• Title/Summary/Keyword: 수력성능

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Prediction of Hydraulic Performance of a Scaled-Down Model of SMART Reactor Coolant Pump (스마트 원자로냉각재펌프의 축소모형에 대한 수력성능 예측)

  • Kwon, Sun-Guk;Park, Jin-Seok;Yu, Je-Yong;Lee, Won-Jae
    • Transactions of the Korean Society of Mechanical Engineers A
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    • v.34 no.8
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    • pp.1059-1065
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    • 2010
  • An analysis was conducted to predict the hydraulic performance of a reactor coolant pump (RCP) of SMART at the off-design as well as design points. In order to reduce the analysis time efficiently, a single passage containing an impeller and a diffuser was considered as the computational domain. A stage scheme was used to perform a circumferential averaging of the flux on the impeller-diffuser interface. The pressure difference between the inlet and outlet of the pump was determined and was used to compute the head, efficiency, and break horse power (BHP) of a scaled-down model under conditions of steady-state incompressible flow. The predicted curves of the hydraulic performance of an RCP were similar to the typical characteristic curves of a conventional mixed-flow pump. The complex internal fluid flow of a pump, including the internal recirculation loss due to reverse flow, was observed at a low flow rate.

Water Performance Test of Pumps for a 7 Ton Class Rocket Engine (7톤급 로켓엔진용 펌프 수류 성능시험)

  • Hong, Soonsam;Kim, Daejin;Choi, Changho
    • Journal of the Korean Society of Propulsion Engineers
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    • v.19 no.3
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    • pp.89-95
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    • 2015
  • Performance test was conducted for an oxidizer pump and a fuel pump for a 7 ton class rocket engine, by using water. The pumps were driven by an electric motor. The hydrodynamic performance and the suction performance were measured at flow ratio of the design and off-design conditions. Head-flow curve, efficiency-flow curve, and head-cavitation number curve were obtained. It is confirmed that the pumps can satisfy the design requirements of hydrodynamic performance in terms of the head and the efficiency. The pumps also satisfied the design requirements of suction performance.

Water Tests of Lox Pump for 75-ton Class Liquid Rocket Engine (75톤급 액체로켓엔진용 산화제펌프의 수류시험)

  • Kim, Dae-Jin;Hong, Soon-Sam;Choi, Chang-Ho;Kim, Jin-Han
    • Aerospace Engineering and Technology
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    • v.10 no.1
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    • pp.122-128
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    • 2011
  • A series of water tests of a Lox pump for liquid rocket engines are performed at a room temperature. According to the hydraulic test results, the head coefficient is slightly decreased when the rotational speed of the pump is increased. However the efficiency is high at the high-speed test. Also, according to the cavitation test results, the cavitation performance of the pump is found to be decreased when the flow ratio is less than 92%. Furthermore, the vibration characteristic is analyzed using measured high frequency data.

로켓엔진용 연료펌프 전산유동해석

  • Noh, Jun-Gu;Choi, Chang-Ho;Kim, Jin-Han
    • Aerospace Engineering and Technology
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    • v.3 no.2
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    • pp.183-190
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    • 2004
  • The performance analysis of a fuel pump for a liquid rocket engine has been performed numerically on its design condition. A commercial three-dimensional Navier-Stokes flow solver has been used for the computation. All of the fuel pump components - inducer, impeller, volute and secondary flow passages - are included in computation for the accurate estimation of the leakage flow rate which affects the performance and axial thrust. A pitchwise-averaged mixing plane method was used on the boundaries among the fuel pump components to save computational time. The predicted overall performance satisfied the design requirement. However, the axial thrust exceeded a permissible limit. In order to reduce the axial thrust, the secondary flow passage design has been changed. With this change, the axial thrust level has been reduced to 30% as compared with the original value.

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로켓엔진용 연료펌프의 성능 시험

  • Kim, Dae-Jin;Hong, Soon-Sam;Choi, Chang-Ho;Kim, Jin-Han
    • Aerospace Engineering and Technology
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    • v.4 no.1
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    • pp.143-149
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    • 2005
  • To evaluate the hydraulic and cavitation performance of a fuel pump for a liquid rocket engine, performance tests of the pump, which consist of hydraulic tests and cavitation tests, were conducted in water environment with various condition. In the hydraulic tests, the head, efficiency and volute pressure distribution of the pump are found to follow the conventional similarity rule, whereas the secondary flow pressure shows a small deviation from the similarity rule. As the floating gap is constricted, the efficiency of the pump improves and the secondary flow pressure decreases. However, the inner diameter of bypass line orifice does not show clear relationship with the pump efficiency. In the cavitation tests, measurements of the head and the NPSH indicate that the pump shows better cavitation performance as the rotational speed of the pump increases.

