적규제기준 이내로 배출되더라도 민원이 발생되고 있다. 이에 대한 대책으로 현장에 적합한 연료첨가제 주입으로 Plume Opacity 발생원인을 제거함과 동시에 배연탈황설비에서 발생된 저온부식 현상을 개선하고, 보일러 내 고온부식 등 연소장애 현상 개선을 통한 열효율 향상 방안에 대해 연구하였다. (중략)

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Study on the Desulfurization Characteristic of Limestone Depending on the Operating Parameters of In-Furnace Desulfurization for Oxy-Fuel Combustion Using Drop Tube Furnace (순산소연소 조건에서 Drop tube furnace를 이용한 운전변수에 따른 석회석의 탈황특성 연구)

  • Choi, Wook;Jo, Hang-Dae;Choi, Won-Kil;Park, Yeong-Sung;Keel, Sang-In;Lee, Hyung-Keun
    • Korean Chemical Engineering Research
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    • v.49 no.6
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    • pp.857-864
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    • 2011
  • Oxy-fuel combustion with many advantages such as high combustion efficiency, low flue gas flow rate and low NOx emission has emerged as a promising CCS technology for coal combustion facilities. In this study, the effects of the direct sulfation reaction on $SO_2$ removal efficiency were evaluated in a drop tube furnace under typical oxy-fuel combustion conditions represented by high concentrations of $CO_2$ and $SO_2$ formed by gas recirculation to control furnace combustion temperature. The effects of the operating parameters including the reaction temperature, $CO_2$ concentration, $SO_2$ concentration, Ca/S ratio and humidity on $SO_2$ removal efficiency were investigated experimentally. $SO_2$ removal efficiency increased with reaction temperature up to 1,200 due to promoted calcination of limestone reagent particles. And $SO_2$ removal efficiency increased with $SO_2$ concentrations and the humidity of the bulk gas. The increase of $SO_2$ removal efficiency with $CO_2$ concentrations showed that $SO_2$ removal by limestone was mainly done by the direct sulfation reaction under oxy-fuel combustion conditions. From the impact assessment of operation parameters, it was shown that these parameters have an effects on the desulfurization reaction by the order of the Ca/S ratio > residence time > $O_2$ concentration > reaction temperature > $SO_2$ concentration > $CO_2$ concentration > water vapor. The semi-empirical model equation for to evaluate the effect of the operating parameters on the performance of in-furnace desulfurization for oxy-fuel combustion was established.