• Title/Summary/Keyword: 상부 Pool

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Study for Reduction Effect of Pool Top Radiation in Research Reactor by Using Ion Exchanger of Hot Water Layer (고온층계통의 이온교환기에 의한 연구로 수조 상부 방사선의 저감효과에 대한 연구)

  • Park, Yong-Chul;Park, Jong-Ho
    • The KSFM Journal of Fluid Machinery
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    • v.2 no.4 s.5
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    • pp.40-47
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    • 1999
  • A hot water layer (HWL hereinafter) was installed at the depth of 1.2 m from the pool surface to reduce the radiation level at the pool top. After the HWL system was improved by the replacement of the filter with the Ion Exchanger to capture the Na-24, to purify the pool water of HWL and finally to reduce the radiation at the pool top. It was confirmed by the performance test of the pump and the measurement of the pressure difference through the Ion Exchanger and the strainer, that the flow characteristics of HWL system was not adversely affected after the system modification. Also the flow analysis using the pressure loss coefficients of the Ion Exchanger and strainer, calculated by the Darcy formula, could predict the flow variations by pressure changes within $10\%$ error in comparison with the field test results. It was also confirmed that HWL was maintained with the depth of 1.2 m from the pool surface because each electric water heater was electrically and thermodynamically maintained at 30 kW and the temperature of HWL was maintained with $5^{\circ}C$ higher temperature than that of pool water. Finally, it was confirmed that the pool top radiation was saturated and stabilized below 10000 nG/hr within 24 hours as the ion exchanger captured the main nucleus, Na-24 and purified the pool water of HWL.

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Analysis on Pool Temperature Variation along Pool Water Management System Operation in Research Reactor (연구용원자로에서 수조수관리계통 운전에 따른 수조수 온도 해석)

  • Choi, Jungwoon;Lee, Sunil;Park, Ki-Jung;Seo, KyoungWoo
    • Transactions of the KSME C: Technology and Education
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    • v.5 no.2
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    • pp.135-143
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    • 2017
  • The domestic unique research reactor, HANARO (Hi-flux Advanced Neutron Application ReactOr), has been constructed with the open-pool, the core is submerged in, for the multi-purpose neutron application. The reactor has a primary cooling system to remove the fission heat from the core and its connected fluidic systems. Since the works are required at the reactor pool top as a characteristic of the research reactor, the radiation shall be minimized with the operation of the hot water layer system to avoid unnecessary radiation exposure on the workers during work at the pool top. Moreover, the pool water management system is connected to the reactor pool to maintain the pool temperature below $50^{\circ}C$ to minimize the uprising radioactive gas or impurity from the colder pool bottom. For the efficient flow rate of the PWMS, the thermal capacity of heat exchanger is selected with 260 kW in the normal operation condition. In this paper, the modeling is formulated to figure out whether or not each pool temperature maintains below the temperature limit and the calculation results show that the designed PWMS heat exchanger has enough capacity with the design margin regardless of the reactor operation mode.

Seismic Response Analysis of Rectangular Tank with Base-Isolation System (구형 면진유체저장조의 지진시 거동해석)

  • 전영선;최인길;황신일;김진웅
    • Computational Structural Engineering
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    • v.8 no.1
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    • pp.107-113
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    • 1995
  • Spent fuel storage pool should maintain its structural integrity and the safety of stored spent fuels against design earthquake load. In this study, the seismic response analysis of the pool with LRB isolation system is performed for two different earthquakes. To investigate the seismic response of the base isolated pool, the analysis results are compared with the responses of conventional type. In conclusion, the base-isolation system is effective to reduce the seismic forces transmitted to the superstructure and the responses, and to secure the safety of the storage pool and stored spent fuel.