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Application Study on Domestic Production of Francis Type Hydro Turbine at Irrigation Reservoir (농업용저수지를 이용한 프란시스수차 국산화 적용 연구)

  • Lee, Chul-Hyung;Park, Wan-Soon
    • Proceedings of the Korea Water Resources Association Conference
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    • 2009.05a
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    • pp.1632-1636
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    • 2009
  • 소수력자원은 신재생에너지 중에서도 온실가스 배출량이 가장 적고 에너지밀도가 매우 높기 때문에 개발할 가치가 큰 청정부존자원으로 평가되고 있다. 본 연구는 프란시스 수차의 국산화 개발 연구로써 프란시스수차 외형설계에 필요한 기본사항과 제작, 프란시스수차의 설치 및 시운전, 프란시스수차의 성능시험을 수행하였다. 이에 대한 분석 결과, 개발된 프란시스수차는 기계적인 성능과 수력학적인 성능면에서 만족할 만한 결과를 보여주어 프란시스수차의 상용화에 대한 기반이 마련되었다.

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The Effects of Distal Sinus on the Hydrodynamic Performance of the Prosthetic Heart Valves (인공판막 후부 공동부가 판막의 수력학적 성능에 미치는 영향)

  • 이계한;서종천
    • Journal of Biomedical Engineering Research
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    • v.19 no.3
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    • pp.297-303
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    • 1998
  • The sinus distal to the prosthetic heart valve influences the valve closure behavior and velocity field near the valve, therefore affects the hydrodynamic performance of the prosthetic heart valve. In order to study the effects of valve distal geometry on the hydrodynamic performance of the prosthetic valves, mechanical bileaflet valve(SJMV), monoleaflet polymer valve(MLPV) and trileaflet polymer valve(FTPV) are inserted in the test sections which have the straight and the sinus shape distal to the valve. Leakage volumes and systolic mean pressure drops are measured in the pulsatile mock circulation flow loop. Leakage volumes are slightly less and systolic mean pressure drops are higher in the sinus test section comparing to those in the straight test section, but the differences are statistically insignificant. Flow waveforms are analyzed in order to predict the valve closure behavior. The distal sinus does not affect the closure of the MLPV, but early valve closure of SJMV is observed in the sinus test section. This effect is more significant in FTPV, and the reverse flow peak of FTPV is reduced in the sinus test section. Therefore the sinus distal to the valve can reduce the reverse flow jet caused by sudden valve closure.

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Hydraulic Performance Analysis of a Francis Turbine (프란시스 수차의 수력학적 성능해석)

  • Yoon, Eui-Soo;Oh, Hyoung-Woo;Park, Moo-Ryong
    • 유체기계공업학회:학술대회논문집
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    • 2006.08a
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    • pp.53-56
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    • 2006
  • The hydraulic performances of a Francis turbine which had been designed and tested by IMHEF were calculated with a commercial code and compared with the IMHEF test results. The non-dimensional specific speed of the turbine is 0.5, the runner exit diameter 0.4m and maximum efficiency 93.1% respectively. To make the calculation of the turbine more exact, the stay vanes, the guide vane, the runner and the draft tube were calculated simultaneously. The calculation results gave a quite good agreement with the IMHEF test data, and therefore it is expected that the present calculation technique will be utilized for the hydraulic design of efficient Francis turbines.

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A Numerical Study on Improving the Thermal Hydraulic Performance of Printed Circuit Heat Exchanger Using the Supercritical Carbon Dioxide (초임계 이산화탄소를 작동유체로 한 PCHE의 열수력 성능 향상을 위한 수치해석적 연구)

  • Park, Bo Guen;Kim, Dae Hyun;Chung, Jin Taek
    • Transactions of the Korean Society of Mechanical Engineers B
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    • v.39 no.10
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    • pp.779-786
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    • 2015
  • The objective of this study is to propose a new channel shape that improves thermal-hydraulic performance. The existing Zigzag channel has high pressure loss due to flow separation and reverse flow. To improve this disadvantage, partial straight channel is inserted into bended points. Also, the effects of straight channel's length change on heat transfer and pressure loss are analyzed. Thermal-hydraulic performance of the new shape and existing Zigzag channel are quantitatively compared in terms of Goodness Factor. Mass flow rate was changed from $1.41{\times}10^{-4}$ to $2.48{\times}10^{-4}kg/s$. The average volume goodness factor of 1mm straight channel shape was increased by 25% compared to the Zigzag channel.