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Reduction Characteristics of Pool Top Radiation Level in HANARO (하나로 수조 방사선 준위의 저감 특성)

  • Park, Yong-Chul
    • The KSFM Journal of Fluid Machinery
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    • v.5 no.1 s.14
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    • pp.49-54
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    • 2002
  • HANARO, 30 MW of research reactor, was installed at the depth of 13m in an open pool. The $90\%$ of primary coolant was designed to pass through the core and to remove the reaction heat of the cote. The rest, $10\%$, of the primary coolant was designed to bypass the core. And the reactor coolant through and bypass the core was inhaled at the top of chimney by the coolant pump to prevent the radiated gas from being lifted to the top of reactor pool. But, the part of core bypass coolant was not inhaled by the reactor coolant pump and reached at the top of reactor pool by natural convection, and increased the radiation lovel on the top of reactor pool. To reduce the radiation level by protecting the natural convection of the core bypass flow, the hot water layer (HWL, hereinafter) was installed with the depth of 1.2 m from the top of reactor pool. As the HWL was normally operated, the radiation level was reduced to five percent ($5\%$) in comparing with that before the installation of the HWL. When HANARO was operated at a higher temperature than the normal temperature of the HWL by operating the standby heater, it was found that the radiation level was more reduced than that before operation. To verify the reason, the heat loss of the HWL was calculated by Visual Basic Program. It was confirmed through the results that the larger the temperature difference between the HWL and reactor hall was, the more the evaporation loss increased. And it was verified that the radiation level above was reduced mote safely by increasing the capacity of heater.

Reduction Characteristics of Pool Top Radiation Level in HANARO (하나로 수조 방사선 준위의 저감 특성)

  • Park, Yong-Chul
    • 유체기계공업학회:학술대회논문집
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    • 2001.11a
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    • pp.221-226
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    • 2001
  • HANARO, 30MW of research reactor, was installed at the depth of 13m of open pool, The $90\%$ of primary coolant was designed to pass through the core and to remove the reaction heat of the core. The rest $10\%$, of the primary coolant was designed to bypass the core. And the reactor coolant through and bypass the core was inhaled at the top of chimney by the coolant pump to protect that the radiated gas was lifted to the top of reactor pool. But, the part of core bypass coolant was not inhaled by the reactor coolant pump and reached at the top of reactor pool by natural convection and increased the radiation level on the top of reactor pool. To reduce the radiation level by protecting the natural convection of the core bypass flow, the hot water layer (HWL, hereinafter) was installed with the depth of 1.2m from the top of reactor pool. As the HWL was normally operated, the radiation level was reduced to five percent ($5\%$) in comparing with that before the installation of the HWL. When HANARO was operated with higher temperature than the normal temperature of the HWL by operating the standby heater, it was found that the radiation level was more reduced than that before operation. To verify the reason, the heat loss of the HWL was calculated. It was confirmed through the results that the larger the temperature difference between the HWL and reactor hall was, the more the evaporation loss was increased. And it was verified that the radiation level above was reduced more safely by increasing the capacity of heater.

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2-D Dynamic analysis method of base-isolated pool structure (면진수조의 2차원 동적 해석기법 개발)

  • 전영선;최인걸;김진웅
    • Computational Structural Engineering
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    • v.8 no.3
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    • pp.67-74
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    • 1995
  • This study develops 2-D analysis method of a base-isolated pool structure, and verifies the method through shaking table test using a scaled model. A wall of the pool structure is modeled as lumped mass, and added mass of the fluid is imposed on the nodes of the structure to consider the hydrodynamic effect of contained fluid. The equation of motion of base-isolated pool structure is obtained by coupling of two equations for superstructure composed of wall and fluid, and for bottom slab and isolator. The scaled model for shaking table test is made with transparent acryle, and 4-high damping laminated rubber bearings are used. The responses of the scaled model by the test are generally good agreement with those by the analysis. It is shown that 2-D analysis method gives somewhat conservative results.

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Development of an Empirical Correlation to Evaluate the Bundle Effect in Saturated Pool Boiling of Water (물의 포화풀비등에서 다발효과를 평가하기 위한 실험식 개발)

  • Kang, Myeong-Gie
    • Transactions of the Korean Society of Mechanical Engineers B
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    • v.41 no.1
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    • pp.1-8
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    • 2017
  • A new empirical correlation was developed for application to the tandem tubes for saturated water at atmospheric pressure. The correlation was obtained by using experimental data and the least square method to calculate the bundle effect. A statistical analysis was performed to identify the suitability of the correlation. The correlation predicted the experimental data within ${\pm}8%$. The applicable ranges of the correlation correspond to a tube pitch of 28.5~114 mm, an elevation angle of $0^{\circ}{\sim}90^{\circ}$, an inclination angle of $0^{\circ}{\sim}90^{\circ}$, and heat fluxes of $0{\sim}120kW/m^2$ of the lower and upper tubes.